PNO-III-87-118, on 870906,reactor Shut Down.Caused by Reactor Trip Due to Various Equipment Malfunctions.Two Valves Removed for Insp & Events & Malfunctions Under Evaluation. Confirmatory Action Ltr Re Plant Startup Will Be Issued: Difference between revisions

From kanterella
Jump to navigation Jump to search
StriderTol Bot change
StriderTol Bot change
 
Line 14: Line 14:
| page count = 2
| page count = 2
}}
}}
{{#Wiki_filter:,                                                                       ._      -    _ _ _ _ _ _ _ _ _ _ .            _ _ _ _ _ _ _ _ _ _ _ .
{{#Wiki_filter:,
PREL_1dNARYNOTIFICATIONOFEVENTORUNUSUALOCCURRENCE--PNO-III-87-118             Date September 8, 1987-This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.                                                                                                                        .
PREL_1dNARYNOTIFICATIONOFEVENTORUNUSUALOCCURRENCE--PNO-III-87-118 Date September 8, 1987-This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.
Facility: Toledo Edison Company Licensee Emergency Classification:
Facility: Toledo Edison Company Licensee Emergency Classification:
Davis Besse Nuclear Plant                   Notification of an Unusual Event 5503 N. State Rte #2                       Alert Oak Harbor, OH 43449                       Site Area Emergency General Emergency Docket No: 50-346                     XX   Not Applicable
Davis Besse Nuclear Plant Notification of an Unusual Event 5503 N. State Rte #2 Alert Oak Harbor, OH 43449 Site Area Emergency General Emergency Docket No: 50-346 XX Not Applicable


==Subject:==
==Subject:==
Line 23: Line 23:
. flow to the steam generators (SG). This resulted in a rapid cooling of the primary coolant,
. flow to the steam generators (SG). This resulted in a rapid cooling of the primary coolant,
) increasing reactivity, and causing the reactor to automatically shut down on high
) increasing reactivity, and causing the reactor to automatically shut down on high
; flux at about 11:42 a.m. Several problems occurred during this event including, but not limited to, the following:
; flux at about 11:42 a.m.
the transfer breaker from station to one of two startup transformers did not function, causing a loss of power to a non-vital bus, shutting down two reactor coolant pumps,                                                   1 and causing loss of power to a vital bus. The associated emergency diesel generator                                                   j started as required,                                                                                                                     i a service water pump did not automatically restart after the vital bus was reenergized l           (it was restarted manually from the control room).
Several problems occurred during this event including, but not limited to, the following:
the transfer breaker from station to one of two startup transformers did not function, causing a loss of power to a non-vital bus, shutting down two reactor coolant pumps, 1
and causing loss of power to a vital bus. The associated emergency diesel generator j
started as required, i
a service water pump did not automatically restart after the vital bus was reenergized l
(it was restarted manually from the control room).
a main steam safety valve failed to reseat fully.
a main steam safety valve failed to reseat fully.
I
I Subsequent to the event, other problems occurred:
!    Subsequent to the event, other problems occurred:
I an operator inadvertently tripped one of the two operating reactor coolant pumps.
I an operator inadvertently tripped one of the two operating reactor coolant pumps.
_ It was restarted immediately in accordance with plant procedures.
_ It was restarted immediately in accordance with plant procedures.
a turbine bypass valve failed open causing a decrease in steam generator level and automatic actuation of the auxiliary feedwater system which functioned properly.
a turbine bypass valve failed open causing a decrease in steam generator level and automatic actuation of the auxiliary feedwater system which functioned properly.
!a         pressurizer level decrease due to the presence of unidentified voids in the decay heat system.
!a pressurizer level decrease due to the presence of unidentified voids in the decay heat system.
The licensee is currently evaluating this event and the various malfunctions. Two steam safety valves (the one which failed to reseat properly and a second one) have been removed for inspection and evaluation.
The licensee is currently evaluating this event and the various malfunctions. Two steam safety valves (the one which failed to reseat properly and a second one) have been removed for inspection and evaluation.
blSTRIBUTION:
blSTRIBUTION:
H. St.                     ED0       NRR         E/W       Willste     Mail: ADM:DMB E*NW Chairman Zech               PA                   IE         NMSS               D0T:Trans only Comm. Roberts               ELD                   OIA       RES Comm. Bernthal                                   AE00                   NRC Ops Ctr Comm. Carr                                                                                                3.' /O_.
i H. St.
l Comm. Rogers l -ACRS                         SP 5.'Il       Regional Offices dud E SECY                                                                                                       d LCA                             INP0 5.'IS           NSAC 5:/6                                               >C d PDR                         RIII Resident Office i P = ae:     E .' 06       (Corp. Office - Reactor Lic. Only)'
ED0 NRR E/W Willste Mail:
l     8709140077 070908 PDR     I&E PNO-II I-B7-118 PDR                                                           _g
ADM:DMB E*NW Chairman Zech PA IE NMSS D0T:Trans only Comm. Roberts ELD OIA RES Comm. Bernthal AE00 NRC Ops Ctr 3.' /O_.
Comm. Carr l Comm. Rogers l -ACRS SP 5.'Il Regional Offices d
E SECY d ud LCA INP0 5.'IS NSAC 5:/6
>C d PDR RIII Resident Office i P = ae:
E.' 06 (Corp. Office - Reactor Lic. Only)'
l 8709140077 070908 PDR I&E PNO-II I-B7-118 PDR
_g


i PRELIM'JARY NOTIFICATION OF EVENT OR UNVSUAL OCCURRENCE--PNO-f!I-87-118     Date September 8, 1987:
PRELIM' ARY NOTIFICATION OF EVENT OR UNVSUAL OCCURRENCE--PNO-f!I-87-118 Date September 8, 1987:
i J
2 Re'gion III management and the Senior Resident Inspector (SRI) monitored the status of the plant throughout the event, and the SRI responded to the-site over the Labor Day Weekend as needed. On Sunday, the day of the event, the licensee verbally agreed not to restart the-reactor without.first contacting the SRI and Region III.
2 Re'gion III management and the Senior Resident Inspector (SRI) monitored the status of the plant throughout the event, and the SRI responded to the-site over the Labor Day Weekend as needed. On Sunday, the day of the event, the licensee verbally agreed not to restart the-reactor without.first contacting the SRI and Region III.
An Augmented Inspection Team, led by a Region III senior manager and supported by NRC Headquarters personnel has-been dispatched to the site (two members of the team are already on site obtaining additional facts). The AIT will have a formal entrance meeting oMWednesday morning, September 9, 1987.                                                             .,
An Augmented Inspection Team, led by a Region III senior manager and supported by NRC Headquarters personnel has-been dispatched to the site (two members of the team are already on site obtaining additional facts).
A Confirmatory Action Letter -(CAL) is being issued by Region III' confirming that thh' plant will not start up without specific authorization from the Regional Administrator or_ hist.3 designee.                                                                               -
The AIT will have a formal entrance meeting oMWednesday morning, September 9, 1987.
Th'e State of Ohio will be notified.                                                         -
A Confirmatory Action Letter -(CAL) is being issued by Region III' confirming that thh' plant will not start up without specific authorization from the Regional Administrator or_ hist.3 designee.
Til .
Th'e State of Ohio will be notified.
  'This information is current as of 3:30 p.m. (EDT) Se ember 8, 1987, and will be updated by the AIT Team Leader from the site as appropriate.-                     ~
Til.
9/     * ''
'This information is current as of 3:30 p.m. (EDT) Se ember 8, 1987, and will be updated by the AIT Team Leader from the site as appropriate.-
~
9/
/
{
CONTACT:
R. DeFayette W.
R. DeFayette W.
                                                      / de {
de 388-5767 388-5574 l
CONTACT:
388-5767                           388-5574 l
4 I
4 I
l I
l I


                                                                                                            ''    o M
o M
N m
N mC3 4 i
C3      i 4
C.3 CC l
C.3                                     _
Z m b
CC                                       _
=>
l                    Z m
v>
                      => v>
r==h l
b r==
h l
1 i
1 i
I
I
                                                                                      . - - - _ _ _ _ _ _ _}}
. - - - _ _ _ _ _ _ _}}


{{PNO-Nav|region=III}}
{{PNO-Nav|region=III}}

Latest revision as of 05:35, 2 December 2024

PNO-III-87-118:on 870906,reactor Shut Down.Caused by Reactor Trip Due to Various Equipment Malfunctions.Two Valves Removed for Insp & Events & Malfunctions Under Evaluation. Confirmatory Action Ltr Re Plant Startup Will Be Issued
ML20238E042
Person / Time
Site: Davis Besse 
Issue date: 09/08/1987
From: Defayette R, Guldemond W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
References
CAL, PNO-III-87-118, NUDOCS 8709140077
Download: ML20238E042 (2)


,

PREL_1dNARYNOTIFICATIONOFEVENTORUNUSUALOCCURRENCE--PNO-III-87-118 Date September 8, 1987-This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.

Facility: Toledo Edison Company Licensee Emergency Classification:

Davis Besse Nuclear Plant Notification of an Unusual Event 5503 N. State Rte #2 Alert Oak Harbor, OH 43449 Site Area Emergency General Emergency Docket No: 50-346 XX Not Applicable

Subject:

REACTOR TRIP DUE TO EQUIPMENT MALFUNCTION; AIT DISPATCHED TO PLANT At about 11:40 a.m. (EDT), September 6, 1987, while the unit was operating at full power, a feedwater flow transmitter failed, causing the integrated control system to increase water

. flow to the steam generators (SG). This resulted in a rapid cooling of the primary coolant,

) increasing reactivity, and causing the reactor to automatically shut down on high

flux at about 11
42 a.m.

Several problems occurred during this event including, but not limited to, the following:

the transfer breaker from station to one of two startup transformers did not function, causing a loss of power to a non-vital bus, shutting down two reactor coolant pumps, 1

and causing loss of power to a vital bus. The associated emergency diesel generator j

started as required, i

a service water pump did not automatically restart after the vital bus was reenergized l

(it was restarted manually from the control room).

a main steam safety valve failed to reseat fully.

I Subsequent to the event, other problems occurred:

I an operator inadvertently tripped one of the two operating reactor coolant pumps.

_ It was restarted immediately in accordance with plant procedures.

a turbine bypass valve failed open causing a decrease in steam generator level and automatic actuation of the auxiliary feedwater system which functioned properly.

!a pressurizer level decrease due to the presence of unidentified voids in the decay heat system.

The licensee is currently evaluating this event and the various malfunctions. Two steam safety valves (the one which failed to reseat properly and a second one) have been removed for inspection and evaluation.

blSTRIBUTION:

i H. St.

ED0 NRR E/W Willste Mail:

ADM:DMB E*NW Chairman Zech PA IE NMSS D0T:Trans only Comm. Roberts ELD OIA RES Comm. Bernthal AE00 NRC Ops Ctr 3.' /O_.

Comm. Carr l Comm. Rogers l -ACRS SP 5.'Il Regional Offices d

E SECY d ud LCA INP0 5.'IS NSAC 5:/6

>C d PDR RIII Resident Office i P = ae:

E.' 06 (Corp. Office - Reactor Lic. Only)'

l 8709140077 070908 PDR I&E PNO-II I-B7-118 PDR

_g

PRELIM' ARY NOTIFICATION OF EVENT OR UNVSUAL OCCURRENCE--PNO-f!I-87-118 Date September 8, 1987:

i J

2 Re'gion III management and the Senior Resident Inspector (SRI) monitored the status of the plant throughout the event, and the SRI responded to the-site over the Labor Day Weekend as needed. On Sunday, the day of the event, the licensee verbally agreed not to restart the-reactor without.first contacting the SRI and Region III.

An Augmented Inspection Team, led by a Region III senior manager and supported by NRC Headquarters personnel has-been dispatched to the site (two members of the team are already on site obtaining additional facts).

The AIT will have a formal entrance meeting oMWednesday morning, September 9, 1987.

A Confirmatory Action Letter -(CAL) is being issued by Region III' confirming that thh' plant will not start up without specific authorization from the Regional Administrator or_ hist.3 designee.

Th'e State of Ohio will be notified.

Til.

'This information is current as of 3:30 p.m. (EDT) Se ember 8, 1987, and will be updated by the AIT Team Leader from the site as appropriate.-

~

9/

/

{

CONTACT:

R. DeFayette W.

de 388-5767 388-5574 l

4 I

l I

o M

N mC3 4 i

C.3 CC l

Z m b

=>

v>

r==h l

1 i

I

. - - - _ _ _ _ _ _ _