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{{#Wiki_filter:ENT000343  
{{#Wiki_filter:ENT000343
Submitted: March 29, 2012
                                                                            Submitted: March 29, 2012
UNITED STATES NUCLEAR REGULATORY  
                                            UNITED STATES
COMMISSION  
                                NUCLEAR REGULATORY COMMISSION
REGION I Mr. Joseph Pollock Site Vice President  
                                                REGION I
Entergy Nuclear Operations, Inc. Indian Point Energy Center 450 Broadway, GSB P.O. Box 249 Buchanan, NY 10511-0249  
                                          475 ALLENDALE ROAD
4 7 5 ALLENDALE
                                      KING OF PRUSSIA, PA 19406-1415
ROAD KING OF PR USSIA, PA 19406-1415
                                                  October 19, 2009
October 19, 2009 SUBJECT: INDIAN POINT NUCLEAR GENERATING
Mr. Joseph Pollock
UNITS 1 ,2 & 3 -NRC INSPECTION  
Site Vice President
REPORT NOS. 05000003/2009008
Entergy Nuclear Operations, Inc.
; 05000247/2009008
Indian Point Energy Center
; AND 05000286/2009008  
450 Broadway, GSB
Dear Mr. Pollock: On September  
P.O. Box 249
4, 2009, the U.S. Nuclear Regulatory  
Buchanan, NY 10511-0249
Commission (NRC) completed  
SUBJECT:        INDIAN POINT NUCLEAR GENERATING UNITS 1, 2 & 3 - NRC INSPECTION
an inspection  
                REPORT NOS. 05000003/2009008 ; 05000247/2009008; AND
at Indian Point Nuclear Generating  
                05000286/2009008
Units 1, 2, & 3. The enclosed report documents  
Dear Mr. Pollock:
the inspection  
On September 4, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
results, which were discussed  
inspection at Indian Point Nuclear Generating Units 1, 2, & 3. The enclosed report documents
on August 19 and September  
the inspection results, which were discussed on August 19 and September 4, 2009, with Mr. Don
4 , 2009 , with Mr. Don Mayer and other members of your staff. The purpose of this inspection  
Mayer and other members of your staff.
was to assess the establishment, implementation, and maintenance  
The purpose of this inspection was to assess the establishment, implementation, and
of your Long-Term  
maintenance of your Long-Term Groundwater Monitoring Program ; review the circumstances
G r oundwater
surrounding a previously identified occurrence involving the detection of tritated water in a Unit 3
Monitoring  
storm drain system; review the performance of the site's Radiation Monitoring System; and
Program; review the circumstances  
inspect and assess your performance relative to radiological effluents monitoring and control.
surrounding  
The inspection involved an examination of activities conducted under Entergy's license as
a prev i ously identified  
related to safety and compliance with the Commission's rules and regulations and with the
occurrence  
conditions of your license. Within these areas, the inspection consisted of a selected
involving  
examination of procedures and representative records, observations of activities, interviews with
the detection  
personnel, and independent assessment activities.
of tritated water in a Unit 3 storm drain system; review the performance  
Based on the results of this inspection, no findings of significance were identified . Further, the
of the site's Radiation  
inspectors determined that Entergy's Long-Term Groundwater Monitoring Program for the .lndian
Monitoring  
Point Energy Center was effectively implemented and maintained in a manner that provided
System; and inspect and assess your performance  
continued radiological monitoring of the groundwater conditions to confirm conformance with
r elative to radiological  
NRC regulatory requirements relative to the maintenance of public health and safety, and
effluents  
protection of the environment.
monitoring  
Since 2005, as approved by NRC's Executive Director of Operations, Region I conducted
and control. The inspection  
frequent and focused reviews of your groundwater investigation activities and long-term
involved an examination  
monitoring program that exceeded the scope of NRC's normal baseline inspection program. As
of activ i ties conducted  
a result, we have developed confidence in your commitment and ability to continue effective
under Entergy's license as related to safety and compliance  
monitoring and assessment of the on-site conditions to assure the maintenance of
with the Commission's  
rules and regulations  
and with the conditions  
of your license. Within these areas, the inspection  
consisted  
of a selected examination  
of procedures  
and representative  
records, observations  
of activities , interviews  
with personnel, and independent  
assessment  
activities.  
Based on the results of this inspection , no findings of significance  
were identified. Further, the inspectors  
determined  
that Entergy's Long-Term  
Groundwater  
Monitoring  
Program for the.lndian Point Energy Center was effectively  
implemented  
and maintained  
in a manner that provided continued  
radiological  
monitoring  
of the groundwater  
conditions  
to confirm conformance  
with NRC regulatory  
requirements  
relative to the maintenance  
of public health and safety, and protection  
of the environment.  
Since 2005 , as approved by NRC's E x ecutive Director of Operations , Region I c onducted frequent and focused reviews of your groundwater  
investigation  
activities  
and long-term  
monitoring  
program that exceeded the scope of NRC's normal baseline inspection  
program. As a result, we have developed  
confidence  
i n your commitment  
and ability to continue effective  
monitoring  
and assessment  
of the on-s i te cond i tions to assure the maintenance  
of
J. Pollock 2 public health and safety, protection
of the environment, and conformance
with NRC regulatory
requirements.
Our inspectors
confirmed
that the objectives
specified
in our deviation
memorandum
dated December 16,2008 (ML083590057)
have been satisfied.
However, we will continue to monitor your performance
in this area , and will re-assess
the need for continued
heightened
inspection
oversight
during our end-of-cycle
review of your CY 2009 perfonmance.
In accordance
with 10 CFR2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure
will be available
electronically
for public inspection
in the NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is accessible
from the NRC Web site at
rm/adams.html (the Public Electronic
Reading Room).
Darrell J. Roberts, Director Division of Reactor Safety Docket Nos: 50-003, 50-247, 50-286 License Nos: DPR-5, DPR-26, DPR-64 Enclosure:
Inspection
Report Nos. 05000003/2009008, 05000247/2009008, 05000286/2009008
w/Attachment:
Supplemental
Information
cc w/encj: Distribution
via ListServ 
J. Pollock 2 public health and safety , protection
of the environment, and conformance
with NRC regulatory
requirements. Our inspectors
confirmed
that the objectives
specified
in our deviation
memorandum
dated December 16, 2008 (ML083590057)
have been satisfied.
However, we will continue to monitor your performance
in this area, and will re-assess
the need for continued
heightened
inspection
oversight
during our end-of-cycle
review of your CY 2009 performance.
In accordance
with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure
will be available
electronically
for public inspection
in. the NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is access i ble from the NRC Web site at hllp: llwww.nrc.
rm/adams.html (the Public Electronic
Reading Room). Sincerely, IRA by Peter R. Wilson forI Darrell J. Roberts, Director Divis i on of Reactor Safety Docket Nos: 50-003 , 50-247 , 50-286 License Nos: DPR-5, DPR-26, DPR-64 Enclosure:
Inspection
Report Nos. 05000003/2009008, 05000247/2009008, 05000286/2009008 w/Allachment:
Supplemental
Information
cc w/encl: Distribution
via ListServ Distribution
w/encl: (via E-mail) S. Collins, RA (R10RAMAIL
RESOURCE)
M. Dapas, DRA (R10RAMAIL
RESOURCE)
D. Lew, DRP (R1 DRPMAIL RESOURCE)
J. Clifford, DRP (R1DRPMAIL
RESOURCE)
L. Trocine , Ri OEDO RIDSNRRPMINDIANPOINTRESOURCE
B. Welling, DRP B. Bickell, DRP S. McCarver , DRP G. Malone , DRP , Senior Resident Inspector
-Indian Point 2 D. Hochmuth , DRP D. Bearde, DRP Region I Docket Room (w/concurrences)
ROPreport
Resource D. Roberts , DRS P. Wilson, DRS J. White, DRS SUNSI Review Complete:
JRW (Reviewer's
Inrtials) OOCUMENT NA M E: G:I ORS I P la nt S upport B ranch 2 INoggl e II P 2009008 Re v1.do c After declaring
thi s document Offi c ial Agency Rec o rd w it will be rel ea s e d to the Pub lic. To receive a copy of this document, Indicate in the box: "e" = C Opy without attachm en t/enclosure "E" = COpy with atta c hment/enclosur
e "N" = No CQP"y OFFICE RIIDRS I RES I RIIDRS I RIIDRP I RIIDRS I NAME JNoggle/JDN TNicholsonltjn
JWhite/jrw'
ehg BWeliinglBW
DRoberts/prw
for (telecon)
for' DATE 10/06/09 10/14/09 10/19/09 10/16/09 10/16/09
* see pnor concurrence
OFFICIAL RECORD COPY 
Docket Nos. License Nos. Report Nos. Licensee: Facility:
Location:
Dates: . Inspectors:
Approved by: U.S. NUCLEAR REGULATORY
COMMISSION
REGION I 50-003 , 50-247 , 50-286 DPR-3, DPR-26, DPR-64 05000003/2009008, 05000247/2009008, and 05000286/2009008
Entergy Nuclear Northeast
Indian Point Nuclear Generating
Station Units 1, 2, & 3 295 Broadway Buchanan, NY 10511-0308
Augusr18 , 2009 -September
4, 2009 J. Noggle, Sr. Health Physicist, CHP, team leader T. Nicholson, Sr. Technical
Advisor for Radionuclide
Transport
J. Williams , U.S. Geological
Survey , Troy , New York John R. White, Chief Plant Support Branch 2 Division of Reactor Safety Enclosure 
SUMMARY OF FINDINGS IR 05000003/2009008, IR 05000247/2009008, IR 05000286/2009008;
08/18/2009
-9/04/2009;
Indian Point Nuclear Generating
Station Units 1, 2 & 3; Other Activities
-associated
with ROP deviation
memorandum, one PI&R sample, and radioactive
effluents
baseline inspection.
No findings of significance
were identified.
The report covers the period from August 18 through September
4, 2009, and discusses
inspection
activities
conducted
by a region-based
inspector, and an inspection
team comprised
of representatives
of Region I, NRC's Office of Research, and the U. S. Geological
Survey. The inspection
provided bases for the NRC to determine
that Entergy had completed
actions necessary
to satisfy the objectives
delineated
in our deviation
memorandum, "Request for Renewal of Deviation
to the Action Matrix
to Provide Heightened
NRC Oversight
of the Onsite Groundwater
Monitoring
at the Indian Point Energy Center," (ML083590057), dated December 16,2008. The NRC's program for overseeing
the safe operation
of commercial
nuclear power reactors is described
in NUREG-1649, "Reactor Oversight
Process," Revision 4, dated December 2006. ii Enclosure 
Report Details 2. RADIATION
SAFETY Cornerstone:
Public Radiation
Safety (PS) 2PS1 Gaseous and Liguid Effluents
(71122.01 -3 samples) a. Inspection
Scope 1) The inspector
reviewed the following
documents
to evaluate the effectiveness
of the licensee's
radioactive
gaseous and liquid effluent control programs relative to the applicable
regulatory
requirements
specified
in the Technical
Specifications
and the Offsite Dose Calculation
Manual (TS/ODCM). * The 2007 and 2008 Radiological
Annual Effluent Release Reports were reviewed including
independently
assessing
selected public dose calculations.
There were no anomalous
results reported in these two reports. The report included discussion
of current groundwater
conditions
and the result of required monitoring
activities;
and instances
involving
out-of-service
radiation
monitors or effluent release flow
rate monitors were listed in the reports and these were evaluated
during this inspection.
* The current ODCM was reviewed, including
technical
justifications
for any changes made since the previous revision.
* Applicable
sections of the Updated Final Safety Analysis Report (UFSAR) were reviewed to verify the adequacy of system descriptions
for gaseous radioactive
waste and station ventilation
systems. * The latest quality assurance
audits of radioactive
effluents
and chemistry
were reviewed, including
Entergy's
program for identifying , controlling
and assessing
potential
contam i nated spills and leakage. * There were no measurable
effluent releases to the environment
based on off-site dose calculations , and there were no reported off-site environmental
sample measurements
i dentifying
plant-related
radioactive
materials
during the 2007 and 2008 report period. 2) The inspector
observed the following plant
equipment
and work activit i es to evaluate the effectiveness
of the licensee's
radioactive
gaseous and liquid effluent control programs.
* Walkdowns
were performed
of accessible
gaseous and liquid release system components
to review any recent changes or modifications
; and to confirm the alignment, operation
and material condition
of the radioactive
liquid and gaseous effluent radiation
monitoring
systems (RMS) at Units 1, 2 and 3. * Observations
were conducted
of radioactive
effluent related sampling and associated
laboratory
measurement
techniques.
* Procedural
controls and selected radioactive
gaseous and liquid effluent release permits were reviewed to verify that radiation
monitor alarm setpoint values and releases were in agreement
with Technical
Specification
and ODCM requirements.
Enclosure 
2 * Chemistry
logs, relative to out-of-service
radiation
monitoring
conditions, were reviewed to confirm the performance
of compensatory
sampling activities.
* Surveillance
tests of gaseous filtration
discharge
systems were reviewed to confirm operability
and ventilation
flow rates with respect to the assumed flow rates used in gaseous effluent release calculations.
* Entergy's
surveillance
program of non-radioactive
system interfaces
with radioactive
process systems was reviewed to confirm effective
monitoring
and control of potential
effluent discharge
paths to the environment.
* Radiation
monitoring
system and chemistry
laboratory
counting instrument
calibration
and quality control records were reviewed with respect to ODCM surveillance
requirements
to confirm the licensee's
ability identify and report detectable
radionuclides
in radioactive
measurement
results. 3) Radioactive
effluent control related corrective
action program activities
for 2007 through August 2009 were reviewed , including
the results of audits and the resolution
of issues identified
through the condition
report system. A comprehensive
review was conducted
of conditions
and occurrences
involving
out-of-service
radiation
monitoring
system components.
Section 40A2 pertains.
b. Findings and Observations
No findings of significance
were identified.
The following
table summarizes
the dose consequence
of radiological
effluent release in the period between 2007 and 2008. Table of Effluent Release calculated
dose and public dose limits for 2007 and 2008 Dose in Air Dose %of Air Dose %of liquid '10 of Liquid %of mrem/yr Whole limit Max Organ Limit Dose limit Dose limit Body WB MaxO 2007 Units 1&2 2.43E-3 0.016 2.43E-3 0.016 5.3 5E-4 0.018 1.3E-3 0.013 2008 Units 1&2 2.07E-3 0.014 2.67E-3 0.018 6.11E-4 0.020 1.47E-3 0.Q15 2007 Unit 3 3.BBE-3 0.026 3.BBE-3 0.026 3.2E-4 0.007 2.14E-4 0.002 2008 Unit 3 1.99E-3 0.013 1.99E-3 0.013 1.56E-4 0.005 2.B3E-4 0.003 2007 Groundwater
2.66E-4 0.009 9.94E-4 0.01 2008 Groundwater
2.86E-4 0.009 9.35E-4 0.009 4. OTHER ACTIVITIES (OA) 40A2 Identification
and Resolution
of Problems Cornerstone:
Public Radiation
Safety .1 Radioactive
Gaseous and Liquid Effluent Treatment
and Monitoring
Systems a. Inspection
Scope (71122.01)
The inspector
reviewed approximately
one hundred corrective
action condition
reports, initiated
between january 2007 and August 2009, that were associated
with the gaseous, liquid, and groundwater
radioactive
effluents
program. The review was performed
to Enclosure 
3 verify that problems identified
by these condition
reports were properly characterized
in the licensee's
event reporting
system, causes were identified, and actions implemented
commensurate
the safety significance
of the matters. b. Findings and Observations
No findings of significance
were identified . . 2 Radioactive
Effluent Radiation
Monitor System (RMS) Maintenance
(71152 -1 sample) a. Inspection
Scope The inspectors
conducted
a review corrective
action program condition
reports associated
with out-of-service
radiation
monitoring
system equipment
that was identified
in the period between January 2007 and August 2009. Licensee personnel
having cognizance
of Radiation
Monitoring
System (RMS) performance
and activities
were interviewed, including
the RMS system engineer and senior chemistry
staff. "Radiation
Monitoring
System, Second Quarter 2009, Condition
Report Trend Review for Radiation. Monitoring
System Improvement
: dated September
2, 2009, was also reviewed.
b. Findings and Observations
No findings of Significance
were identified.
A large number of condition
reports associated
with the radiation
monitoring
system were initiated
during the past two years. Most of the condition
reports were associated
with interruption
of service of the RMS display consoles in both the Unit 2 and Unit 3 control rooms. While these temporary
display outages affected operators'
ability to poll individual
detector readout displays , they did not interfere
with control room annunciator
actuation
or actual detector operability. The cause of the Unit 3 display console issues was determined
to be related to excessive
temperature
in the RMS electronics cabinets
that affected certain control
room RMS display console components.
Short-term
corrective
actions included installing
permanent
air conditioning
to effect improved cooling of the RMS electronics
cabinets.
The cause of Unit 2 RMS display console service interruptions
continues
to be under review. Notwithstanding, Entergy is evaluating
replacing
the RMS display console equipment
in both control rooms to support station-wide
computer network access improvements.
Less frequently
occurring
RMS equipment
issues remain to be resolved, including
occurrences
involving
the R-56 detectors, which monitor the discharge
of waste sewage from Units 2 and 3. The location of these detectors
was determined
to be susceptible
to failure due to flooding , power spiking, and power outages. In such conditions, waste sewage is diverted to an on-site holding tank in order to conduct sampling prior to off-site release. Accordingly, there is no safety significance
to these RMS system failures.
The inspector
confirmed
that the licensee has implemented
appropriate
remedial actions for these occurrences, and has initiated
actions to improve the operating
environment
and detector function to reduce the out-of-service
time. Enclosure 
4 Entergy has identified
the Unit 2 RMS as an upgrade project in its Top Ten Action Plan for 2009. System engineering
activities
have been initiated
for this improvement
activity.
The inspector
determined
that the majority of identified
problems with the Unit 2 and Unit 3 radiation
monitoring
systems were not associated
with radiation
detector operability
or effluent release control functions.
For those instances
that resulted in out-of-service
conditions, the licensee implemented
appropriate
compensatory
measures as required by regulatory
requirements.
The inspector
confirmed
that Entergy is engaged in RMS . improvement
activities, and has initiated
appropriate
corrective
actions. 40A5 Other Activities
.1 Assessment
of Licensee Performance
Relative to Meeting the Objectives
of the December 16.2008 Memorandum
Reguesting
Deviation
from the Action Matrix Background:
On September
1, 2005, the NRC was informed by Entergy that cracks in a Unit 2 spent fuel pool wall had been discovered
during excavation
work inside the spent fuel pool building.
Low levels of radioactive
contamination
were found in the vicinity.
Entergy's
initial investigation
of the issue revealed that groundwater
in the vicinity was contaminated
with tritium. On September
20, 2005, Region I initiated
a special inspection
of this matter to examine the licensee's
performance
and determine
if the contaminated
groundwater
affected, or could affect, public health and safety. Subsequently, Entergy initiated
actions to perform a comprehensive
groundwater
site characterization, identify the sources, and effect mitigation
and remediation
of the condition.
The NRC special inspection
report, issued in March 2006, assessed Entergy's
performance, achievements, and plans for more extensive
site characterization, and reported that the groundwater
contamination
did not, nor was likely to, adversely
affect public health and safety. In the report, and subsequent
public meetings, NRC indicated
that a final conclusion
would be reached after Entergy completed
its groundwater
characterization
initiative.
The NRC Region I continued
inspection
and monitoring
of Entergy's
activities
in accordance
with successive
approved deviation
to the normal Reactor Oversight
Process for calendar years 2006 (ML053010404), 2007 (ML063480016), 2008 (ML073480290)
and 2009 (ML083590057).
During this period, the NRC staff closely monitored
Entergy's
groundwater
characterization
efforts, performed
independent
inspections
and testing, and independently
evaluated
radiological
and hydrological
conditions
affecting
groundwater
onsite. Additionally, the NRC independently
verified groundwater
releases by conducting
split monitoring
well sampling with Entergy and the State of New York. On January 11, 2008, Entergy submitted
the results of its comprehensive
hydrogeologic
site characterization
investigation (ML080320600), and included its plan for remediation
and long-term
monitoring
of the on-site groundwater
conditions.
In its report, Entergy described
the source of groundwater
contamination
to be from the Unit 1 and Unit 2 spent fuel pools. The NRC documented
its review of Entergy's
report in inspection
report 05000247 & 05000003/2007010
on May 13, 2008 (ML081340425).
In a subsequent
inspection
05000247/2008004 (ML08311 0566) dated November 6,2008, the NRC Enclosure 
5 confirmed
that Entergy's
conceptual
site model of the site, which included both the vadose zone and saturated
zone processes
and conditions, effectively
characterized
the onsite groundwater
plume behavior and radionuclide
transport. Evaluation
of radionuclide
concentrations
and pathway analyses indicated
that the groundwater
contamination
did not adversely
affect public health and safety. Detailed discussions
and analyses indicated
that the licensee's
plans for long-term
monitoring
of the site, relative to monitoring
natural attenuation
of residual groundwater
contamination, were reasonable.
On November 3, 2008, Entergy completed
Unit 1 spent fuel pool system drainage and sludge removal activities, essentially
terminating
the source from that facility. Given the change in conditions, Entergy initiated
actions to establish
a new groundwater
contaminant
baseline in support of its long-term
monitoring
program. a. Inspection
Scope The most recently approved Memorandum
of Deviation, i.e., " Request for Renewal of Deviation
to the Action Matrix to Provide Heightened
NRC Oversight
of the Onsite Groundwater
Monitoring
at the Indian Point Energy Center," dated December 16, 2008 (ML083590057), identified
the following
objectives
to be addressed
in order to support resumption
of normal inspection
activities
in accordance
with the Reactor Oversight
Process: * Entergy has completed
sufficient
data collection
and assessment
to establish
a new groundwater
contaminant
baseline, now that the Unit 1 source term has been terminated.
* Entergy has determined
whether active leakage has been terminated
or continues
to persist in regard to the Unit 2 spent fuel pool; and has implemented
appropriate
monitoring
and control measures, as necessary.
* Entergy has established
and implemented
effluent control and environmental
monitoring
procedures
that provide reasonable
assurance
that the existing groundwater
conditions
will continue to be effectively
monitored
and assessed, that the procedures
will detect new or changed conditions
in a timely manner, and that the procedures
are sufficient
to monitor natural attenuation
of the Unit 1 and Unit 2 groundwater
contamination
plumes. The NRC team reviewed the licensee's
performance
and achievements
relative to the completion
of these objectives.
b. Findings and Observations
No findings of significance
were identified.
The inspectors
determined
that Entergy completed
the actions necessary
to satisfy the objectives
delineated
in the approved Memorandum
of Deviation, dated December 16, 2008, (ML083590057).
Notwithstanding, NRC will continue to monitor performance
in this area, and re-assess
the need for continued
heightened
inspection
oversight
as part of the CY 2009 end-of-cycle
performance
review of IPEC. Enclosure 
6 The following
pertains:
* Objective
1: Completion
of sufficient
data collection
and assessment
to establish
a new groundwater
contaminant
baseline, now that the Unit 1 source term has been terminated.
As a result of the defueling, drainage, and de-sludging
of the Unit 1 spent fuel pool system in the Fall of 2008, the groundwater
contamination
source term from the Unit 1 facility was terminated.
The inspectors
confirmed
that Entergy's subsequent
data collection
and assessment
activities , associated
with the continual
monitoring
of the residual groundwater
contamination, would be sufficient
and effective
to establish
a new baseline relative to monitoring
the residual groundwater
condition
and subsequent
assessment
of dose consequence. As expected, the first and second-quarter
ground-water
sample results in 2009, collected
from Monitoring
Wells in the immediate
vicinity o f the Unit 1 spent fuel pool, indicated
an increase in Sr-90 groundwater
concentrations. As determined
from review of the licensee's
data and analysis, this increased
concentration
was the expected result of the volume of water that was necessary
to fill the spent fuel pool system to effect defueling.
Accordingly, Entergy's baseline data was predicated
on the existing groundwater
conditions
determined
from its continuing
analysis of collected
monitoring
data. Given that the original source of the contamination
associated
with leakage from the Unit 1. spent fuel pool system has been terminated , the residual groundwater
contamination
involving
Sr-90 is expected to naturally
attenuate
over time. The inspectors
confirmed
that the current groundwater
contaminant
concentrations
have not, nor are expected to, affect public health and safety; and the public radiological
dose consequence
is expected to continue to be a fraction of the NRC annual regulatory
limit affecting
liquid effluents.
The inspectors
confirmed
that cont i nual monitoring
of the migration
and attenuation
of the Unit 1 associated
groundwater
contamination
condition
is being performed
in accordance
with Entergy's
Long-Term Ground-Water
Monitoring
Program (LTGWMP).
The inspectors
confirmed
that Entergy has established , implemented
and maintains
a long-term
ground-water
monitoring
program that has sufficient
in scope and implementation
requirements
to effectively
monitor and assess this condition. Accordingly, the intent of this objective
was considered
satisfied. * Objective
2: Determination
whether active leakage has been terminated
or continues
to persist in regard to the Unit 2 spent fuel pool , and that appropriate
monitoring
and control measures have been implemented , as necessary.
Entergy has been actively engaged in analyzing
Monitoring
Well data associated
with the H-3 (tritium)
groundwater
contamination
condition
that resulted from previously
identified
leakage from the Unit 2 spent fuel pool: Entergy's analysis indicated
an overall . decreaSing
trend in tritium concentration
in the groundwater
as a result of previous efforts to e x amine the condition
of the spent fuel pool and transfer canal liner , and effect repair , as necessary.
Notwithstanding , as previously
reported , Entergy's
e x amination
of the spent fuel pool liner was necessarily
limited to only the accessible
surfaces.
That is, only about 40 % of the total liner surfaces were accessible
for examination;
the remaining
surfaces were necessarily
inaccessible
due to the pro x imity of stored spent fuel that prevented
examination.
Enclosure 
7 The inspectors
reviewed the licensee's
analysis derived from groundwater
monitoring
data, and confirmed
that there was no apparent indication
of any significant
large flux going active leakage. The inspectors
also reviewed the licensee's monitoring
well detect i on sensitivity
data , which supports that active leakage , if occurring , would likely not exceed 30 gallons per day (0.02 gpm). This sensitivity
analysis was based on comparison
of the tritium concentration
that is available
in the spent fuel pool and the actual tritium concentration
derived from samples collected
from relevant monitoring
wells in the near vicinity of the spent fuel pool. Additionally, the inspectors
reviewed licensee analysis and data from a long-term
tracer test that indicated
the potential
for slow, episodic trit i um migration
in the fractures
of the vadose zone that affect the mobility of contamina t ed groundwater
from the immediate
vicinity of the Unit 2 spent fuel pool to the water table. The licensee's analysis is supported
by the fact that fluorescine
dye, which was injected as part of the groundwater
characterization
study over two years ago, is still detectable
in certain nearby monitor i ng wells. The inspectors noted that
there were occasional
spikes and general variability
in some monitor i ng well tritium concentration
values that were not characteristic
of the e x pected attenuation
that would normally be expected at this time. Additionally , the licensee continued
to occasionally
collect a small quantity of water from the leak collection
box that was installed
on the Unit 2 spent fuel pool wall crack that was identified
in 2005. Accordingly, while there was no indication
of any significant
large flux active leakage, there was insufficient
basis to conclude that there is absolutely
no persistent
low flux leakage from the Unit 2 spent fuel pool, at this time. Notwithstanding , the inspectors
determined
that the licensee's sensitivity
analysis of groundwater
monitoring
data, relative to its ability to detect active leakage in e x cess of about 30 gallons per day , was reasonably
derived. Additionally , the inspectors
confirmed
that the current groundwater
conditions, even if there was persistent
low flux leakage from the Unit 2 spent fuel pool, has not, nor would be e x pected to, affect public health and safety; and the public radiological
dose consequence
would be expected to continue to be a fraction of the NRC annual regulatory
limit affecting
liquid effluents.
The inspectors
confirmed
that continual
monitoring
of the mig r ation and attenuation
of the Un it 2 associated
groundwater
contamination
condition
was being performed
in accordance
with Entergy's Long-Term
Ground-Water Monitoring
Program; and that the program implemented
appropriate
monitoring
and control measures for this condition.
The inspectors
confirmed
that Entergy has established, implemented
and maintained
a long-term
ground-water
monitoring
program that has sufficient
scope and implementation
requirements
to effectively
monitor and assess the present condition. Further, the licensee is considering
monitOring
in the vadose zone , in the vicinity of the Unit 2 facility , to assist in the detection
of large flu x releases. Accord i ngly , the intent of this objective
was considered
satisfied.
* Objective
3: Establishment
and implementation
of effluent control and environmental
monitoring
procedures
that provide reasonable
assurance
that the e x isting groundwater
conditions
will continue to be effectively
monitored
and assessed, that t he procedures
will detect new or changed conditions
in a timely manner, and that the procedures
are sufficient
to monitor natural attenuation
of the Unit 1 and Unit2 groundwater
contamination
plumes. Enclosure 
8 The NRC has conducted several
inspections (August 2007, October 2008, and August 2009) of the licensee's
Long-Term
Ground-Water
Monitoring
Program. The inspectors
confirmed
that Entergy has established, implemented
and maintained
a Long-Term
Ground-Water
Monitoring
Program that was sufficient
in scope and implementation
requirements
to effectively
monitor and assess the existing contaminated
groundwater
conditions
affecting
the Indian Point Energy Center. During this inspection, the inspectors
examined the refurbishment
of the LaFarge No.2 Monitoring
Well (one of the principal off-site monitoring
wells) and confirmed
its acceptability
as a valid off-site monitoring
location.
Additionally , the inspectors
verified that the administrative
controls, established
in the Long-Term
Groundwater
Monitoring
Program, were sufficient
t9 provide assurance
of review and appropriate
communication
of activities
and changes that affect ground-water
monitoring
conditions;
and that the program included sufficient
sampling requirements
for storm drains and the Unit 1 foundation
drain systems. During this inspection, the inspectors
reviewed a March 25, 2009 instance involving
the licensee's
detection
of tritiated
water in the catch basin of a storm drain in the vicinity of Unit 3 , and in an adjacent shallow monitoring
well. The licensee conducted
an extensive
investigation
but was unable to find an explanation
for this one-time occurrence.
The inspectors
confirmed
that the occurrence
had no radiological
consequence
onsite or offsite; and no leakage was identified
from any Unit 3 component
containing
tritiated
water. However, the nature of the occurrence
indicated
uncertainty
in the ability of the existing Unit 3 monitoring
wells to detect potential
leakage from that facility.
While there was no current on-going leakage affecting
the groundwater
at Unit 3 , Entergy initiated
action to re-evaluate
the Unit 3 groundwater
monitoring
configuration (both vertically
and horizontally)
to determine
its effectiveness
in meeting the objectives
and recommendations
of the NEI "Industry
Groundwater
Protection
Initiative-
Final Guidance Document, August 2007" (ML072600292
and ML07261 0036); and amend the Term Groundwater
Monitoring
Program , as necessary.
Notwithstanding, the inspectors
confirmed
that Entergy has established, implemented
and maintained
a Long-Term
Ground-Water
Monitoring
Program that has sufficient
scope and implementation
requirements
to effectively
monitor and assess the existing* groundwater
conditions
affecting
Indian Point Energy Center. Accordingly, the intent of this objective
was considered
satisfied . . 2 Groundwater
Sampling a. Inspection
Scope During the licensee's
groundwater
investigation, over 1200 groundwater
samples were collected
and analyzed from the established
on-site monitoring
well network by the second quarter of 2009. The analytical
results provide the basis for assessing
the extent of the groundwater
plume and for performing
calculations
of offsite doses to members of the public. In order to assess Entergy's
performance
in this area, the NRC implemented
an independent
split sample collection
program with the licensee beginning
in September
2005. The monitoring
wells selected for independent
verification
included the southem boundary wells and those wells bordering
the Hudson River that were used Enclosure 
9 in support of effluent release and dose assessment
calculations.
Sample identity was assured by chain-of-custody
procedures
that included sample collection
observation
by the NRC or a representative
of the NYS DEC. The NRC samples were analyzed by an independent
govemment
laboratory
to ensure validation
of the licensee's
groundwater
contamination
results and off-site environmental
sample radioactive
measurements.
By the second quarter of 2009, over 300 split groundwater
samples were obtained to provide an independent
check of Entergy's
analytical
results and to independently
verify if there was any detectable
migration
of groundwater
contaminants
offsite. These split samples represent
over 1,200 analyses, primarily
for hydrogen-3 (tritium), strontium-90, nickel-63, and gamma-emitting
radionuclides
that characterized
the effluent releases. Analyses for other radionuclides
were performed, but none were detected.
b. Findings and Assessment
No findings of significance
were identified. In general, Entergy's
groundwater
measurements
of radioactivity
were of good quality and of sufficient
sensitivity
to assess radiological
impact. The quality of Entergy's
measurements
were confirmed
by various split samples analyzed by the NRC. Of the over 1200 results that were reviewed, there were only a few sample disagreements
based on the statistical
comparison
criteria specified
in NRC Inspection
Procedure
84750, "Radioactive
Waste Treatment, and Effluent and Environmental
Monitoring." As a result of these few discrepancies, Entergy took corrective
action to establish, implement, and maintain procedures
to effect improved quality control and assurance
of sample analysis performed
by its own laboratory
and contract analytical
laboratories.
During the past 3)1" years, the on-site groundwater
transport
pathway has been effectively
characterized
by the licensee, and a significant
quantity of on-site groundwater
monitoring
data has been collected
and analyzed by Entergy. A representative
numbers of split samples have confirmed
the overall efficacy of the licensee's
analytical
capability.
As the site characterization
was tested through pumping and tracer testing, the contaminant
plume uncertainty
has been significantly
reduced. Given this accomplishment, and the NRC determination
that Entergy has demonstrated
an effective
groundwater
sample quality control program, the NRC will discontinue
any further split sampling activities.
40A6 Meetings, including
Exit .1 Exit Meeting Summary The inspectors
presented
the inspection
results to Mr. D. Mayer and other licensee and New York State representatives
on August 19, 2009 and September
4, 2009. The licensee acknowledged
the findings presented.
Based upon discussions
with the licensee, none of the information
presented
at the exit meeting and included in this report was considered
proprietary.
Enclosure 
Licensee Personnel
J. Pollock M. BaNenik P. Conroy D. Croulet P. Donahue C. English G. Hinrichs D. Loope T. Jones R. LaVera D. Mayer J. Michetti J. Peters D. Rusczyk S. Sandike J. Simpson R. Walpole A-1 ATTACHMENT
SUPPLEMENTAL
INFORMATION
KEY POINTS OF CONTACT Site Vice President
Principal
Engineer, GZA Geo EnVironmental, Inc. Director, Nuclear Safety Assurance
Licensing
Engineer Chemistry
Specialist
Unit 1 Project Engineer Project Engineer Radiation
Protection
Superintendent
Licensing
Engineer Radiological
Engineer Director, Special Projects RMS System Engineer Plant Chemist Environmental
Assessment, GZA Chemistry
ODCM Specialist
Environmental
Assessment, GZA Manager, Licensing
New York State Inspection
ObseNers L. Rosenmann
Engineering
Geologist, New York State, Department
of Environmental
ConseNations
INSPECTION
PROCEDURES
USED 71122.01 Radioactive
Gaseous and Liquid Effluent Treatment
and Monitoring
Systems LIST OF DOCUMENTS
REVIEWED Annual Radiological
Effluent Release Reports -2007 and 2008 Off-Site Dose Calculation
Manual, Revision 2 O-CY-2730, Rev. 1, Airbome Radioactive
Effluents
O-CY-2740, Rev. 1, Liquid Radioactive
Effluents
IP-SMM-CY-001, Rev. 7, Radioactive
Effluents
Control Program IP-SMM-CY-110, Rev. 3, Radiological
Groundwater
Monitoring
Program 2-CY-2625, Rev. 14, General Plant Systems Specifications
and Frequencies
3-CY-2325, Rev. 8, Radioactive
Sampling Schedule 2-S0P-5.2.4, Rev. 33, Calculation
and Recording
of Radioactive
Gaseous Releases 2-S0P-5.1.5, Rev. 34, Calculation
and Recording
of Radioactive
Liquid Releases 3-S0P-WDS-014, Rev. 25, Liquid Waste Releases Attachment 
A-2 3-S0P-WDS-013 , Rev. 25 , Gaseous Waste Releases EN-RP-113 , Response to Contaminated
Spills/Leaks
EN-CY-109, Sampling and Analysis of Groundwater
Monitoring
Wells EN-CY-108, Monitoring
of Non-Radioactive
Systems " Industry Groundwater
Protection
Initiative
-Final Guidance Document , August 2007" (ML072600292
and ML072610036)
Unit 2 Liquid Release Permit No. 090016 Unit 2 Gaseous Release Permit No. 090126 Unit 3 Liquid Release Permit No. 090081 Unit 3 Gaseous Release Permit No. 090067 Condition
Reports: CR-IP3-2007 -0803 CR-IP2-2009
-2089 CR-IP3-2009-3356
CR-IP2-2009-2528
CR-IP2-2009-3307
CR-IP3-2007-3954
CR-IP2-200S-0270
CR-IP2-200S-0375
CR-IP3-200S-071S
CR-IP2-200S-0377
CR-IP2-2009-2266
CR-IP2-200S-1236
CR-IP3-2007 -3860 CR-IP3-200S-1112
CR*IP3*200S*2915
CR*IP3*200S*1042
CR*IP2*200S*2767
CR*IP2*200S*4136 CR*IP3*200S*2184
CR*IP2*200S*3662
CR*IP3*200S*2125
CR*IP2 c 200S*4130
CR*IP2*200S*4529


CR*IP2-200S-4191
J. Pollock                                    2
CR-IP2-200S-456S
public health and safety, protection of the environment, and conformance with NRC regulatory
CR-IP3-2007-0151
requirements. Our inspectors confirmed that the objectives specified in our deviation
CR-IP3-2007
memorandum dated December 16,2008 (ML083590057) have been satisfied. However, we will
-2S99 CR-IP3-2007
continue to monitor your performance in this area, and will re-assess the need for continued
-2134 CR-IP3-2007
heightened inspection oversight during our end-of-cycle review of your CY 2009 perfonmance.
-3129 CR-IP2-2008-4981
In accordance with 10 CFR2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document Room
or from the Publicly Available Records (PARS) component of the NRC's document system
(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-
rm/adams.html (the Public Electronic Reading Room).
                                  J);W~
                                      Darrell J. Roberts, Director
                                      Division of Reactor Safety
Docket Nos: 50-003, 50-247, 50-286
License Nos: DPR-5, DPR-26, DPR-64
Enclosure:      Inspection Report Nos. 05000003/2009008, 05000247/2009008,
              05000286/2009008
                  w/Attachment: Supplemental Information
cc w/encj: Distribution via ListServ


CR-IP2-2008-5552
              J. Pollock                                                      2
CR-IP2-2009-0609
              public health and safety, protection of the environment, and conformance with NRC regulatory
CR-IP2-2009-0565
              requirements . Our inspectors confirmed that the objectives specified in our deviation
CR-IP2-2009-223S
              memorandum dated December 16, 2008 (ML083590057) have been satisfied. However, we will
CR-IP2-2009-1334
              continue to monitor your performance in this area, and will re-assess the need for continued
CR-IP2-2009-2352
              heightened inspection oversight during our end-of-cycle review of your CY 2009 performance.
CR-IP3-2009-3201
              In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
CR-IP3-2009-3254
              enclosure will be available electronically for public inspection in.the NRC Public Document Room
CR-IP2-2009-3306
              or from the Publicly Available Records (PARS) component of the NRC's document system
CR-IP3-2007-3925
              (ADAMS). ADAMS is accessible from the NRC Web site at hllp:llwww.nrc.gov/reading-
CR-IP2-2007-5226
              rm/adams.html (the Public Electronic Reading Room).
CR-IP2-200S-0549
                                                                    Sincerely,
CR-IP2-200S-0960
                                                                    IRA by Peter R. Wilson forI
CR-IP2-200S-0144
                                                                    Darrell J. Roberts, Director
CR-IP3-200S-0569
                                                                    Division of Reactor Safety
CR-IP3-200S-0852
              Docket Nos: 50-003, 50-247, 50-286
CR-IP3-2008-0942
              License Nos: DPR-5, DPR-26, DPR-64
CR-IP2-2008-2468
              Enclosure:          Inspection Report Nos. 05000003/2009008, 05000247/2009008,
CR-IP3-2008-1215
                                  05000286/2009008
CR-IP2-2008-2581
                                      w/Allachment: Supplemental Information
CR-IP3-2008-1218
              cc w/encl: Distribution via ListServ
CR-IP3-2008-200
              Distribution w/encl: (via E-mail)                                          S. McCarver, DRP
1 CR-IP2-2008-3342
              S. Collins, RA (R10RAMAIL RESOURCE)                                        G. Malone, DRP, Senior Resident Inspector
CR-IP3-200S-1S99
              M. Dapas, DRA (R10RAMAIL                                                        - Indian Point 2
CR-IP2-200S-4193
                      RESOURCE)                                                          D. Hochmuth , DRP
CR-IP2-200S-4254
              D. Lew, DRP (R1 DRPMAIL RESOURCE)                                          D. Bearde, DRP
CR-IP2-200S-4337
              J. Clifford, DRP (R1DRPMAIL                                                Region I Docket Room (w/concurrences)
CR-IP3-200S-2279
                      RESOURCE)                                                          ROPreport Resource
CR-IP3-2008-0624
              L. Trocine, Ri OEDO                                                        D. Roberts , DRS
CR-IP3-2007-3367
              RIDSNRRPMINDIANPOINTRESOURCE                                              P. Wilson, DRS
CR-IP3-2007-3061
              B. Welling, DRP                                                            J. White, DRS
CR-IP3-2007
              B. Bickell, DRP
-3075 CR-IP2-2008-4S48
SUNSI Review Complete:          JRW              (Reviewer's Inrtials)
CR-IP2-200S-5055
OOCUMENT NAME: G:IORSIPlant Support Branch 2INoggleIIP2009008Rev1 .doc
CR-IP3-2009-003S
After declaring this document ~An Official Agency Record w it will be rel eased to the Public.
CR-IP2-2009-1125
To receive a copy of this document, Indicate in the box: "e" = COpy without attachment/enclosure "E" = COpy with attachment/enclosure "N" = No CQP"y
CR-IP2-2009-079S
OFFICE                RIIDRS              I    RES                      I      RIIDRS            I    RIIDRP        I      RIIDRS              I
CR-IP2-2009-1295
NAME                  JNoggle/JDN                TNicholsonltjn                  JWhite/jrw' ehg        BWeliinglBW          DRoberts/prw for
CR-IP2-2009-2090
                                                  (telecon)                      for'
DATE                  10/06/09                  10/14/09                        10/19/09              10/16/09              10/16/09
                *see pnor concurrence                            OFFICIAL RECORD COPY


CR-IP2-2009-2603
                U.S. NUCLEAR REGULATORY COMMISSION
CR-IP3-2009-320S
                                  REGION I
CR-IP3-2007
Docket Nos.  50-003 , 50-247, 50-286
-3953 CR-IP3-2007
License Nos. DPR-3, DPR-26, DPR-64
-41S3 CR-IP2-2007-5217
Report Nos.  05000003/2009008, 05000247/2009008, and 05000286/2009008
CR-IP2-2008-1149
Licensee:    Entergy Nuclear Northeast
CR-IP2-2008-0404
Facility:    Indian Point Nuclear Generating Station Units 1, 2, & 3
CR-IP2-2008-0492
Location:    295 Broadway
CR-IP3-2008-0S46
            Buchanan, NY 10511-0308
CR-IP2-2008-0179
Dates: .    Augusr18, 2009 - September 4, 2009
CR-IP2-2008-3154
Inspectors:  J. Noggle, Sr. Health Physicist, CHP, team leader
CR-IP3-2008-0194
            T. Nicholson, Sr. Technical Advisor for Radionuclide Transport
CR-IP2-2008-3526 CR-IP2-2008-2691
            J. Williams, U.S. Geological Survey, Troy, New York
CR-IP3-2009-00S0
Approved by: John R. White, Chief
CR-IP2-2008-2955
            Plant Support Branch 2
CR-IP2-2008-3492
            Division of Reactor Safety
CR-IP3-2008-1979
                                                                            Enclosure
CR-IP2-2008-4108
CR-IP2-2008-4202
CR-IP3-2008-2296
CR-IP3-2008-2294


CR-IP3-2007
                                    SUMMARY OF FINDINGS
-0005 CR-I P3-2007 -27 48 CR-IP3-2007-2S70
IR 05000003/2009008, IR 05000247/2009008, IR 05000286/2009008; 08/18/2009 - 9/04/2009;
CR-IP2-2008-1132
Indian Point Nuclear Generating Station Units 1, 2 & 3; Other Activities - associated with ROP
CR-IP3-200S-2S62
deviation memorandum, one PI&R sample, and radioactive effluents baseline inspection.
CR-IP2-2009-0477
No findings of significance were identified. The report covers the period from August 18 through
September 4, 2009, and discusses inspection activities conducted by a region-based inspector,
and an inspection team comprised of representatives of Region I, NRC's Office of Research,
and the U. S. Geological Survey. The inspection provided bases for the NRC to determine that
Entergy had completed actions necessary to satisfy the objectives delineated in our deviation
memorandum, "Request for Renewal of Deviation to the Action Matrix to Provide Heightened
NRC Oversight of the Onsite Groundwater Monitoring at the Indian Point Energy Center,"
(ML083590057), dated December 16,2008. The NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
Oversight Process," Revision 4, dated December 2006.
                                                ii
                                                                                        Enclosure


CR-IP2-2009
                                          Report Details
-01S4 CR-IP3-2009-0494
2.    RADIATION SAFETY
      Cornerstone: Public Radiation Safety (PS)
2PS1  Gaseous and Liguid Effluents (71122.01 - 3 samples)
a.    Inspection Scope
    1) The inspector reviewed the following documents to evaluate the effectiveness of the
      licensee's radioactive gaseous and liquid effluent control programs relative to the
      applicable regulatory requirements specified in the Technical Specifications and the
      Offsite Dose Calculation Manual (TS/ODCM).
          *    The 2007 and 2008 Radiological Annual Effluent Release Reports were
                reviewed including independently assessing selected public dose calculations.
                There were no anomalous results reported in these two reports . The report
                included discussion of current groundwater conditions and the result of required
                monitoring activities; and instances involving out-of-service radiation monitors or
                effluent release flow rate monitors were listed in the reports and these were
                evaluated during this inspection.
          *    The current ODCM was reviewed, including technical justifications for any
                changes made since the previous revision.
          *    Applicable sections of the Updated Final Safety Analysis Report (UFSAR) were
                reviewed to verify the adequacy of system descriptions for gaseous radioactive
                waste and station ventilation systems.
          *    The latest quality assurance audits of radioactive effluents and chemistry were
                reviewed, including Entergy's program for identifying, controlling and assessing
                potential contaminated spills and leakage.
          *    There were no measurable effluent releases to the environment based on off-site
                dose calculations, and there were no reported off-site environmental sample
                measurements identifying plant-related radioactive materials during the 2007 and
                2008 report period.
    2) The inspector observed the following plant equipment and work activities to evaluate the
      effectiveness of the licensee's radioactive gaseous and liquid effluent control programs.
          *      Walkdowns were performed of accessible gaseous and liquid release system
                components to review any recent changes or modifications; and to confirm the
                alignment, operation and material condition of the radioactive liquid and
                gaseous effluent radiation monitoring systems (RMS) at Units 1, 2 and 3.
          *      Observations were conducted of radioactive effluent related sampling and
                associated laboratory measurement techniques.
          *      Procedural controls and selected radioactive gaseous and liquid effluent release
                permits were reviewed to verify that radiation monitor alarm setpoint values and
                releases were in agreement with Technical Specification and ODCM
                requirements.
                                                                                        Enclosure


CR-IP3-2009-0591  
                                                      2
Attachment
            *    Chemistry logs, relative to out-of-service radiation monitoring conditions, were
A-3 NRC Groundwater  
                  reviewed to confirm the performance of compensatory sampling activities.
Sample Result Documentation  
            *    Surveillance tests of gaseous filtration discharge systems were reviewed to
ICY 2009. 1 s t Quarter) ML090400502.  
                  confirm operability and ventilation flow rates with respect to the assumed flow
ML090920949.  
                  rates used in gaseous effluent release calculations.
ML090920932  
            *    Entergy's surveillance program of non-radioactive system interfaces with
FSAR GPM LTGWMP NYS DEC ODCM pCi/L PI&R Rap LIST OF ACRONYMS USED Final Safety Analysis Report gallons per minute Long Term Ground-Water  
                  radioactive process systems was reviewed to confirm effective monitoring and
Monitoring  
                control of potential effluent discharge paths to the environment.
Program State of New York Department  
            *    Radiation monitoring system and chemistry laboratory counting instrument
of Environmental  
                calibration and quality control records were reviewed with respect to ODCM
Conservation Offsite Dose  
                surveillance requirements to confirm the licensee's ability identify and report
Calculation  
                detectable radionuclides in radioactive measurement results.
Manual pico-Curies  
    3) Radioactive effluent control related corrective action program activities for 2007 through
per Liter Problem Identification  
        August 2009 were reviewed, including the results of audits and the resolution of issues
and Resolution  
        identified through the condition report system. A comprehensive review was conducted
Reactor Oversight  
        of conditions and occurrences involving out-of-service radiation monitoring system
Process Attachment
        components. Section 40A2 pertains.
  b.    Findings and Observations
        No findings of significance were identified. The following table summarizes the dose
        consequence of radiological effluent release in the period between 2007 and 2008.
        Table of Effluent Release calculated dose and public dose limits for 2007 and 2008
          Dose in          Air Dose    %of    Air Dose    %of      liquid    '10 of Liquid    %of
          mrem/yr          Whole        limit  Max Organ    Limit    Dose      limit  Dose      limit
                            Body                                      WB                MaxO
2007      Units 1&2        2.43E-3      0.016  2.43E-3      0.016    5.35E-4  0.018  1.3E-3    0.013
2008      Units 1&2        2.07E-3      0.014  2.67E-3      0.018    6.11E-4  0.020  1.47E-3  0.Q15
2007      Unit 3          3.BBE-3      0.026  3.BBE-3      0.026    3.2E-4    0.007  2.14E-4  0.002
2008      Unit 3          1.99E-3      0.013  1.99E-3      0.013    1.56E-4  0.005  2.B3E-4  0.003
2007      Groundwater                                                2.66E-4  0.009  9.94E-4    0.01
2008      Groundwater                                                2.86E-4  0.009  9.35E-4  0.009
4.      OTHER ACTIVITIES (OA)
40A2 Identification and Resolution of Problems
        Cornerstone: Public Radiation Safety
.1      Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems
  a.    Inspection Scope (71122.01)
        The inspector reviewed approximately one hundred corrective action condition reports,
        initiated between january 2007 and August 2009, that were associated with the gaseous,
        liquid, and groundwater radioactive effluents program. The review was performed to
                                                                                            Enclosure
 
                                                3
      verify that problems identified by these condition reports were properly characterized in
      the licensee's event reporting system, causes were identified, and actions implemented
      commensurate the safety significance of the matters.
  b.  Findings and Observations
      No findings of significance were identified .
.2    Radioactive Effluent Radiation Monitor System (RMS) Maintenance (71152 - 1 sample)
  a. Inspection Scope
      The inspectors conducted a review corrective action program condition reports
      associated with out-of-service radiation monitoring system equipment that was identified
      in the period between January 2007 and August 2009. Licensee personnel having
      cognizance of Radiation Monitoring System (RMS) performance and activities were
      interviewed, including the RMS system engineer and senior chemistry staff. "Radiation
      Monitoring System, Second Quarter 2009, Condition Report Trend Review for Radiation .
      Monitoring System Improvement: dated September 2, 2009, was also reviewed.
  b.  Findings and Observations
      No findings of Significance were identified.
      A large number of condition reports associated with the radiation monitoring system were
      initiated during the past two years . Most of the condition reports were associated with
      interruption of service of the RMS display consoles in both the Unit 2 and Unit 3 control
      rooms. While these temporary display outages affected operators' ability to poll
      individual detector readout displays, they did not interfere with control room annunciator
      actuation or actual detector operability.
      The cause of the Unit 3 display console issues was determined to be related to
      excessive temperature in the RMS electronics cabinets that affected certain control room
      RMS display console components. Short-term corrective actions included installing
      permanent air conditioning to effect improved cooling of the RMS electronics cabinets.
      The cause of Unit 2 RMS display console service interruptions continues to be under
      review. Notwithstanding, Entergy is evaluating replacing the RMS display console
      equipment in both control rooms to support station-wide computer network access
      improvements.
      Less frequently occurring RMS equipment issues remain to be resolved, including
      occurrences involving the R-56 detectors, which monitor the discharge of waste sewage
      from Units 2 and 3. The location of these detectors was determined to be susceptible to
      failure due to flooding , power spiking, and power outages. In such conditions, waste
      sewage is diverted to an on-site holding tank in order to conduct sampling prior to off-site
      release . Accordingly, there is no safety significance to these RMS system failures. The
      inspector confirmed that the licensee has implemented appropriate remedial actions for
      these occurrences, and has initiated actions to improve the operating environment and
      detector function to reduce the out-of-service time.
                                                                                        Enclosure
 
                                                  4
      Entergy has identified the Unit 2 RMS as an upgrade project in its Top Ten Action Plan
      for 2009. System engineering activities have been initiated for this improvement activity.
      The inspector determined that the majority of identified problems with the Unit 2 and Unit
      3 radiation monitoring systems were not associated with radiation detector operability or
      effluent release control functions. For those instances that resulted in out-of-service
      conditions, the licensee implemented appropriate compensatory measures as required
      by regulatory requirements. The inspector confirmed that Entergy is engaged in RMS
    . improvement activities, and has initiated appropriate corrective actions.
40A5 Other Activities
.1    Assessment of Licensee Performance Relative to Meeting the Objectives of the
      December 16.2008 Memorandum Reguesting Deviation from the Action Matrix
      Background:
      On September 1, 2005, the NRC was informed by Entergy that cracks in a Unit 2 spent
      fuel pool wall had been discovered during excavation work inside the spent fuel pool
      building. Low levels of radioactive contamination were found in the vicinity. Entergy's
      initial investigation of the issue revealed that groundwater in the vicinity was
      contaminated with tritium. On September 20, 2005, Region I initiated a special inspection
      of this matter to examine the licensee's performance and determine if the contaminated
      groundwater affected, or could affect, public health and safety. Subsequently, Entergy
      initiated actions to perform a comprehensive groundwater site characterization, identify
      the sources, and effect mitigation and remediation of the condition.
      The NRC special inspection report, issued in March 2006, assessed Entergy's
      performance, achievements, and plans for more extensive site characterization, and
      reported that the groundwater contamination did not, nor was likely to, adversely affect
      public health and safety. In the report, and subsequent public meetings, NRC indicated
      that a final conclusion would be reached after Entergy completed its groundwater
      characterization initiative.
      The NRC Region I continued inspection and monitoring of Entergy's activities in
      accordance with successive approved deviation to the normal Reactor Oversight
      Process for calendar years 2006 (ML053010404), 2007 (ML063480016), 2008
      (ML073480290) and 2009 (ML083590057). During this period, the NRC staff closely
      monitored Entergy's groundwater characterization efforts, performed independent
      inspections and testing, and independently evaluated radiological and hydrological
      conditions affecting groundwater onsite. Additionally, the NRC independently verified
      groundwater releases by conducting split monitoring well sampling with Entergy and the
      State of New York.
      On January 11, 2008, Entergy submitted the results of its comprehensive hydrogeologic
      site characterization investigation (ML080320600), and included its plan for remediation
      and long-term monitoring of the on-site groundwater conditions. In its report, Entergy
      described the source of groundwater contamination to be from the Unit 1 and Unit 2
      spent fuel pools. The NRC documented its review of Entergy's report in inspection report
      05000247 & 05000003/2007010 on May 13, 2008 (ML081340425). In a subsequent
      inspection 05000247/2008004 (ML08311 0566) dated November 6,2008, the NRC
                                                                                        Enclosure
 
                                              5
  confirmed that Entergy's conceptual site model of the site, which included both the
  vadose zone and saturated zone processes and conditions, effectively characterized the
  onsite groundwater plume behavior and radionuclide transport. Evaluation of
  radionuclide concentrations and pathway analyses indicated that the groundwater
  contamination did not adversely affect public health and safety. Detailed discussions
  and analyses indicated that the licensee's plans for long-term monitoring of the site,
  relative to monitoring natural attenuation of residual groundwater contamination, were
  reasonable.
  On November 3, 2008, Entergy completed Unit 1 spent fuel pool system drainage and
  sludge removal activities, essentially terminating the source from that facility. Given the
  change in conditions, Entergy initiated actions to establish a new groundwater
  contaminant baseline in support of its long-term monitoring program.
a. Inspection Scope
  The most recently approved Memorandum of Deviation, i.e., "Request for Renewal of
  Deviation to the Action Matrix to Provide Heightened NRC Oversight of the Onsite
  Groundwater Monitoring at the Indian Point Energy Center," dated December 16, 2008
  (ML083590057), identified the following objectives to be addressed in order to support
  resumption of normal inspection activities in accordance with the Reactor Oversight
  Process:
  *      Entergy has completed sufficient data collection and assessment to establish a
          new groundwater contaminant baseline, now that the Unit 1 source term has
          been terminated.
  *      Entergy has determined whether active leakage has been terminated or
          continues to persist in regard to the Unit 2 spent fuel pool; and has implemented
          appropriate monitoring and control measures, as necessary.
  *      Entergy has established and implemented effluent control and environmental
          monitoring procedures that provide reasonable assurance that the existing
          groundwater conditions will continue to be effectively monitored and assessed,
          that the procedures will detect new or changed conditions in a timely manner, and
          that the procedures are sufficient to monitor natural attenuation of the Unit 1 and
          Unit 2 groundwater contamination plumes.
  The NRC team reviewed the licensee's performance and achievements relative to the
  completion of these objectives.
b. Findings and Observations
  No findings of significance were identified.
  The inspectors determined that Entergy completed the actions necessary to satisfy the
  objectives delineated in the approved Memorandum of Deviation, dated December 16,
  2008, (ML083590057). Notwithstanding, NRC will continue to monitor performance in
  this area, and re-assess the need for continued heightened inspection oversight as part
  of the CY 2009 end-of-cycle performance review of IPEC.
                                                                                      Enclosure
 
                                            6
The following pertains:
*        Objective 1: Completion of sufficient data collection and assessment to establish
        a new groundwater contaminant baseline, now that the Unit 1 source term has
        been terminated.
As a result of the defueling, drainage, and de-sludging of the Unit 1 spent fuel pool
system in the Fall of 2008, the groundwater contamination source term from the Unit 1
facility was terminated. The inspectors confirmed that Entergy's subsequent data
collection and assessment activities, associated with the continual monitoring of the
residual groundwater contamination, would be sufficient and effective to establish a new
baseline relative to monitoring the residual groundwater condition and subsequent
assessment of dose consequence.
As expected, the first and second-quarter ground-water sample results in 2009, collected
from Monitoring Wells in the immediate vicinity of the Unit 1 spent fuel pool, indicated an
increase in Sr-90 groundwater concentrations . As determined from review of the
licensee's data and analysis, this increased concentration was the expected result of the
volume of water that was necessary to fill the spent fuel pool system to effect defueling.
Accordingly, Entergy's baseline data was predicated on the existing groundwater
conditions determined from its continuing analysis of collected monitoring data. Given
that the original source of the contamination associated with leakage from the Unit 1.
spent fuel pool system has been terminated , the residual groundwater contamination
involving Sr-90 is expected to naturally attenuate over time. The inspectors confirmed
that the current groundwater contaminant concentrations have not, nor are expected to,
affect public health and safety; and the public radiological dose consequence is
expected to continue to be a fraction of the NRC annual regulatory limit affecting liquid
effluents. The inspectors confirmed that continual monitoring of the migration and
attenuation of the Unit 1 associated groundwater contamination condition is being
performed in accordance with Entergy's Long-Term Ground-Water Monitoring Program
(LTGWMP).
The inspectors confirmed that Entergy has established , implemented and maintains a
long-term ground-water monitoring program that has sufficient in scope and
implementation requirements to effectively monitor and assess this condition .
Accordingly, the intent of this objective was considered satisfied.
*        Objective 2: Determination whether active leakage has been terminated or
        continues to persist in regard to the Unit 2 spent fuel pool, and that appropriate
        monitoring and control measures have been implemented , as necessary.
Entergy has been actively engaged in analyzing Monitoring Well data associated with the
H-3 (tritium) groundwater contamination condition that resulted from previously identified
leakage from the Unit 2 spent fuel pool: Entergy's analysis indicated an overall .
decreaSing trend in tritium concentration in the groundwater as a result of previous
efforts to examine the condition of the spent fuel pool and transfer canal liner, and effect
repair, as necessary. Notwithstanding , as previously reported , Entergy's examination of
the spent fuel pool liner was necessarily limited to only the accessible surfaces. That is,
only about 40 % of the total liner surfaces were accessible for examination; the
remaining surfaces were necessarily inaccessible due to the proximity of stored spent
fuel that prevented examination.
                                                                                    Enclosure
 
                                            7
The inspectors reviewed the licensee's analysis derived from groundwater monitoring
data, and confirmed that there was no apparent indication of any significant large flux on-
going active leakage. The inspectors also reviewed the licensee's monitoring well
detection sensitivity data, which supports that active leakage, if occurring, would likely
not exceed 30 gallons per day (0.02 gpm). This sensitivity analysis was based on
comparison of the tritium concentration that is available in the spent fuel pool and the
actual tritium concentration derived from samples collected from relevant monitoring
wells in the near vicinity of the spent fuel pool. Additionally, the inspectors reviewed
licensee analysis and data from a long-term tracer test that indicated the potential for
slow, episodic tritium migration in the fractures of the vadose zone that affect the mobility
of contaminated groundwater from the immediate vicinity of the Unit 2 spent fuel pool to
the water table. The licensee's analysis is supported by the fact that fluorescine dye,
which was injected as part of the groundwater characterization study over two years ago,
is still detectable in certain nearby monitoring wells.
The inspectors noted that there were occasional spikes and general variability in some
monitoring well tritium concentration values that were not characteristic of the expected
attenuation that would normally be expected at this time . Additionally, the licensee
continued to occasionally collect a small quantity of water from the leak collection box
that was installed on the Unit 2 spent fuel pool wall crack that was identified in 2005.
Accordingly, while there was no indication of any significant large flux active leakage,
there was insufficient basis to conclude that there is absolutely no persistent low flux
leakage from the Unit 2 spent fuel pool, at this time.
Notwithstanding, the inspectors determined that the licensee's sensitivity analysis of
groundwater monitoring data, relative to its ability to detect active leakage in excess of
about 30 gallons per day, was reasonably derived. Additionally, the inspectors
confirmed that the current groundwater conditions, even if there was persistent low flux
leakage from the Unit 2 spent fuel pool, has not, nor would be expected to, affect public
health and safety; and the public radiological dose consequence would be expected to
continue to be a fraction of the NRC annual regulatory limit affecting liquid effluents. The
inspectors confirmed that continual monitoring of the migration and attenuation of the
Unit 2 associated groundwater contamination condition was being performed in
accordance with Entergy's Long-Term Ground-Water Monitoring Program; and that the
program implemented appropriate monitoring and control measures for this condition.
The inspectors confirmed that Entergy has established, implemented and maintained a
long-term ground-water monitoring program that has sufficient scope and
implementation requirements to effectively monitor and assess the present condition .
Further, the licensee is considering monitOring in the vadose zone , in the vicinity of the
Unit 2 facility, to assist in the detection of large flux releases . Accordingly, the intent of
this objective was considered satisfied.
*        Objective 3: Establishment and implementation of effluent control and
          environmental monitoring procedures that provide reasonable assurance that the
          existing groundwater conditions will continue to be effectively monitored and
          assessed, that the procedures will detect new or changed conditions in a timely
          manner, and that the procedures are sufficient to monitor natural attenuation of
          the Unit 1 and Unit2 groundwater contamination plumes.
                                                                                      Enclosure
 
                                                8
    The NRC has conducted several inspections (August 2007, October 2008, and August
    2009) of the licensee's Long-Term Ground-Water Monitoring Program. The inspectors
    confirmed that Entergy has established, implemented and maintained a Long-Term
    Ground-Water Monitoring Program that was sufficient in scope and implementation
    requirements to effectively monitor and assess the existing contaminated groundwater
    conditions affecting the Indian Point Energy Center.
    During this inspection, the inspectors examined the refurbishment of the LaFarge No.2
    Monitoring Well (one of the principal off-site monitoring wells) and confirmed its
    acceptability as a valid off-site monitoring location. Additionally, the inspectors verified
    that the administrative controls, established in the Long-Term Groundwater Monitoring
    Program, were sufficient t9 provide assurance of review and appropriate communication
    of activities and changes that affect ground-water monitoring conditions; and that the
    program included sufficient sampling requirements for storm drains and the Unit 1
    foundation drain systems.
    During this inspection, the inspectors reviewed a March 25, 2009 instance involving the
    licensee's detection of tritiated water in the catch basin of a storm drain in the vicinity of
    Unit 3, and in an adjacent shallow monitoring well. The licensee conducted an extensive
    investigation but was unable to find an explanation for this one-time occurrence. The
    inspectors confirmed that the occurrence had no radiological consequence onsite or
    offsite; and no leakage was identified from any Unit 3 component containing tritiated
    water. However, the nature of the occurrence indicated uncertainty in the ability of the
    existing Unit 3 monitoring wells to detect potential leakage from that facility. While there
    was no current on-going leakage affecting the groundwater at Unit 3, Entergy initiated
    action to re-evaluate the Unit 3 groundwater monitoring configuration (both vertically and
    horizontally) to determine its effectiveness in meeting the objectives and
    recommendations of the NEI "Industry Groundwater Protection Initiative- Final Guidance
    Document, August 2007" (ML072600292 and ML07261 0036); and amend the Long-
    Term Groundwater Monitoring Program, as necessary.
    Notwithstanding, the inspectors confirmed that Entergy has established, implemented
    and maintained a Long-Term Ground-Water Monitoring Program that has sufficient
    scope and implementation requirements to effectively monitor and assess the existing *
    groundwater conditions affecting Indian Point Energy Center. Accordingly, the intent of
    this objective was considered satisfied .
.2  Groundwater Sampling
a. Inspection Scope
    During the licensee's groundwater investigation, over 1200 groundwater samples were
    collected and analyzed from the established on-site monitoring well network by the
    second quarter of 2009. The analytical results provide the basis for assessing the extent
    of the groundwater plume and for performing calculations of offsite doses to members of
    the public. In order to assess Entergy's performance in this area, the NRC implemented
    an independent split sample collection program with the licensee beginning in
    September 2005. The monitoring wells selected for independent verification included
    the southem boundary wells and those wells bordering the Hudson River that were used
                                                                                        Enclosure
 
                                                9
      in support of effluent release and dose assessment calculations. Sample identity was
      assured by chain-of-custody procedures that included sample collection observation by
      the NRC or a representative of the NYS DEC. The NRC samples were analyzed by an
      independent govemment laboratory to ensure validation of the licensee's groundwater
      contamination results and off-site environmental sample radioactive measurements.
      By the second quarter of 2009, over 300 split groundwater samples were obtained to
      provide an independent check of Entergy's analytical results and to independently verify
      if there was any detectable migration of groundwater contaminants offsite. These split
      samples represent over 1,200 analyses, primarily for hydrogen-3 (tritium), strontium-90,
      nickel-63, and gamma-emitting radionuclides that characterized the effluent releases.
      Analyses for other radionuclides were performed, but none were detected.
  b. Findings and Assessment
      No findings of significance were identified.
      In general, Entergy's groundwater measurements of radioactivity were of good quality
      and of sufficient sensitivity to assess radiological impact. The quality of Entergy's
      measurements were confirmed by various split samples analyzed by the NRC. Of the
      over 1200 results that were reviewed, there were only a few sample disagreements
      based on the statistical comparison criteria specified in NRC Inspection Procedure
      84750, "Radioactive Waste Treatment, and Effluent and Environmental Monitoring." As
      a result of these few discrepancies, Entergy took corrective action to establish,
      implement, and maintain procedures to effect improved quality control and assurance of
      sample analysis performed by its own laboratory and contract analytical laboratories.
    During the past 3)1" years, the on-site groundwater transport pathway has been
    effectively characterized by the licensee, and a significant quantity of on-site groundwater
    monitoring data has been collected and analyzed by Entergy. A representative numbers
    of split samples have confirmed the overall efficacy of the licensee's analytical capability.
    As the site characterization was tested through pumping and tracer testing, the
    contaminant plume uncertainty has been significantly reduced . Given this
    accomplishment, and the NRC determination that Entergy has demonstrated an effective
    groundwater sample quality control program, the NRC will discontinue any further split
    sampling activities.
40A6 Meetings, including Exit
.1  Exit Meeting Summary
    The inspectors presented the inspection results to Mr. D. Mayer and other licensee and
    New York State representatives on August 19, 2009 and September 4, 2009. The
    licensee acknowledged the findings presented. Based upon discussions with the
    licensee, none of the information presented at the exit meeting and included in this report
    was considered proprietary.
                                                                                        Enclosure
 
                                              A-1
                                        ATTACHMENT
                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
J. Pollock            Site Vice President
M. BaNenik            Principal Engineer, GZA Geo EnVironmental, Inc.
P. Conroy            Director, Nuclear Safety Assurance
D. Croulet            Licensing Engineer
P. Donahue            Chemistry Specialist
C. English            Unit 1 Project Engineer
G. Hinrichs          Project Engineer
D. Loope              Radiation Protection Superintendent
T. Jones              Licensing Engineer
R. LaVera            Radiological Engineer
D. Mayer              Director, Special Projects
J. Michetti          RMS System Engineer
J. Peters            Plant Chemist
D. Rusczyk            Environmental Assessment, GZA
S. Sandike            Chemistry ODCM Specialist
J. Simpson            Environmental Assessment, GZA
R. Walpole            Manager, Licensing
New York State Inspection ObseNers
L. Rosenmann          Engineering Geologist, New York State, Department of Environmental
                      ConseNations
                              INSPECTION PROCEDURES USED
71122.01        Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems
                              LIST OF DOCUMENTS REVIEWED
        Annual Radiological Effluent Release Reports - 2007 and 2008
        Off-Site Dose Calculation Manual, Revision 2
        O-CY-2730, Rev. 1, Airbome Radioactive Effluents
        O-CY-2740, Rev. 1, Liquid Radioactive Effluents
        IP-SMM-CY-001, Rev. 7, Radioactive Effluents Control Program
        IP-SMM-CY-110, Rev. 3, Radiological Groundwater Monitoring Program
        2-CY-2625, Rev. 14, General Plant Systems Specifications and Frequencies
        3-CY-2325, Rev. 8, Radioactive Sampling Schedule
        2-S0P-5.2.4, Rev. 33, Calculation and Recording of Radioactive Gaseous Releases
        2-S0P-5.1.5, Rev. 34, Calculation and Recording of Radioactive Liquid Releases
        3-S0P-WDS-014, Rev. 25, Liquid Waste Releases
                                                                                  Attachment
 
                                              A-2
      3-S0P-WDS-013, Rev. 25, Gaseous Waste Releases
      EN-RP-113, Response to Contaminated Spills/Leaks
      EN-CY-109, Sampling and Analysis of Groundwater Monitoring Wells
      EN-CY-108, Monitoring of Non-Radioactive Systems
      "Industry Groundwater Protection Initiative
      - Final Guidance Document, August 2007" (ML072600292 and ML072610036)
      Unit 2 Liquid Release Permit No. 090016
      Unit 2 Gaseous Release Permit No. 090126
      Unit 3 Liquid Release Permit No. 090081
      Unit 3 Gaseous Release Permit No. 090067
Condition Reports:
CR-IP3-2007 -0803            CR-IP2-2009-1334          CR-IP2-2009-1295
CR-IP2-2009-2089            CR-IP2-2009-2352          CR-IP2-2009-2090
CR-IP3-2009-3356            CR-IP3-2009-3201          CR-IP2-2009-2603
CR-IP2-2009-2528            CR-IP3-2009-3254          CR-IP3-2009-320S
CR-IP2-2009-3307            CR-IP2-2009-3306          CR-IP3-2007 -3953
CR-IP3-2007-3954            CR-IP3-2007-3925          CR-IP3-2007 -41S3
CR-IP2-200S-0270            CR-IP2-2007-5226          CR-IP2-2007-5217
CR-IP2-200S-0375            CR-IP2-200S-0549          CR-IP2-2008-1149
CR-IP3-200S-071S            CR-IP2-200S-0960          CR-IP2-2008-0404
CR-IP2-200S-0377            CR-IP2-200S-0144          CR-IP2-2008-0492
CR-IP2-2009-2266            CR-IP3-200S-0569          CR-IP3-2008-0S46
CR-IP2-200S-1236            CR-IP3-200S-0852          CR-IP2-2008-0179
CR-IP3-2007 -3860            CR-IP3-2008-0942          CR-IP2-2008-3154
CR-IP3-200S-1112            CR-IP2-2008-2468          CR-IP3-2008-0194
CR* IP3*200S*2915            CR-IP3-2008-1215          CR-IP2-2008-3526
CR*IP3*200S*1042            CR-IP2-2008-2581          CR-IP2-2008-2691
CR* IP2*200S*2767            CR-IP3-2008-1218          CR-IP3-2009-00S0
CR*IP2*200S* 4136            CR-IP3-2008-200 1        CR-IP2-2008-2955
CR* IP3*200S*2184            CR-IP2-2008-3342          CR-IP2-2008-3492
CR*IP2*200S*3662            CR-IP3-200S-1S99          CR-IP3-2008-1979
CR*IP3* 200S*2125            CR-IP2-200S-4193          CR-IP2-2008-4108
CR*IP2 c200S*4130            CR-IP2-200S-4254          CR-IP2-2008-4202
CR*IP2*200S*4529            CR-IP2-200S-4337          CR-IP3-2008-2296
CR*IP2-200S-4191            CR-IP3-200S-2279          CR-IP3-2008-2294
CR-IP2-200S-456S            CR-IP3-2008-0624          CR-IP3-2007-0005
CR-IP3-2007-0151            CR-IP3-2007-3367          CR-I P3-2007-27 48
CR-IP3-2007 -2S99            CR-IP3-2007-3061          CR-IP3-2007-2S70
CR-IP3-2007 -2134            CR-IP3-2007 -3075        CR-IP2-2008-1132
CR-IP3-2007-3129            CR-IP2-2008-4S48          CR-IP3-200S-2S62
CR-IP2-2008-4981            CR-IP2-200S-5055          CR-IP2-2009-0477
CR-IP2-2008-5552            CR-IP3-2009-003S          CR-IP2-2009-01S4
CR-IP2-2009-0609            CR-IP2-2009-1125          CR-IP3-2009-0494
CR-IP2-2009-0565            CR-IP2-2009-079S          CR-IP3-2009-0591
CR-IP2-2009-223S
                                                                          Attachment
 
                                          A-3
NRC Groundwater Sample Result Documentation ICY 2009. 1st Quarter)
ML090400502. ML090920949. ML090920932
                              LIST OF ACRONYMS USED
FSAR        Final Safety Analysis Report
GPM        gallons per minute
LTGWMP      Long Term Ground-Water Monitoring Program
NYS DEC    State of New York Department of Environmental Conservation
ODCM        Offsite Dose Calculation Manual
pCi/L      pico-Curies per Liter
PI&R        Problem Identification and Resolution
Rap        Reactor Oversight Process
                                                                      Attachment
}}
}}

Revision as of 05:52, 12 November 2019

Entergy Prefiled Hearing Exhibit ENT000343 - Indian Point Nuclear Generating Units 1, 2 & 3 - NRC Inspection Reports Nos. 05000003/2009008; 05000247/2009008 and 05000286/2009008
ML12089A605
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 10/19/2009
From: Darrell Roberts
Division of Reactor Safety I
To: Joseph E Pollock
Entergy Nuclear Operations, Atomic Safety and Licensing Board Panel
SECY RAS
Shared Package
ML12089A599 List:
References
RAS 22132, ASLBP 07-858-03-LR-BD01, 50-247-LR, 50-286-LR IR-09-008
Download: ML12089A605 (17)


See also: IR 05000003/2009008

Text

ENT000343

Submitted: March 29, 2012

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

October 19, 2009

Mr. Joseph Pollock

Site Vice President

Entergy Nuclear Operations, Inc.

Indian Point Energy Center

450 Broadway, GSB

P.O. Box 249

Buchanan, NY 10511-0249

SUBJECT: INDIAN POINT NUCLEAR GENERATING UNITS 1, 2 & 3 - NRC INSPECTION

REPORT NOS. 05000003/2009008 ; 05000247/2009008; AND

05000286/2009008

Dear Mr. Pollock:

On September 4, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at Indian Point Nuclear Generating Units 1, 2, & 3. The enclosed report documents

the inspection results, which were discussed on August 19 and September 4, 2009, with Mr. Don

Mayer and other members of your staff.

The purpose of this inspection was to assess the establishment, implementation, and

maintenance of your Long-Term Groundwater Monitoring Program ; review the circumstances

surrounding a previously identified occurrence involving the detection of tritated water in a Unit 3

storm drain system; review the performance of the site's Radiation Monitoring System; and

inspect and assess your performance relative to radiological effluents monitoring and control.

The inspection involved an examination of activities conducted under Entergy's license as

related to safety and compliance with the Commission's rules and regulations and with the

conditions of your license. Within these areas, the inspection consisted of a selected

examination of procedures and representative records, observations of activities, interviews with

personnel, and independent assessment activities.

Based on the results of this inspection, no findings of significance were identified . Further, the

inspectors determined that Entergy's Long-Term Groundwater Monitoring Program for the .lndian

Point Energy Center was effectively implemented and maintained in a manner that provided

continued radiological monitoring of the groundwater conditions to confirm conformance with

NRC regulatory requirements relative to the maintenance of public health and safety, and

protection of the environment.

Since 2005, as approved by NRC's Executive Director of Operations, Region I conducted

frequent and focused reviews of your groundwater investigation activities and long-term

monitoring program that exceeded the scope of NRC's normal baseline inspection program. As

a result, we have developed confidence in your commitment and ability to continue effective

monitoring and assessment of the on-site conditions to assure the maintenance of

J. Pollock 2

public health and safety, protection of the environment, and conformance with NRC regulatory

requirements. Our inspectors confirmed that the objectives specified in our deviation

memorandum dated December 16,2008 (ML083590057) have been satisfied. However, we will

continue to monitor your performance in this area, and will re-assess the need for continued

heightened inspection oversight during our end-of-cycle review of your CY 2009 perfonmance.

In accordance with 10 CFR2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document Room

or from the Publicly Available Records (PARS) component of the NRC's document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

J);W~

Darrell J. Roberts, Director

Division of Reactor Safety

Docket Nos: 50-003, 50-247, 50-286

License Nos: DPR-5, DPR-26, DPR-64

Enclosure: Inspection Report Nos. 05000003/2009008, 05000247/2009008,

05000286/2009008

w/Attachment: Supplemental Information

cc w/encj: Distribution via ListServ

J. Pollock 2

public health and safety, protection of the environment, and conformance with NRC regulatory

requirements . Our inspectors confirmed that the objectives specified in our deviation

memorandum dated December 16, 2008 (ML083590057) have been satisfied. However, we will

continue to monitor your performance in this area, and will re-assess the need for continued

heightened inspection oversight during our end-of-cycle review of your CY 2009 performance.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in.the NRC Public Document Room

or from the Publicly Available Records (PARS) component of the NRC's document system

(ADAMS). ADAMS is accessible from the NRC Web site at hllp:llwww.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

IRA by Peter R. Wilson forI

Darrell J. Roberts, Director

Division of Reactor Safety

Docket Nos: 50-003, 50-247, 50-286

License Nos: DPR-5, DPR-26, DPR-64

Enclosure: Inspection Report Nos. 05000003/2009008, 05000247/2009008,

05000286/2009008

w/Allachment: Supplemental Information

cc w/encl: Distribution via ListServ

Distribution w/encl: (via E-mail) S. McCarver, DRP

S. Collins, RA (R10RAMAIL RESOURCE) G. Malone, DRP, Senior Resident Inspector

M. Dapas, DRA (R10RAMAIL - Indian Point 2

RESOURCE) D. Hochmuth , DRP

D. Lew, DRP (R1 DRPMAIL RESOURCE) D. Bearde, DRP

J. Clifford, DRP (R1DRPMAIL Region I Docket Room (w/concurrences)

RESOURCE) ROPreport Resource

L. Trocine, Ri OEDO D. Roberts , DRS

RIDSNRRPMINDIANPOINTRESOURCE P. Wilson, DRS

B. Welling, DRP J. White, DRS

B. Bickell, DRP

SUNSI Review Complete: JRW (Reviewer's Inrtials)

OOCUMENT NAME: G:IORSIPlant Support Branch 2INoggleIIP2009008Rev1 .doc

After declaring this document ~An Official Agency Record w it will be rel eased to the Public.

To receive a copy of this document, Indicate in the box: "e" = COpy without attachment/enclosure "E" = COpy with attachment/enclosure "N" = No CQP"y

OFFICE RIIDRS I RES I RIIDRS I RIIDRP I RIIDRS I

NAME JNoggle/JDN TNicholsonltjn JWhite/jrw' ehg BWeliinglBW DRoberts/prw for

(telecon) for'

DATE 10/06/09 10/14/09 10/19/09 10/16/09 10/16/09

  • see pnor concurrence OFFICIAL RECORD COPY

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos.50-003 , 50-247, 50-286

License Nos. DPR-3, DPR-26, DPR-64

Report Nos. 05000003/2009008, 05000247/2009008, and 05000286/2009008

Licensee: Entergy Nuclear Northeast

Facility: Indian Point Nuclear Generating Station Units 1, 2, & 3

Location: 295 Broadway

Buchanan, NY 10511-0308

Dates: . Augusr18, 2009 - September 4, 2009

Inspectors: J. Noggle, Sr. Health Physicist, CHP, team leader

T. Nicholson, Sr. Technical Advisor for Radionuclide Transport

J. Williams, U.S. Geological Survey, Troy, New York

Approved by: John R. White, Chief

Plant Support Branch 2

Division of Reactor Safety

Enclosure

SUMMARY OF FINDINGS

IR 05000003/2009008, IR 05000247/2009008, IR 05000286/2009008; 08/18/2009 - 9/04/2009;

Indian Point Nuclear Generating Station Units 1, 2 & 3; Other Activities - associated with ROP

deviation memorandum, one PI&R sample, and radioactive effluents baseline inspection.

No findings of significance were identified. The report covers the period from August 18 through

September 4, 2009, and discusses inspection activities conducted by a region-based inspector,

and an inspection team comprised of representatives of Region I, NRC's Office of Research,

and the U. S. Geological Survey. The inspection provided bases for the NRC to determine that

Entergy had completed actions necessary to satisfy the objectives delineated in our deviation

memorandum, "Request for Renewal of Deviation to the Action Matrix to Provide Heightened

NRC Oversight of the Onsite Groundwater Monitoring at the Indian Point Energy Center,"

(ML083590057), dated December 16,2008. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor

Oversight Process," Revision 4, dated December 2006.

ii

Enclosure

Report Details

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety (PS)

2PS1 Gaseous and Liguid Effluents (71122.01 - 3 samples)

a. Inspection Scope

1) The inspector reviewed the following documents to evaluate the effectiveness of the

licensee's radioactive gaseous and liquid effluent control programs relative to the

applicable regulatory requirements specified in the Technical Specifications and the

Offsite Dose Calculation Manual (TS/ODCM).

  • The 2007 and 2008 Radiological Annual Effluent Release Reports were

reviewed including independently assessing selected public dose calculations.

There were no anomalous results reported in these two reports . The report

included discussion of current groundwater conditions and the result of required

monitoring activities; and instances involving out-of-service radiation monitors or

effluent release flow rate monitors were listed in the reports and these were

evaluated during this inspection.

  • The current ODCM was reviewed, including technical justifications for any

changes made since the previous revision.

reviewed to verify the adequacy of system descriptions for gaseous radioactive

waste and station ventilation systems.

  • The latest quality assurance audits of radioactive effluents and chemistry were

reviewed, including Entergy's program for identifying, controlling and assessing

potential contaminated spills and leakage.

  • There were no measurable effluent releases to the environment based on off-site

dose calculations, and there were no reported off-site environmental sample

measurements identifying plant-related radioactive materials during the 2007 and

2008 report period.

2) The inspector observed the following plant equipment and work activities to evaluate the

effectiveness of the licensee's radioactive gaseous and liquid effluent control programs.

  • Walkdowns were performed of accessible gaseous and liquid release system

components to review any recent changes or modifications; and to confirm the

alignment, operation and material condition of the radioactive liquid and

gaseous effluent radiation monitoring systems (RMS) at Units 1, 2 and 3.

  • Observations were conducted of radioactive effluent related sampling and

associated laboratory measurement techniques.

  • Procedural controls and selected radioactive gaseous and liquid effluent release

permits were reviewed to verify that radiation monitor alarm setpoint values and

releases were in agreement with Technical Specification and ODCM

requirements.

Enclosure

2

  • Chemistry logs, relative to out-of-service radiation monitoring conditions, were

reviewed to confirm the performance of compensatory sampling activities.

  • Surveillance tests of gaseous filtration discharge systems were reviewed to

confirm operability and ventilation flow rates with respect to the assumed flow

rates used in gaseous effluent release calculations.

  • Entergy's surveillance program of non-radioactive system interfaces with

radioactive process systems was reviewed to confirm effective monitoring and

control of potential effluent discharge paths to the environment.

  • Radiation monitoring system and chemistry laboratory counting instrument

calibration and quality control records were reviewed with respect to ODCM

surveillance requirements to confirm the licensee's ability identify and report

detectable radionuclides in radioactive measurement results.

3) Radioactive effluent control related corrective action program activities for 2007 through

August 2009 were reviewed, including the results of audits and the resolution of issues

identified through the condition report system. A comprehensive review was conducted

of conditions and occurrences involving out-of-service radiation monitoring system

components. Section 40A2 pertains.

b. Findings and Observations

No findings of significance were identified. The following table summarizes the dose

consequence of radiological effluent release in the period between 2007 and 2008.

Table of Effluent Release calculated dose and public dose limits for 2007 and 2008

Dose in Air Dose %of Air Dose %of liquid '10 of Liquid %of

mrem/yr Whole limit Max Organ Limit Dose limit Dose limit

Body WB MaxO

2007 Units 1&2 2.43E-3 0.016 2.43E-3 0.016 5.35E-4 0.018 1.3E-3 0.013

2008 Units 1&2 2.07E-3 0.014 2.67E-3 0.018 6.11E-4 0.020 1.47E-3 0.Q15

2007 Unit 3 3.BBE-3 0.026 3.BBE-3 0.026 3.2E-4 0.007 2.14E-4 0.002

2008 Unit 3 1.99E-3 0.013 1.99E-3 0.013 1.56E-4 0.005 2.B3E-4 0.003

2007 Groundwater 2.66E-4 0.009 9.94E-4 0.01

2008 Groundwater 2.86E-4 0.009 9.35E-4 0.009

4. OTHER ACTIVITIES (OA)

40A2 Identification and Resolution of Problems

Cornerstone: Public Radiation Safety

.1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

a. Inspection Scope (71122.01)

The inspector reviewed approximately one hundred corrective action condition reports,

initiated between january 2007 and August 2009, that were associated with the gaseous,

liquid, and groundwater radioactive effluents program. The review was performed to

Enclosure

3

verify that problems identified by these condition reports were properly characterized in

the licensee's event reporting system, causes were identified, and actions implemented

commensurate the safety significance of the matters.

b. Findings and Observations

No findings of significance were identified .

.2 Radioactive Effluent Radiation Monitor System (RMS) Maintenance (71152 - 1 sample)

a. Inspection Scope

The inspectors conducted a review corrective action program condition reports

associated with out-of-service radiation monitoring system equipment that was identified

in the period between January 2007 and August 2009. Licensee personnel having

cognizance of Radiation Monitoring System (RMS) performance and activities were

interviewed, including the RMS system engineer and senior chemistry staff. "Radiation

Monitoring System, Second Quarter 2009, Condition Report Trend Review for Radiation .

Monitoring System Improvement: dated September 2, 2009, was also reviewed.

b. Findings and Observations

No findings of Significance were identified.

A large number of condition reports associated with the radiation monitoring system were

initiated during the past two years . Most of the condition reports were associated with

interruption of service of the RMS display consoles in both the Unit 2 and Unit 3 control

rooms. While these temporary display outages affected operators' ability to poll

individual detector readout displays, they did not interfere with control room annunciator

actuation or actual detector operability.

The cause of the Unit 3 display console issues was determined to be related to

excessive temperature in the RMS electronics cabinets that affected certain control room

RMS display console components. Short-term corrective actions included installing

permanent air conditioning to effect improved cooling of the RMS electronics cabinets.

The cause of Unit 2 RMS display console service interruptions continues to be under

review. Notwithstanding, Entergy is evaluating replacing the RMS display console

equipment in both control rooms to support station-wide computer network access

improvements.

Less frequently occurring RMS equipment issues remain to be resolved, including

occurrences involving the R-56 detectors, which monitor the discharge of waste sewage

from Units 2 and 3. The location of these detectors was determined to be susceptible to

failure due to flooding , power spiking, and power outages. In such conditions, waste

sewage is diverted to an on-site holding tank in order to conduct sampling prior to off-site

release . Accordingly, there is no safety significance to these RMS system failures. The

inspector confirmed that the licensee has implemented appropriate remedial actions for

these occurrences, and has initiated actions to improve the operating environment and

detector function to reduce the out-of-service time.

Enclosure

4

Entergy has identified the Unit 2 RMS as an upgrade project in its Top Ten Action Plan

for 2009. System engineering activities have been initiated for this improvement activity.

The inspector determined that the majority of identified problems with the Unit 2 and Unit

3 radiation monitoring systems were not associated with radiation detector operability or

effluent release control functions. For those instances that resulted in out-of-service

conditions, the licensee implemented appropriate compensatory measures as required

by regulatory requirements. The inspector confirmed that Entergy is engaged in RMS

. improvement activities, and has initiated appropriate corrective actions.

40A5 Other Activities

.1 Assessment of Licensee Performance Relative to Meeting the Objectives of the

December 16.2008 Memorandum Reguesting Deviation from the Action Matrix

Background:

On September 1, 2005, the NRC was informed by Entergy that cracks in a Unit 2 spent

fuel pool wall had been discovered during excavation work inside the spent fuel pool

building. Low levels of radioactive contamination were found in the vicinity. Entergy's

initial investigation of the issue revealed that groundwater in the vicinity was

contaminated with tritium. On September 20, 2005, Region I initiated a special inspection

of this matter to examine the licensee's performance and determine if the contaminated

groundwater affected, or could affect, public health and safety. Subsequently, Entergy

initiated actions to perform a comprehensive groundwater site characterization, identify

the sources, and effect mitigation and remediation of the condition.

The NRC special inspection report, issued in March 2006, assessed Entergy's

performance, achievements, and plans for more extensive site characterization, and

reported that the groundwater contamination did not, nor was likely to, adversely affect

public health and safety. In the report, and subsequent public meetings, NRC indicated

that a final conclusion would be reached after Entergy completed its groundwater

characterization initiative.

The NRC Region I continued inspection and monitoring of Entergy's activities in

accordance with successive approved deviation to the normal Reactor Oversight

Process for calendar years 2006 (ML053010404), 2007 (ML063480016), 2008

(ML073480290) and 2009 (ML083590057). During this period, the NRC staff closely

monitored Entergy's groundwater characterization efforts, performed independent

inspections and testing, and independently evaluated radiological and hydrological

conditions affecting groundwater onsite. Additionally, the NRC independently verified

groundwater releases by conducting split monitoring well sampling with Entergy and the

State of New York.

On January 11, 2008, Entergy submitted the results of its comprehensive hydrogeologic

site characterization investigation (ML080320600), and included its plan for remediation

and long-term monitoring of the on-site groundwater conditions. In its report, Entergy

described the source of groundwater contamination to be from the Unit 1 and Unit 2

spent fuel pools. The NRC documented its review of Entergy's report in inspection report

05000247 & 05000003/2007010 on May 13, 2008 (ML081340425). In a subsequent

inspection 05000247/2008004 (ML08311 0566) dated November 6,2008, the NRC

Enclosure

5

confirmed that Entergy's conceptual site model of the site, which included both the

vadose zone and saturated zone processes and conditions, effectively characterized the

onsite groundwater plume behavior and radionuclide transport. Evaluation of

radionuclide concentrations and pathway analyses indicated that the groundwater

contamination did not adversely affect public health and safety. Detailed discussions

and analyses indicated that the licensee's plans for long-term monitoring of the site,

relative to monitoring natural attenuation of residual groundwater contamination, were

reasonable.

On November 3, 2008, Entergy completed Unit 1 spent fuel pool system drainage and

sludge removal activities, essentially terminating the source from that facility. Given the

change in conditions, Entergy initiated actions to establish a new groundwater

contaminant baseline in support of its long-term monitoring program.

a. Inspection Scope

The most recently approved Memorandum of Deviation, i.e., "Request for Renewal of

Deviation to the Action Matrix to Provide Heightened NRC Oversight of the Onsite

Groundwater Monitoring at the Indian Point Energy Center," dated December 16, 2008

(ML083590057), identified the following objectives to be addressed in order to support

resumption of normal inspection activities in accordance with the Reactor Oversight

Process:

  • Entergy has completed sufficient data collection and assessment to establish a

new groundwater contaminant baseline, now that the Unit 1 source term has

been terminated.

  • Entergy has determined whether active leakage has been terminated or

continues to persist in regard to the Unit 2 spent fuel pool; and has implemented

appropriate monitoring and control measures, as necessary.

  • Entergy has established and implemented effluent control and environmental

monitoring procedures that provide reasonable assurance that the existing

groundwater conditions will continue to be effectively monitored and assessed,

that the procedures will detect new or changed conditions in a timely manner, and

that the procedures are sufficient to monitor natural attenuation of the Unit 1 and

Unit 2 groundwater contamination plumes.

The NRC team reviewed the licensee's performance and achievements relative to the

completion of these objectives.

b. Findings and Observations

No findings of significance were identified.

The inspectors determined that Entergy completed the actions necessary to satisfy the

objectives delineated in the approved Memorandum of Deviation, dated December 16,

2008, (ML083590057). Notwithstanding, NRC will continue to monitor performance in

this area, and re-assess the need for continued heightened inspection oversight as part

of the CY 2009 end-of-cycle performance review of IPEC.

Enclosure

6

The following pertains:

  • Objective 1: Completion of sufficient data collection and assessment to establish

a new groundwater contaminant baseline, now that the Unit 1 source term has

been terminated.

As a result of the defueling, drainage, and de-sludging of the Unit 1 spent fuel pool

system in the Fall of 2008, the groundwater contamination source term from the Unit 1

facility was terminated. The inspectors confirmed that Entergy's subsequent data

collection and assessment activities, associated with the continual monitoring of the

residual groundwater contamination, would be sufficient and effective to establish a new

baseline relative to monitoring the residual groundwater condition and subsequent

assessment of dose consequence.

As expected, the first and second-quarter ground-water sample results in 2009, collected

from Monitoring Wells in the immediate vicinity of the Unit 1 spent fuel pool, indicated an

increase in Sr-90 groundwater concentrations . As determined from review of the

licensee's data and analysis, this increased concentration was the expected result of the

volume of water that was necessary to fill the spent fuel pool system to effect defueling.

Accordingly, Entergy's baseline data was predicated on the existing groundwater

conditions determined from its continuing analysis of collected monitoring data. Given

that the original source of the contamination associated with leakage from the Unit 1.

spent fuel pool system has been terminated , the residual groundwater contamination

involving Sr-90 is expected to naturally attenuate over time. The inspectors confirmed

that the current groundwater contaminant concentrations have not, nor are expected to,

affect public health and safety; and the public radiological dose consequence is

expected to continue to be a fraction of the NRC annual regulatory limit affecting liquid

effluents. The inspectors confirmed that continual monitoring of the migration and

attenuation of the Unit 1 associated groundwater contamination condition is being

performed in accordance with Entergy's Long-Term Ground-Water Monitoring Program

(LTGWMP).

The inspectors confirmed that Entergy has established , implemented and maintains a

long-term ground-water monitoring program that has sufficient in scope and

implementation requirements to effectively monitor and assess this condition .

Accordingly, the intent of this objective was considered satisfied.

  • Objective 2: Determination whether active leakage has been terminated or

continues to persist in regard to the Unit 2 spent fuel pool, and that appropriate

monitoring and control measures have been implemented , as necessary.

Entergy has been actively engaged in analyzing Monitoring Well data associated with the

H-3 (tritium) groundwater contamination condition that resulted from previously identified

leakage from the Unit 2 spent fuel pool: Entergy's analysis indicated an overall .

decreaSing trend in tritium concentration in the groundwater as a result of previous

efforts to examine the condition of the spent fuel pool and transfer canal liner, and effect

repair, as necessary. Notwithstanding , as previously reported , Entergy's examination of

the spent fuel pool liner was necessarily limited to only the accessible surfaces. That is,

only about 40 % of the total liner surfaces were accessible for examination; the

remaining surfaces were necessarily inaccessible due to the proximity of stored spent

fuel that prevented examination.

Enclosure

7

The inspectors reviewed the licensee's analysis derived from groundwater monitoring

data, and confirmed that there was no apparent indication of any significant large flux on-

going active leakage. The inspectors also reviewed the licensee's monitoring well

detection sensitivity data, which supports that active leakage, if occurring, would likely

not exceed 30 gallons per day (0.02 gpm). This sensitivity analysis was based on

comparison of the tritium concentration that is available in the spent fuel pool and the

actual tritium concentration derived from samples collected from relevant monitoring

wells in the near vicinity of the spent fuel pool. Additionally, the inspectors reviewed

licensee analysis and data from a long-term tracer test that indicated the potential for

slow, episodic tritium migration in the fractures of the vadose zone that affect the mobility

of contaminated groundwater from the immediate vicinity of the Unit 2 spent fuel pool to

the water table. The licensee's analysis is supported by the fact that fluorescine dye,

which was injected as part of the groundwater characterization study over two years ago,

is still detectable in certain nearby monitoring wells.

The inspectors noted that there were occasional spikes and general variability in some

monitoring well tritium concentration values that were not characteristic of the expected

attenuation that would normally be expected at this time . Additionally, the licensee

continued to occasionally collect a small quantity of water from the leak collection box

that was installed on the Unit 2 spent fuel pool wall crack that was identified in 2005.

Accordingly, while there was no indication of any significant large flux active leakage,

there was insufficient basis to conclude that there is absolutely no persistent low flux

leakage from the Unit 2 spent fuel pool, at this time.

Notwithstanding, the inspectors determined that the licensee's sensitivity analysis of

groundwater monitoring data, relative to its ability to detect active leakage in excess of

about 30 gallons per day, was reasonably derived. Additionally, the inspectors

confirmed that the current groundwater conditions, even if there was persistent low flux

leakage from the Unit 2 spent fuel pool, has not, nor would be expected to, affect public

health and safety; and the public radiological dose consequence would be expected to

continue to be a fraction of the NRC annual regulatory limit affecting liquid effluents. The

inspectors confirmed that continual monitoring of the migration and attenuation of the

Unit 2 associated groundwater contamination condition was being performed in

accordance with Entergy's Long-Term Ground-Water Monitoring Program; and that the

program implemented appropriate monitoring and control measures for this condition.

The inspectors confirmed that Entergy has established, implemented and maintained a

long-term ground-water monitoring program that has sufficient scope and

implementation requirements to effectively monitor and assess the present condition .

Further, the licensee is considering monitOring in the vadose zone , in the vicinity of the

Unit 2 facility, to assist in the detection of large flux releases . Accordingly, the intent of

this objective was considered satisfied.

  • Objective 3: Establishment and implementation of effluent control and

environmental monitoring procedures that provide reasonable assurance that the

existing groundwater conditions will continue to be effectively monitored and

assessed, that the procedures will detect new or changed conditions in a timely

manner, and that the procedures are sufficient to monitor natural attenuation of

the Unit 1 and Unit2 groundwater contamination plumes.

Enclosure

8

The NRC has conducted several inspections (August 2007, October 2008, and August

2009) of the licensee's Long-Term Ground-Water Monitoring Program. The inspectors

confirmed that Entergy has established, implemented and maintained a Long-Term

Ground-Water Monitoring Program that was sufficient in scope and implementation

requirements to effectively monitor and assess the existing contaminated groundwater

conditions affecting the Indian Point Energy Center.

During this inspection, the inspectors examined the refurbishment of the LaFarge No.2

Monitoring Well (one of the principal off-site monitoring wells) and confirmed its

acceptability as a valid off-site monitoring location. Additionally, the inspectors verified

that the administrative controls, established in the Long-Term Groundwater Monitoring

Program, were sufficient t9 provide assurance of review and appropriate communication

of activities and changes that affect ground-water monitoring conditions; and that the

program included sufficient sampling requirements for storm drains and the Unit 1

foundation drain systems.

During this inspection, the inspectors reviewed a March 25, 2009 instance involving the

licensee's detection of tritiated water in the catch basin of a storm drain in the vicinity of

Unit 3, and in an adjacent shallow monitoring well. The licensee conducted an extensive

investigation but was unable to find an explanation for this one-time occurrence. The

inspectors confirmed that the occurrence had no radiological consequence onsite or

offsite; and no leakage was identified from any Unit 3 component containing tritiated

water. However, the nature of the occurrence indicated uncertainty in the ability of the

existing Unit 3 monitoring wells to detect potential leakage from that facility. While there

was no current on-going leakage affecting the groundwater at Unit 3, Entergy initiated

action to re-evaluate the Unit 3 groundwater monitoring configuration (both vertically and

horizontally) to determine its effectiveness in meeting the objectives and

recommendations of the NEI "Industry Groundwater Protection Initiative- Final Guidance

Document, August 2007" (ML072600292 and ML07261 0036); and amend the Long-

Term Groundwater Monitoring Program, as necessary.

Notwithstanding, the inspectors confirmed that Entergy has established, implemented

and maintained a Long-Term Ground-Water Monitoring Program that has sufficient

scope and implementation requirements to effectively monitor and assess the existing *

groundwater conditions affecting Indian Point Energy Center. Accordingly, the intent of

this objective was considered satisfied .

.2 Groundwater Sampling

a. Inspection Scope

During the licensee's groundwater investigation, over 1200 groundwater samples were

collected and analyzed from the established on-site monitoring well network by the

second quarter of 2009. The analytical results provide the basis for assessing the extent

of the groundwater plume and for performing calculations of offsite doses to members of

the public. In order to assess Entergy's performance in this area, the NRC implemented

an independent split sample collection program with the licensee beginning in

September 2005. The monitoring wells selected for independent verification included

the southem boundary wells and those wells bordering the Hudson River that were used

Enclosure

9

in support of effluent release and dose assessment calculations. Sample identity was

assured by chain-of-custody procedures that included sample collection observation by

the NRC or a representative of the NYS DEC. The NRC samples were analyzed by an

independent govemment laboratory to ensure validation of the licensee's groundwater

contamination results and off-site environmental sample radioactive measurements.

By the second quarter of 2009, over 300 split groundwater samples were obtained to

provide an independent check of Entergy's analytical results and to independently verify

if there was any detectable migration of groundwater contaminants offsite. These split

samples represent over 1,200 analyses, primarily for hydrogen-3 (tritium), strontium-90,

nickel-63, and gamma-emitting radionuclides that characterized the effluent releases.

Analyses for other radionuclides were performed, but none were detected.

b. Findings and Assessment

No findings of significance were identified.

In general, Entergy's groundwater measurements of radioactivity were of good quality

and of sufficient sensitivity to assess radiological impact. The quality of Entergy's

measurements were confirmed by various split samples analyzed by the NRC. Of the

over 1200 results that were reviewed, there were only a few sample disagreements

based on the statistical comparison criteria specified in NRC Inspection Procedure

84750, "Radioactive Waste Treatment, and Effluent and Environmental Monitoring." As

a result of these few discrepancies, Entergy took corrective action to establish,

implement, and maintain procedures to effect improved quality control and assurance of

sample analysis performed by its own laboratory and contract analytical laboratories.

During the past 3)1" years, the on-site groundwater transport pathway has been

effectively characterized by the licensee, and a significant quantity of on-site groundwater

monitoring data has been collected and analyzed by Entergy. A representative numbers

of split samples have confirmed the overall efficacy of the licensee's analytical capability.

As the site characterization was tested through pumping and tracer testing, the

contaminant plume uncertainty has been significantly reduced . Given this

accomplishment, and the NRC determination that Entergy has demonstrated an effective

groundwater sample quality control program, the NRC will discontinue any further split

sampling activities.

40A6 Meetings, including Exit

.1 Exit Meeting Summary

The inspectors presented the inspection results to Mr. D. Mayer and other licensee and

New York State representatives on August 19, 2009 and September 4, 2009. The

licensee acknowledged the findings presented. Based upon discussions with the

licensee, none of the information presented at the exit meeting and included in this report

was considered proprietary.

Enclosure

A-1

ATTACHMENT

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Pollock Site Vice President

M. BaNenik Principal Engineer, GZA Geo EnVironmental, Inc.

P. Conroy Director, Nuclear Safety Assurance

D. Croulet Licensing Engineer

P. Donahue Chemistry Specialist

C. English Unit 1 Project Engineer

G. Hinrichs Project Engineer

D. Loope Radiation Protection Superintendent

T. Jones Licensing Engineer

R. LaVera Radiological Engineer

D. Mayer Director, Special Projects

J. Michetti RMS System Engineer

J. Peters Plant Chemist

D. Rusczyk Environmental Assessment, GZA

S. Sandike Chemistry ODCM Specialist

J. Simpson Environmental Assessment, GZA

R. Walpole Manager, Licensing

New York State Inspection ObseNers

L. Rosenmann Engineering Geologist, New York State, Department of Environmental

ConseNations

INSPECTION PROCEDURES USED

71122.01 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

LIST OF DOCUMENTS REVIEWED

Annual Radiological Effluent Release Reports - 2007 and 2008

Off-Site Dose Calculation Manual, Revision 2

O-CY-2730, Rev. 1, Airbome Radioactive Effluents

O-CY-2740, Rev. 1, Liquid Radioactive Effluents

IP-SMM-CY-001, Rev. 7, Radioactive Effluents Control Program

IP-SMM-CY-110, Rev. 3, Radiological Groundwater Monitoring Program

2-CY-2625, Rev. 14, General Plant Systems Specifications and Frequencies

3-CY-2325, Rev. 8, Radioactive Sampling Schedule

2-S0P-5.2.4, Rev. 33, Calculation and Recording of Radioactive Gaseous Releases

2-S0P-5.1.5, Rev. 34, Calculation and Recording of Radioactive Liquid Releases

3-S0P-WDS-014, Rev. 25, Liquid Waste Releases

Attachment

A-2

3-S0P-WDS-013, Rev. 25, Gaseous Waste Releases

EN-RP-113, Response to Contaminated Spills/Leaks

EN-CY-109, Sampling and Analysis of Groundwater Monitoring Wells

EN-CY-108, Monitoring of Non-Radioactive Systems

"Industry Groundwater Protection Initiative

- Final Guidance Document, August 2007" (ML072600292 and ML072610036)

Unit 2 Liquid Release Permit No. 090016

Unit 2 Gaseous Release Permit No. 090126

Unit 3 Liquid Release Permit No. 090081

Unit 3 Gaseous Release Permit No. 090067

Condition Reports:

CR-IP3-2007 -0803 CR-IP2-2009-1334 CR-IP2-2009-1295

CR-IP2-2009-2089 CR-IP2-2009-2352 CR-IP2-2009-2090

CR-IP3-2009-3356 CR-IP3-2009-3201 CR-IP2-2009-2603

CR-IP2-2009-2528 CR-IP3-2009-3254 CR-IP3-2009-320S

CR-IP2-2009-3307 CR-IP2-2009-3306 CR-IP3-2007 -3953

CR-IP3-2007-3954 CR-IP3-2007-3925 CR-IP3-2007 -41S3

CR-IP2-200S-0270 CR-IP2-2007-5226 CR-IP2-2007-5217

CR-IP2-200S-0375 CR-IP2-200S-0549 CR-IP2-2008-1149

CR-IP3-200S-071S CR-IP2-200S-0960 CR-IP2-2008-0404

CR-IP2-200S-0377 CR-IP2-200S-0144 CR-IP2-2008-0492

CR-IP2-2009-2266 CR-IP3-200S-0569 CR-IP3-2008-0S46

CR-IP2-200S-1236 CR-IP3-200S-0852 CR-IP2-2008-0179

CR-IP3-2007 -3860 CR-IP3-2008-0942 CR-IP2-2008-3154

CR-IP3-200S-1112 CR-IP2-2008-2468 CR-IP3-2008-0194

CR* IP3*200S*2915 CR-IP3-2008-1215 CR-IP2-2008-3526

CR*IP3*200S*1042 CR-IP2-2008-2581 CR-IP2-2008-2691

CR* IP2*200S*2767 CR-IP3-2008-1218 CR-IP3-2009-00S0

CR*IP2*200S* 4136 CR-IP3-2008-200 1 CR-IP2-2008-2955

CR* IP3*200S*2184 CR-IP2-2008-3342 CR-IP2-2008-3492

CR*IP2*200S*3662 CR-IP3-200S-1S99 CR-IP3-2008-1979

CR*IP3* 200S*2125 CR-IP2-200S-4193 CR-IP2-2008-4108

CR*IP2 c200S*4130 CR-IP2-200S-4254 CR-IP2-2008-4202

CR*IP2*200S*4529 CR-IP2-200S-4337 CR-IP3-2008-2296

CR*IP2-200S-4191 CR-IP3-200S-2279 CR-IP3-2008-2294

CR-IP2-200S-456S CR-IP3-2008-0624 CR-IP3-2007-0005

CR-IP3-2007-0151 CR-IP3-2007-3367 CR-I P3-2007-27 48

CR-IP3-2007 -2S99 CR-IP3-2007-3061 CR-IP3-2007-2S70

CR-IP3-2007 -2134 CR-IP3-2007 -3075 CR-IP2-2008-1132

CR-IP3-2007-3129 CR-IP2-2008-4S48 CR-IP3-200S-2S62

CR-IP2-2008-4981 CR-IP2-200S-5055 CR-IP2-2009-0477

CR-IP2-2008-5552 CR-IP3-2009-003S CR-IP2-2009-01S4

CR-IP2-2009-0609 CR-IP2-2009-1125 CR-IP3-2009-0494

CR-IP2-2009-0565 CR-IP2-2009-079S CR-IP3-2009-0591

CR-IP2-2009-223S

Attachment

A-3

NRC Groundwater Sample Result Documentation ICY 2009. 1st Quarter)

ML090400502. ML090920949. ML090920932

LIST OF ACRONYMS USED

FSAR Final Safety Analysis Report

GPM gallons per minute

LTGWMP Long Term Ground-Water Monitoring Program

NYS DEC State of New York Department of Environmental Conservation

ODCM Offsite Dose Calculation Manual

pCi/L pico-Curies per Liter

PI&R Problem Identification and Resolution

Rap Reactor Oversight Process

Attachment