ENS 45753: Difference between revisions

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| event date = 03/08/2010 16:35 CST
| event date = 03/08/2010 16:35 CST
| last update date = 03/08/2010
| last update date = 03/08/2010
| title = Automatic Reactor Scram On Low Reactor Water Level
| title = Automatic Reactor Scram on Low Reactor Water Level
| event text = An 'A' reactor feed pump trip occurred and initiated a recirculation pump flow control valve runback.  During the flow control valve runback, the 'A' recirculation hydraulic power unit tripped causing an incomplete runback.
| event text = An 'A' reactor feed pump trip occurred and initiated a recirculation pump flow control valve runback.  During the flow control valve runback, the 'A' recirculation hydraulic power unit tripped causing an incomplete runback.
Reactor water level 3 (11.4 inches) was reached which is an RPS scram setpoint and also a setpoint for Group 2 (RHR to Radwaste) and Group 3 (Shutdown Cooling Isolation).  No valves isolated in these systems due to [the valves] being in their normally closed position. The lowest reactor water level reached was -28 inches wide range.
Reactor water level 3 (11.4 inches) was reached which is an RPS scram setpoint and also a setpoint for Group 2 (RHR to Radwaste) and Group 3 (Shutdown Cooling Isolation).  No valves isolated in these systems due to [the valves] being in their normally closed position. The lowest reactor water level reached was -28 inches wide range.

Latest revision as of 21:10, 1 March 2018

ENS 45753 +/-
Where
Grand Gulf Entergy icon.png
Mississippi (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-2.8 h-0.117 days <br />-0.0167 weeks <br />-0.00384 months <br />)
Opened: Terry Holcombe
19:47 Mar 8, 2010
NRC Officer: Howie Crouch
Last Updated: Mar 8, 2010
45753 - NRC Website
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