ML12334A503: Difference between revisions
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{{#Wiki_filter:United States Nuclear Regulatory Commission Official Hearing Exhibit | {{#Wiki_filter:United States Nuclear Regulatory Commission Official Hearing Exhibit NYS000035 Entergy Nuclear Operations, Inc. | ||
In the Matter of: | |||
ASLBP #:07-858-03-LR-BD01 Docket #:05000247 l 05000286 Exhibit # | (Indian Point Nuclear Generating Units 2 and 3) Submitted: December 12, 2011 u....~p..p. REG(J~)- ASLBP #: 07-858-03-LR-BD01 | ||
!~~ :" | |||
Docket #: 05000247 l 05000286 | |||
~ 0 Exhibit #: NYS000035-00-BD01 Identified: 10/15/2012 | |||
~ ~ | |||
-REGION III October 19, 2011 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE | I./l I ' ~ | ||
-PNO-III-11-012A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. | Admitted: 10/15/2012 Withdrawn: | ||
The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date. Facility Perry Nuclear Power Plant FirstEnergy Nuclear Operating Company Perry, Ohio Docket: 50-440 License: NPF-58 | ~ ~ | ||
~1-: | |||
" .*..... ,- | |||
0- Rejected: | |||
Other: | |||
Stricken: | |||
PRELIMINARY NOTIFICATION - REGION III October 19, 2011 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-11-012A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date. | |||
Facility Licensee Emergency Classification Perry Nuclear Power Plant Notification of Unusual Event FirstEnergy Nuclear Operating Company Alert Perry, Ohio _ Site Area Emergency Docket: 50-440 _ General Emergency License: NPF-58 .x.. Not Applicable | |||
==SUBJECT:== | ==SUBJECT:== | ||
PERRY UNPLANNED SHUTDOWN GREATER THAN 72 HOURS (UPDATE) DESCRIPTION: | PERRY UNPLANNED SHUTDOWN GREATER THAN 72 HOURS (UPDATE) | ||
On October 2,2011, at 1 :00 a.m. (EDT), Perry Nuclear Power Plant began to shut down the reactor (Event Notification 47312) as required by Technical Specification 3.8.1.A.2 due to one of two required off-site power sources being inoperable. | DESCRIPTION: | ||
On October 2,2011, at 1:00 a.m. (EDT), Perry Nuclear Power Plant began to shut down the reactor (Event Notification 47312) as required by Technical Specification 3.8.1.A.2 due to one of two required off-site power sources being inoperable. | |||
The Unit 1 startup transformer, one of the two required off-site power sources, was declared inoperable at 5:29 a.m. (EDT) on September 29,2011, due to a suspected internal electrical fault, which also caused a crack in the reservoir that holds oil used to cool the transformer. | The Unit 1 startup transformer, one of the two required off-site power sources, was declared inoperable at 5:29 a.m. (EDT) on September 29,2011, due to a suspected internal electrical fault, which also caused a crack in the reservoir that holds oil used to cool the transformer. | ||
This put the plant in a Technical Specification Limiting Condition for Operation (LCO) to restore the startup transformer within 72 hours or shutdown. | This put the plant in a Technical Specification Limiting Condition for Operation (LCO) to restore the startup transformer within 72 hours or shutdown. The other source of off-site power remained available. | ||
The other source of off-site power remained available. | |||
On October 17, 2011, the NRC approved an emergency, one-time Technical Specification amendment request to allow the licensee to operate for approximately 60 days with the startup transformer currently out-of-service, while another transformer is modified and installed. | On October 17, 2011, the NRC approved an emergency, one-time Technical Specification amendment request to allow the licensee to operate for approximately 60 days with the startup transformer currently out-of-service, while another transformer is modified and installed. | ||
The NRC resident inspectors verified that the compensatory actions specified in the Technical Specification amendment were implemented. | The NRC resident inspectors verified that the compensatory actions specified in the Technical Specification amendment were implemented. Perry was restarted on October 19, 2011. | ||
Perry was restarted on October 19, 2011. The NRC resident inspectors monitored plant shutdown and restart, and will continue to monitor licensee compensatory actions and activities as they complete the replacement of the transformer. | The NRC resident inspectors monitored plant shutdown and restart, and will continue to monitor licensee compensatory actions and activities as they complete the replacement of the transformer. | ||
The information presented herein has been discussed with the licensee and is current as of October 19, 2011, at 8:30 a.m. (EDT). ADAMS Accession Number ML11292A119 CONTACTS: | The information presented herein has been discussed with the licensee and is current as of October 19, 2011, at 8:30 a.m. (EDT). | ||
Mark Marshfield 440/259-361 0 Mark. Marshfield@nrc.gov | ADAMS Accession Number ML11292A119 CONTACTS: Mark Marshfield John Giessner 440/259-361 0 630/829-9619 Mark. Marshfield@nrc.gov John. Giessner@nrc.gov OAG10001354_00001}} | ||
Revision as of 19:36, 11 November 2019
| ML12334A503 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 12/12/2011 |
| From: | Jack Giessner, Marshfield M Reactor Projects Region 3 Branch 4 |
| To: | Atomic Safety and Licensing Board Panel |
| SECY RAS | |
| References | |
| RAS 21523, 50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01 | |
| Download: ML12334A503 (1) | |
Text
United States Nuclear Regulatory Commission Official Hearing Exhibit NYS000035 Entergy Nuclear Operations, Inc.
In the Matter of:
(Indian Point Nuclear Generating Units 2 and 3) Submitted: December 12, 2011 u....~p..p. REG(J~)- ASLBP #: 07-858-03-LR-BD01
!~~ :"
Docket #: 05000247 l 05000286
~ 0 Exhibit #: NYS000035-00-BD01 Identified: 10/15/2012
~ ~
I./l I ' ~
Admitted: 10/15/2012 Withdrawn:
~ ~
~1-:
" .*..... ,-
0- Rejected:
Other:
Stricken:
PRELIMINARY NOTIFICATION - REGION III October 19, 2011 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-11-012A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.
Facility Licensee Emergency Classification Perry Nuclear Power Plant Notification of Unusual Event FirstEnergy Nuclear Operating Company Alert Perry, Ohio _ Site Area Emergency Docket: 50-440 _ General Emergency License: NPF-58 .x.. Not Applicable
SUBJECT:
PERRY UNPLANNED SHUTDOWN GREATER THAN 72 HOURS (UPDATE)
DESCRIPTION:
On October 2,2011, at 1:00 a.m. (EDT), Perry Nuclear Power Plant began to shut down the reactor (Event Notification 47312) as required by Technical Specification 3.8.1.A.2 due to one of two required off-site power sources being inoperable.
The Unit 1 startup transformer, one of the two required off-site power sources, was declared inoperable at 5:29 a.m. (EDT) on September 29,2011, due to a suspected internal electrical fault, which also caused a crack in the reservoir that holds oil used to cool the transformer.
This put the plant in a Technical Specification Limiting Condition for Operation (LCO) to restore the startup transformer within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or shutdown. The other source of off-site power remained available.
On October 17, 2011, the NRC approved an emergency, one-time Technical Specification amendment request to allow the licensee to operate for approximately 60 days with the startup transformer currently out-of-service, while another transformer is modified and installed.
The NRC resident inspectors verified that the compensatory actions specified in the Technical Specification amendment were implemented. Perry was restarted on October 19, 2011.
The NRC resident inspectors monitored plant shutdown and restart, and will continue to monitor licensee compensatory actions and activities as they complete the replacement of the transformer.
The information presented herein has been discussed with the licensee and is current as of October 19, 2011, at 8:30 a.m. (EDT).
ADAMS Accession Number ML11292A119 CONTACTS: Mark Marshfield John Giessner 440/259-361 0 630/829-9619 Mark. Marshfield@nrc.gov John. Giessner@nrc.gov OAG10001354_00001