ML20009C729: Difference between revisions
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$A S % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION I115 I W@ l 0 l 816 l@l NA l lBl@l Inservice. Inspe: tion 1 ACTIVITY CO TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE RELEASE l | $A S % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION I115 I W@ l 0 l 816 l@l NA l lBl@l Inservice. Inspe: tion 1 ACTIVITY CO TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE RELEASE l | ||
[1.,J.6.J l Zj @D OF RELEASE NA l Z.j@l l. l NA PERSONNEL EXPOS ES NUMBER TYPE DESCRIPTION I117 l l Ol Ol0 l@l_Zj@l NA l PERSONNEL NJU IES NUM8ER DESCRIPTION NA l 11 la l I Ol Ol Ol@l12 80 7 8 9 11 LOSS OF OR DAMAG TO FACILITY I | [1.,J.6.J l Zj @D OF RELEASE NA l Z.j@l l. l NA PERSONNEL EXPOS ES NUMBER TYPE DESCRIPTION I117 l l Ol Ol0 l@l_Zj@l NA l PERSONNEL NJU IES NUM8ER DESCRIPTION NA l 11 la l I Ol Ol Ol@l12 80 7 8 9 11 LOSS OF OR DAMAG TO FACILITY I | ||
1 9 (_2j@l NA 80 7 8 9 to 8107210405 910709 NRC USE ONLY DR ADOCK 05000366 ISSu OE CRIPTION @ PDR | 1 9 (_2j@l NA 80 7 8 9 to 8107210405 910709 NRC USE ONLY DR ADOCK 05000366 ISSu OE CRIPTION @ PDR ((;;;gl;;; ; ; l7 1.3 l oJ LSe81 10 1, ,, , | ||
68 69 80 5 | 68 69 80 5 | ||
.7 #1 3 | .7 #1 3 | ||
Revision as of 12:03, 15 March 2020
| ML20009C729 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 07/09/1981 |
| From: | GEORGIA POWER CO. |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML20009C724 | List: |
| References | |
| LER-81-059-03L-01, LER-81-59-3L-1, NUDOCS 8107210405 | |
| Download: ML20009C729 (2) | |
Text
. __ .
NRC FOZM 366 U. S. NUCLEAR REGULATCRY COMMISSION
-(7 77h LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI CONTROL BLOCK: l i
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7 6 9 LICENSEE CODE 14 l' CON'T 1o111 7 8 SM I 60Li@l 0151 olo 61 I 01316 I 668l@l69 016121218111@l017101918 DOCKET NUMBER EVENT DATE 74 75 REPORT DATE Il80l@
EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h 10 l21 l While coeratina at 210R MWt HNP-2-10RO. Surveillanco C h o c k <: . wat ner- I lo ia l I formed. This procedure revealed a defective transmitter 2T48-N0101A in I
.lo 141 I the ocstaccident torus water level indicator 2T48-R622A. Plant operationl lo is t I was not affected as a result of this event. The health and safety of I lo is] I the oublic was not affected. This is a nonrecetitive event. A ceneric 1 10171 I review revaaled that Unit 1 uses a different tvoe of indicator. I e
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44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i
l i 101 1 Th e cause of this event has been a tt ri b ute[i to low fluid level in the 11 111 I reference lea sensino line. MR 2-R1-9793 was w ri tt en tn backfill the I u_ilj1 low sensino line on the t; ansmitter. The indicator was declared ooera- I W ltive and returned to service. I l
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$A S % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION I115 I W@ l 0 l 816 l@l NA l lBl@l Inservice. Inspe: tion 1 ACTIVITY CO TENT AMOUNT OF ACTIVITY LOCATION OF RELEASE RELEASE l
[1.,J.6.J l Zj @D OF RELEASE NA l Z.j@l l. l NA PERSONNEL EXPOS ES NUMBER TYPE DESCRIPTION I117 l l Ol Ol0 l@l_Zj@l NA l PERSONNEL NJU IES NUM8ER DESCRIPTION NA l 11 la l I Ol Ol Ol@l12 80 7 8 9 11 LOSS OF OR DAMAG TO FACILITY I
1 9 (_2j@l NA 80 7 8 9 to 8107210405 910709 NRC USE ONLY DR ADOCK 05000366 ISSu OE CRIPTION @ PDR ((;;;gl;;; ; ; l7 1.3 l oJ LSe81 10 1, ,, ,
68 69 80 5
.7 #1 3
O LER #: 50-366/1981-059 Licensee: Georgia Power Company Facility Name: Edwin I. Hatch Docket #: 50-366 Narrative Report for LER 50-366/1981-059 On 6-22-81, while oper.ating at 86% power, HNP-2-1050, Daily Channel Surveillance Checks, was performed. This procedure revealed that the postaccident torus water level indicator 2T48-R622A was reading approximately 25 inches higher than the redundant indicator 2T48-R622B. The indicator was declared inoperative per Tech Specs section 3.3.6.4.a. This is a nonrepetitive event. The cause of this event has been attrib-uted to low fluid level in the reference leg sensing line. MR 2-81-2723 was written to backfill the low sensing line on transmitter 2T48-N0101A. The indicator was declared operative and returned to service.
Plant operation was not affected as a result of this event.
The health and safety of the public was not affected. A generic review revealed that Unit 1 uses a different type of indicator.
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