ML20054G329: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot insert)
 
(StriderTol Bot change)
Line 1: Line 1:
{{Adams
#REDIRECT [[05000272/LER-1982-034]]
| number = ML20054G329
| issue date = 06/07/1982
| title = Forwards LER 82-034/03L-0.Detailed Event Analysis Encl
| author name = Midura H
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name = Haynes R
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000272
| license number =
| contact person =
| document report number = NUDOCS 8206210444
| package number = ML20054G330
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| page count = 3
}}
 
=Text=
{{#Wiki_filter:.
* O          >SEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station June 7, 1982 Mr. R. C. Haynes Regional Administrator USNRC Region 1 631 Park Avenue King of Prussia, Pennsylvania                    19406
 
==Dear Mr. Haynes:==
 
LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE              82-034/03L Pursuant to the requirements of Salem Generating Station
      . Unit No. 1, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 82-034/03L. This report is required'within thirty (30) days of the occurrence.
Sincerely yours,
                                                              }}..h{IA "
H. J. Midura General Manager -
Salem Operations RF:ks h
CC:    Distribution B206210444 820607
{DRADOCK 05000272     PnR The Energy People f[M                l r m wonw
 
r-l    Report Number:      82-034/03L Report Date:        06-07-82 Occurrence Date: '05-10-82
                                        ~
Facility:          Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge,.New Jersey    08038 IDENTIFICATION OF OCCURRENCE:.
No. 14 Steam Generator Wide Range Level - Inoperable.
This report was initiated by Incident Report 82-127.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 - Rx Power 98% - Unit Load 1110 MWe.
DESCRIPTION OF OCCURRENCE:
On May 10, 1982 during routine operation, the Control Room Operator noticed the No. 14 Steam Generator Wide Range. Level indication had failed low. The channel was declared inoperable at 0415 hours, and Limiting Condition for Operation 3.3.3.7 Action 1 was entered.
This occurrence constituted operation in a degraded mode in accordance with Technical-Specification 6.9.1.9.b.
l    DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
l The failure of No. 14 Steam Generator Wide Range Level Instrument was due to a loose fuse in the power supply.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.3.3.7 Action 1 requires:
With the number of operable accident monitoring channels less than'the required number of channels, restore the inoperable channel (s) to operable status within 7 days, or be in hot shutdown within the next 12 hours.
l l
s
 
s LER 82-034/03L                        CORRECTIVE ACTION:
The loose fuse was properly-tightened, and the instrument was satisfactorily tested. At 0450 hours, No. 14 Steam Generator Wide Range Level Instrument was declared operable, and Limiting Condition for-Operation 3.3.3.7 Action 1 was terminated.
FAILURE DATA:
Not Applicable Prepared By    R. Frahm                      /!,  ,
                                                              < ec~
General Manager -
Salem Operations SORC Meeting No. 82-57 i
l
,}}

Revision as of 07:15, 15 March 2020