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{{Adams
#REDIRECT [[IR 05000395/1989013]]
| number = ML20246A534
| issue date = 08/04/1989
| title = Insp Rept 50-395/89-13 on 890701-31.Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification,Action on Previous Insp Findings & Other Areas
| author name = Cantrell F, Hopkins P, Prevatte R
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =
| addressee affiliation =
| docket = 05000395
| license number =
| contact person =
| document report number = 50-395-89-13, NUDOCS 8908230003
| package number = ML20246A526
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 8
}}
See also: [[see also::IR 05000395/1989013]]
 
=Text=
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            >
                        > Report No.':: 50-395/89-13:                                          A
                          Licensee:. South Carolina Electric & Gas Company ^
                                                  Columbia, SC 29218
G
                          Docket No.:":50-395                                                          License No.: NPF-12.
      .                                                                                                                      .
                          Facility Name':                  V. C. Summer
                                                                      .
                          Inspection Conducted:.-July;1                            .31,<1989
                            Inspectors:
                                                ~
                                                        b
                                                  R. 'L.- Prevatte
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                                                                                                                      Date' Signed
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    l                                                    @h,idd A                                                        7A//89
                                                                                                                          ~
                                                  P.  C'.    Hopkins                                                Date Signed.  -
g                                                                                  Ug / ' '
                          Approved by:                            Ms
                                                      F.1 .~ Cantrell, Secti                    ef
                                                                                                                      I/
                                                                                                                      Da,te Signed
                                                                                                                                  N
*            '
                                                    ' Division of Reactor Pr ects
              '
    ..
                                                                                          SUMMARY
                          Scope:
                          This routine inspection was conducted.by the resident inspectors onsite in the
                          areas of' monthly surveillance, observations, monthly maintenance observation,
                          operational: safety verification, action' on previous inspection findings,' and:
                          other areas.' Certain tours were conducted'on backshifttor weekends. Backshift
                          or weekend tours were conducted on July 11, 12, 13, 18, 19. 23,'24, 25 .and 26,
                          1989.-
                          Results:
                          The unit began the month at 100 percent power. A trip from 100 percent power
                          occurred.on July 11, 1989, as the result.of a maintenance technician shorting.
      +                ' out a power supply- for the generator stator water cooling system. The unit
                          trip and SCE&G grid heavy loading resulted in a loss of offsite power with a
                          transfer. of the. safety related buses to the emergency diesel generators,
                          paragraph 4.b.                    The unit was restarted and returned to power on July 13, 1989.=
l        ,                It ' operated at full ' power for the remainder of the' month.- The areas of
                          maintenance and: surveillance continue to' perform satisfactorily. A violation
                          for failure to control the temporary installation of portable demineralizers
                          was identified, paragraph 4.c. The licensee's evaluation 'of this event
                          determined that' although a seismic event could effect the operation of safety
                          equipment, the affected systems would still continue to operate satisfactorily.
                              8908230003 890804
                              FDR        ADOCK 05000395
                              Q                                  FDC
                  -
                                                    _            __      -                _                                          O
 
-                                            _                                _
                                                                                          _ .-
  .
            -
.:  .
              ,
        a
                                                                                                j
                                            REPORT DETAILS
          1.-    Persons Contacted
                Licensee Employees
                W. Baehr, Manager, Chemistry and Health Physics
                C. Bowman, Manager, Scheduling and Modifications                                !
              *0. Bradham, Vice President, Nuclear Operations
                M. Browne, Manager, Systems Engineering & Performance
                W. Higgins, Supervisor, Regulatory Compliance
                S. Hunt, Manager, Quality Systems
              *A. Koon, Manager, Nuclear Licensing
                G. Moffatt, Manager, Maintenance Servic2s
                D. Moore, General Manager, Engineering Services
              *K. Nettles, General Manager, Nuclear Safety
                C. Price, Manager, Technical Oversite                                          '
                M. Quinton, General Manager, Station Support
                J. Shepp, Associate Manager, Operations
                J. Skolds, General Manager, Nuclear Plant Operations
              *G. Soult, General Manager, Operations and Maintenance
                      .
                G. Taylor, Manager, Operations
                D. Warner, Manager, Core Engineering and Nuclear Computer Services
              *M. Williams, General Manager, Nuclear Services
                K. Woodward, Manager, Nuclear Operations Education and Training
                Other licensee employees . contacted included engineers, technicians,
                operators, mechanics, security force members, and office personnel.
              * Attended exit interview
                Acronyms and initialisms used throughout this report are listed in the
                last paragraph.
          2.    Monthly Surveillance Observation (61726)
                The inspectors observed surveillance activities of safety related systems
                and components to ascertain that these activities were conducted in
                accordance with license requirements. The inspectors observed portions of
                35 selected surveillance tests including all aspects of Reactor Building      !
                Closecut Inspection, STP 109.001. The inspectors verified that required
                administrative approvals were obtained prior to initiating the test,
                testing was accomplished by qualified personnel, required test instruments-
                tion was properly calibrated, data met TS requirements, test discrepancies
                were rectified, and the systems were properly returned to service. The
                licensee demonstrated good communication between test technicians and          i
                control room personnel during performance of test procedures. The
                materials, parts, components and test equipment used were found to be            l
                correct and documented properly. Technicians had procedures available at
                                                                                                  '
                all times and utilized them properly.
                No violations or deviations were identified.
                                                                                                  i
      _            --  - - _                                                                  l
 
                                                                                                _ _ _
  r  ,
              -
    .  .
                ,
          ,
<                                                        2
a
            3. .  Menthly Maintenance Observation (62703)
                  The inspectors observed maintenance activities of safety related systems
                  and components to ascertain that these activities were conducted in
                  accordance with approved procedures, TS, industry codes and standards.
                  The inspectors determined that the procedures used were ' adequate to
                  control the activity, and that these activities were accomplished by
                  qualified personnel.    The inspectors independently verified that the
                  equipment was properly tested before being returned to service.
                  Additionally, the inspectors reviewed several outstanding job orders to
                  determine that the licensee was giving priority to safety related
l:                maintenance and not developing a backlog which might affect a given
                  system's performance. The operational maintenance activities observed by
'
                  the inspectors during this report were judged.to be satisfactory.        It
                  appears that with the installation of control room barriers and a new
                  tagging desk in the control room, the traffic in the critical areas of the
                -control room has been reduced. This has also resulted in ' smoother
                  processing of MWR's, STP's and other maintenance activities through. the
                  control room.      The following specific maintenance activities were
                  observed:
                  MWR 87C00it          Replace regulator for demineralized instrument air
                                        supply
                  MWR 8901080          Repair controller on hydrogen analyzer
                  MWR 8901211          Calibrate pressurizer control channels 444C & 444D
                  PMTS 115543          Repair air intake transmitter for SW building
                  MWR 89G0095          Repair smoke detectors
                  PMTS 112043          Repair discharge flow transmitter on C FW booster pump
                  PMTS 116745          Calibrate heater coil temperature controller in
                                        auxiliary building supply plenum
                  PMTS 118844          Calibrate temperature element on SW building pump room
                  MWR 88E0125          Repair flexible conduit to smoke analyzer
                  MWR 88E0108          Test and replace smoke analyzer
                  PMTS 117045          Calibrate temperature alarm on SW booster pump
                  MWR 8956808          Remove necessary parts and reinstall torque motor            j
                  PMTS 122056          Perform inspection on open cycle cooling water booster
                                        pump A                                                      1
                                                                                                      J
 
                                          .  __ _    _ _-
                                      ..
  .                                    .
                                                  .
                                            4
                                                                                              3
                                                    PMTS 122063              Rotate turbine on closed cycle cooling water pump A
                                                    PMTS 121916              Verify alignment of 480V breakers
                                                    PMTS 121917              Electrical adjustment on 7.2kV switchgear treaker
                                                    PMTS 119740              Inspection of FW pump turbine
                                                    MWR 8901221              Repair posit.an indication circuitry on pressurizer
                                                                              sample header isolation valve
                                                    MWR 87G0095              Repair sample detection line
                                                    PMTS 122395              Vibration analysis check on RHR pump A
                                                    PMTS 121729              Vibration analysis check on EFW pump A
                                                    PMTS P122139              Audit misalignment log
                                                    PMTS P122104              Inspect 7.2kV switchgear breakers
                                                    No violations or deviations were identified.
                                              4.  Operational Safety Verification (71707)
                                                    a.        The inspectors toured the control room, reviewed plant logs and
                                                              records and held discussions with plant staff personnel to verify
                                                              that the plant was being operated safely and in conformance with
                                                              applicable requirements. Specific items inspected in the control
                                                              room included: adequacy of staffing and attentiveness of control room
                                                              personnel, TS and procedural adherence, operability of equipment and
                                                              indicated control room status, control room' logs, tagout books,
                                                              operating orders, jumper / bypass controls, computer printouts and
                                                              annunciators. Tours of other plant areas were conducted to verify
                                                              equipment operability, control of ignition sources and co,mbustible
                                                              materials, the condition of fire detection and extinguishing
                                                              equipment, the control of maintenance and surveillance cctivities in
                                                              progress, the implementation of radiation protective controls and the  i
                                                              physical security plan.      Tours were conducted during normal and
                                                              random off-hour periods.
                                                    b.        On July 11,1989, at 2:35      p.m., the unit tripped from 100 percent
                                                              power.    The trip resulted from an I&C technician shorting a wire
                                                              while reconnecting a thermocouple inside the stator water cooling
                                                              control cabinet. The short circuit blew the power supply fuses and
                                                              resulted in a low flow signal on stator water cooling.      The normal
l                                                            protective action would have resulted in a turbine run back. This
!                                                            circuit did not function correctly and resulted in a turbine trip and
                                                              reactor trip.
                                                                                                                                      I
                                                                                                                                      1
                                                                                                                                    1
  _ _ _ _ _ _ _ _ _ _ _ _ . . _ _ _ _                      _                                                                        a
 
                -                                      ---
    4
        '
                  %                    vg
                                .
                                                                                        4
              ,
                                                      At the time of.the' reactor trip the utility. grid was' experiencing.a
                                                      high load of approximately 3100.MW's. This loss of-the 900 MW's
                                                            ~
                                                                                                                            .
H          ,
                                                      being generated by Summer resulted in allarge voltage oscillation
                                                      which actuated protective relays that 'also ' tripped 4 pumped storage
                                                      units at the Fairfield Pumped Storage Facility (approximately 250MW) -
                                                                                                ~
      ,
                                                      3 units'~ at the. Saluda Hydro (approximately 135MW), and both fossil
                                                      generating ' units at~ McMeekin Station (approximately 250MW). '.These
                                                      losses resulted in the 230kV offsite power source to Summer dropping
                                                      -to approximately 203kV and the 115kV source dropping to approximately-
                                                      100kV. .This . low voltage condition actuated the undervoltage' relays -
l                                                    which automatically separated the 7200 volt ESF buses from offsite
                                                      power. This started the emergency diesel' generators and placed the
,
'
                                                      safety related buses on the' diesel generator. The non-safety service
                                                      buses remained connected to the degraded offsite power source and
                                                      continued to operate throughout the event. at reduced voltages, . An
'
                                                      unusual event was declared at 3:10 p.m. due to the loss of both
                                                      offsite power sources. The system voltage was returned to normal and.
                                                      thel safety related buses were reconnected to offsite power at
                                                      approximately 5:00 p.m. The DG's'were' secured and the unusual event
                                                      was terminated at 5:11 p.m.
,
                                                      Further investigation by the licensee revealed that the MVAR loading
                                                      of Summer, the, grid MVAR distribution at the time of the unit trip
                                                      and lower.than normal setpoints on some generator back-up protection.
                                                      relays: may have led to this event.        The licensee has developed
                                                      administrative - guidelines to . provide for - improved system MVAR
                                                      distribution that should reduce the probability of future similar
                                                      occurrences. After completing all necessary repairs and implementing
                                                      the'above step, the unit was restarted.on July 12, 1989, and returned
                                                      to power operation on July 13,1989.          The licensee is currently
                                                      preparing a LER on this event.- The event will also be discussed.
                                                      during a meeting scheduled for August 1, 1989. at NRC headquarters.
                                                  c. While. conducting a routine walkdown of the plant on July 6, 1989 -the
                                                      inspectors discovered two temporary demineralizers on the 412
                                                      elevation of the intermediate building. These units are 24 inches in
                                                      diameter and approximately six feet high and are configured to stand    'l
                                                      in an upright position.      The weight of each of the components is
                                                      approximately 1750 lbs. The support for.these units was a 1/2-inch
                                                      sisal' rope which attached these units to two EFW line supports and a
                                                      SW line support. A concern with the effects of this installation on
                                                      the operability of the SW and EFW system and nearby safety-related
                                                      components during a seismic event was immediately discussed with the
                                                      operations shift supervisor. The shift supervisor immediately had
                                                      these units removed from the area and documented this in off-normal
                                                      occurrence 89-058 and NCN 3386.
.
- _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _
 
                                  . _ - - _ _ - .
                                                    .
g                              .
                                                      .
                                                  .
                                                                                              5
                                                          Further investigation into this item revealed that these units had
                                                          been installed on June 1, 1989, to permit draining of the SG while the
                                                          plant was in Mode 5. This installation was accomplished without a
                                                          MWR as required by the Station Housekeeping and plant Inspection
                                                          Program Procedure SAP 142, and Conduct of Maintenance Procedure
                                                          SAP-300.    The unit was restarted on June 11,-1989 with the units
                                                          still in place. This installation had been noted by plant management
                                                          and directions had been given to remove the units on or around June 20,
                                                            1989.
                                                            In this instance personnel were deficient in not performing this work
                                                          under the licensee MWR program.        No documentation to require
                                                          engineering review of this temporary installation was performed as
                                                            required by SAP 142. The above procedure was also inadequate in that
                                                            it did not insure that a seismic evaluation of the installation be
                                                            performed and that time limits were established to insure removal of
                                                            this hazard prior to plant start-up.      This is contrary to the
                                                            requirement of TS 6.8.1.a which requires that procedures be
                                                            established, implemented and maintained for activities referenced in
                                                          Appendix A of Regulatory Guide 1.33, Revision 2 February 1972.
                                                          This is 'a violation, " Failure to Control Temporary Installations,"
                                                            89-13-01.
                                                            The licensee has performed an evaluation which determined that a
                                                            seismic event could have resulted in the portable demineralized
                                                            becoming mobile and possibly damaging two FW line supports and
                                                            shearing off a test connection on a CCW line and a drain line'in the
                                                            SW system. The failure of the EFW supports would not have resulted in
                                                            the system becoming inoperable and the loss of flow in the SW and CCW
                                                            system would not have degraded system flow below the worst case
                                                            analyzed values. The potential flooding from the lines were well
                                                            within the capacity of space dewatering equipment. This analysis
                                                            determined that all systems would remain operable.
                                                            This event is similar to a licensee identified violation that was
                                                            documented in inspection report 89-03. In that event temporary
                                                            scaffolding had been erected for shielding of RHR piping to reduce
                                                            personnel radiation exposure while the plant was in a refueling
                                                            outage. Due to procedural deficiencies and personnel errors the
                                                            scaffolding was not removed prior to plant start-up.          That
                                                            installation had the potential to impact on system operability.
                                                            The licensee, in their response to this violation, should address
                                                            procedural changes made to insure that temporary installations are
                                                            controlled and that dates or mode restraints are established to
                                                            insure that temporary installations which are required while the
                                                            plant is shutdown are removed prior to unit start-up.
                                                        Violations cr deviations were identified.
  - _ _ _ _ - - _ _ - - _ - _ _ - _ - _ _ _ _ - -                            _ _ _ _ _ _ . ._-                                    i
 
-        __                                        _
    .    x
  . '. .              +
                                      ,
        .
                                                                                      6
            5.                              Action on Prev ous Inspection Findings (92701, 92702)
                                                (Closed) TI2513/94, Inspection for verification of licensee changes made
                                              to comply with PWR moderator dilution requirements, multi-plant action
                                                item 13-03. The inspector reviewed inspection requirements specified.in
                                              this instruction and reviewed the V. C. Summer Safety Evaluation Report and
                                              supplements to determine what requirements had been established. This
                                              review identified that dilution events and- preventive measures were
                                              discussed and resolved in section 15 of the SER and in supplements 1 and 3
                                                to the SER. However, multi-plant action item B-03 was not specifically
                                              discussed.      Discussion with Mr. L. Kopp, the NRR lead contact for.this
                                                item, indicates thut this item is not applicable for V. C. Summer. The
                                                SIMS open item list for V. C. Summer also does not list this item. Further
                                              discussion with Mr. Kopp revealed that since V.C. Summer was licensed in
                                                1982, this issue would have been resolved in the normal licensing process
                                                for V. C. Summer and all other plants licensed after 1979. Based on the
                                                above, this item is administratively closed.
            6.                                Other Areas
                                              The inspectors-toured the licensee's lead dispatch center in Columbia, SC
                                                on July 25, 1989. Computer control and indication systems and procedures
                                                that are used to operate' and control SCE&G's grid was discussed in detail.
                                                This tour was very beneficial and provided the inspectors with a better
                                                understanding of this tystem.
            7.                                ExitInterview(30703)
                                                The inspection scope and findings were summarized on July 31, 1989, with
                                                those persons indicated in paragraph 1. The inspectors described the
                                                areas inspected and discussed the inspection findings. The plant trip and
                                                the resulting offsite power loss event which occurred on July 11, 1989, was
                                                discussed in detail. This included the short term corrective measures and
                                                the current investigation into root cause and long term corrective action.
                                                The violation which resulted from the failure to control the temporary
                                                  installation of portable demineralizers in the intermediate building was
                                                attributed to procedural inadequacies and a failure to follow procedures.
                                                  It was also noted that the violation was similar to LIV 89-03-01 when the
                                                  plant was restarted without removing scaffolding that contained temporary
                                                  shielding. No dissenting comments were received from the licensee. The
                                                licensee did not identify as proprietary any of the materials provided to
                                                or reviewed by the inspectors during the inspection.
            8.                                  Acronyms and Initialisms
                                                  CCW        Component Cooling Water
l                                                DG        Diesel Generator                                                ,
                                                  EFW        Emergency Feedwater
                                                  FW        Feedwater
L-            _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ - _ - _ _ _
                                                                                                                              \
 
                              --_                  ,
  L
                                  '*
        ..- -                      ,    :. ,
                                      .-
                                                                                7
o
L
                                                I&C  Instrumentation and Control
                                                MW    Megawatt.
                                              - MWR  Maintenance Work Request
                                                MVAR  Million Volt Amps Reactive
                                                NCN  Non-Conformance Notice
i                                              NRC  Nuclear Regulatory Commission
                                                NRR  Nuclear Reactor Regulation
                                                PMTS  Preventive Maintenance Task Sheet
                                              - QC    Quality Control
                                                RHR  Residual Heat Removal
                                                SAP  Station Administrative Procedure
                                                SCE&G South Carloina Electric & Gas Company
                                                SER  Safety Evaluation Report
                                                SG    Steam Generator
                                                SIMS  Safety Issues Management Systems
                                                STP  Surveillance Test Procedures
                                                SW    Service Water
                                                TS    Technical Specifications
,
----________-______m_______m____
}}

Revision as of 18:25, 24 January 2022