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OPERATING DATA REPORT | OPERATING DATA REPORT Docket No. 50-317 Date: | ||
Docket No. 50-317 Date: August 13, 1986 Completed by R. Porter | August 13, 1986 Completed by R. | ||
: 1. Unit Name: | Porter Telephone: (301) 260-4868 l | ||
: 2. Reporting Period: | OPERATING STATUS | ||
: 3. Licensed Thermal Power (MWT): | : 1. Unit Name: | ||
: 4. Nameplate Rating (Gross MWe): | Chlvert Cliffs No. 1 | ||
: 5. Design Electrical Rating (Net MWe): | : 2. Reporting Period: | ||
: 6. Maximum Dependable Capacity (Gross Mwe): | JULY | ||
: 7. Maximum Dependable Capacity (Net MWe): | : 3. Licensed Thermal Power (MWT): | ||
: 8. Change in Capacity Ratings: | 2,700 | ||
: 9. Power Level to Which Restricted (Net MWe): | : 4. Nameplate Rating (Gross MWe): | ||
: 10. Reasons for Restrictions: | 918 | ||
: 11. Hours in Reporting Period | : 5. Design Electrical Rating (Net MWe): | ||
: 12. Number of Hours Reactor was Critical | 845 | ||
: 13. Reactor Reserve Shutdown Hours | : 6. Maximum Dependable Capacity (Gross Mwe): | ||
: 14. Hours Generator On-Line | 860 | ||
: 15. Unit Reserve Shutdown Hours | : 7. Maximum Dependable Capacity (Net MWe): | ||
: 16. Gross Thermal Energy Generated (MWH) | 825 | ||
: 17. Gross Electrical Energy Generated (MWH) | : 8. Change in Capacity Ratings: | ||
: 18. Net Electrical Energy Generated (MWH) | None | ||
: 21. Unit Capacity Factor (Using MDC Net) | : 9. Power Level to Which Restricted (Net MWe): | ||
: 22. Unit Capacity Factor (Using DER Net) | N/A | ||
: 23. Unit Forced Outage Rate | : 10. Reasons for Restrictions: | ||
N/A This Month Yr-to-Date Cumulative | |||
: 11. Hours in Reporting Period 744^ | |||
5,087 98,460 | |||
: 12. Number of Hours Reactor was Critical 706.4 4,882.8 77,748.3 | |||
: 13. Reactor Reserve Shutdown Hours 0.0 0.0 3,019.4 | |||
: 14. Hours Generator On-Line 704.1 4,849.4 76,208.9 | |||
: 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 | |||
: 16. Gross Thermal Energy Generated (MWH) 1,850,976 12,869,980 190,194,173 l | |||
: 17. Gross Electrical Energy Generated (MWH) 607,564 4,324,446 62,927,258 | |||
: 18. Net Electrical Energy Generated (MWH) 580,549 4,143,505 60,059,800 l | |||
: 19. Unit Service Factor 94.6 95.3 77.4 l | |||
: 20. Unit Availability Factor 94.6 95.3 77.4 | |||
: 21. Unit Capacity Factor (Using MDC Net) 94.6 98.7 74.3 | |||
: 22. Unit Capacity Factor (Using DER Net) 92.3 96.4 72.2 | |||
: 23. Unit Forced Outage Rate 5.4 4.7 8.8 | |||
: 24. Shutdowns Scheduled Over Next Six Months (type, date and duration): | : 24. Shutdowns Scheduled Over Next Six Months (type, date and duration): | ||
Refueling Outage October 25, 1986 - January 4, 1987 | Refueling Outage October 25, 1986 - January 4, 1987 | ||
: 25. If Shutdown at End of Report Period, Estimated Date of Startup: N/A 8608190641 | : 25. If Shutdown at End of Report Period, Estimated Date of Startup: | ||
ADOCK 05000317 PDR | N/A l | ||
8608190641 860813 | |||
~" | |||
DR ADOCK 05000317 PDR | |||
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i UNIT SIRTITIOWNS AND IMMR REDUCTIONS DOCKIE NO. 50-317 UNIT NA>E Calvert Cliffs 1 DAll? August '13, 1986 C(M'I.lMD llY R. Porter REI' ORT PS)N'lli JULY TEI.E11K)NE (301) 260_-4868 | |||
i UNIT SIRTITIOWNS AND IMMR REDUCTIONS | '7 | ||
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Canse & (. ' | |||
Canse & (.. | e. | ||
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y,c g I.icensee gag | |||
.orrecLive | |||
86-06' | ~ | ||
capacitor for 12B Reactor Coolant | h gg g | ||
i | jgy | ||
: Event, y | |||
J | j-Act,, on t o No. | ||
Dat,e t | |||
H 93 y | |||
jjp Repn L // | |||
C-Refueling | diu o | ||
E-Operator Training & License Examinat, ion F-Administrat,ive g | Prevent, Recierrence d | ||
. u>.s v | |||
8 86-06' 860720 F | |||
39.9 A | |||
3 86-04 CB CKTBKR The unit tripped when a surge. | |||
capacitor for 12B Reactor Coolant i | |||
'e Pump failed. | |||
s J | |||
\\ | |||
N s | |||
I 3 | |||
4 F: Forecci Reason: | |||
on tlaxt: | |||
Exhibi t. G-Inst r,ict. ions S: Schedule <l A-Ecinipment, Failure (Explain) 1-Mannat for Preparat ion 'of Dat,a B-Maintenance or Te.st, 2-Ftinnal Scram. | |||
Ent ry Sheet.s foi Licenv? | |||
C-Refueling 3-Antaxnat,ic Scram. | |||
Event, Report, (LER) Fi.le D-Regulat.ory Rest,rict ion 4-Other (Explain) | |||
(NURFG-0161) | |||
E-Operator Training & License Examinat, ion F-Administrat,ive g | |||
p,,,3,g g _ | |||
g. | |||
G-Operat,ional Error (Explain) | G-Operat,ional Error (Explain) | ||
I!-Ot.her (Explain) | I!-Ot.her (Explain) | ||
F_ | F_ | ||
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-317 Calvert Cliffs Unit No. 1 Date: August 13, 1986 Completed by R. Porter Telephone: (301) 260-4868 JULY | AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-317 Calvert Cliffs Unit No. 1 Date: | ||
{~ | August 13, 1986 Completed by R. | ||
Average Daily Power Level | Porter Telephone: (301) 260-4868 JULY | ||
{~ | |||
[ | Average Daily Power Level Average Daily Power Level Day (MWe-Net) pay (MWe-Net) 1 849 17 849 2 | ||
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. | 851 18 850 3 | ||
849 19 839 r | |||
4 853 20 170 5 | |||
854 21 0 | |||
6 853 22 592 7 | |||
853 23 841 8 | |||
850 24 830 9 | |||
347 25 828 10 839 26 773 11 846 27 817 12 846 28 817 E-13 846 29 821 14 844 30 836 m | |||
15 841 31 835 16 797 | |||
[ | |||
INSTRUCTIONS: | |||
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. | |||
Compute to the nearest whole megawatt. | |||
t m | t m | ||
i | i OPERATING DATA REPORT l | ||
OPERATING DATA REPORT l | l l | ||
l l | Docket No. 50-318 Date: | ||
August 13, 1986 l | |||
Completed by R. Porter Telephone: (301) 260-4868 5 | |||
OPERATING STATUS | OPERATING STATUS | ||
: 1. Unit Name: | : 1. Unit Name: | ||
: 2. Reporting Period: | Calvert Cliffs No. 2 | ||
: 2. Reporting Period: | |||
: 4. Nameplate Rating (Gross MWe): | JULY | ||
: 5. | '3. Licensed Thermal Power (MWT): | ||
: 6. Maximum Dependable Capacity (Gross Mwe): | 2,700 | ||
: 7. Maximum Dependable Capacity (Net MWe): | : 4. Nameplate Rating (Gross MWe): | ||
: 8. | 918 | ||
9. | : 5. Design Electrical Rating (Net MWe): | ||
Power Level to Which Restricted (Net MWe): | 845 | ||
: 10. Reasons for Restrictions: | : 6. Maximum Dependable Capacity (Gross Mwe): | ||
: 11. Hours in Reporting Period | 860 | ||
: 12. Number of Hours Reactor was Critical | : 7. Maximum Dependable Capacity (Net MWe): | ||
: 13. Reactor Reserve Shutdown Hours | 825 | ||
: 14. Hours Generator On-Line | : 8. Change in Capacity Ratings: | ||
: 15. Unit Reserve Shutdown Hours | None | ||
: 16. Gross Thermal Energy Generated (MWH) | : 9. Power Level to Which Restricted (Net MWe): | ||
: 17. Gross Electrical Energy Generated (MWH) | N/A | ||
: 18. Net Electrical Energy Generated (MWH) | : 10. Reasons for Restrictions: | ||
: 19. Unit Service Factor | N/A This Month Yr-to-Date Cumulative | ||
: 20. Unit Availability Factor | : 11. Hours in Reporting Period 744 5,087 01,815 | ||
: 21. Unit Capacity Factor (Using MDC Net)., | : 12. Number of Hours Reactor was Critical 592.3 4,853.2 68,296.2 | ||
: 22. Unit Capacity Factor (Using DER Net) | : 13. Reactor Reserve Shutdown Hours 0.0 24.3 1,285.0 | ||
: 23. Unit Forced Outage Rate | : 14. Hours Generator On-Line 591.6 4,841.7 67,253.0 | ||
: 24. Shutdowns Scheduled Over Next Six Months (type, date and duration): | : 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0 | ||
: 16. Gross Thermal Energy Generated (MWH) 1,557,132 12,449,838 168,931,874 | |||
: 17. Gross Electrical Energy Generated (MWH) 515,538 4,202,500 55,724,024 | |||
: 18. Net Electrical Energy Generated (MWH) 493,574 4,026,032 53,176,289 | |||
: 19. Unit Service Factor 79.5 95.2 82.2 | |||
: 20. Unit Availability Factor 79.5 95.2 82.2 | |||
: 21. Unit Capacity Factor (Using MDC Net)., | |||
80.4 95.9 78.9 | |||
: 22. Unit Capacity Factor (Using DER Net) 78.5 93.7 76.9 | |||
: 23. Unit Forced Outage Rate 20.5 4.3 6.0 | |||
: 24. Shutdowns Scheduled Over Next Six Months (type, date and duration): | |||
None | |||
: 25. If Shutdown at End of Report Period, Estimated Date of Startup: | : 25. If Shutdown at End of Report Period, Estimated Date of Startup: | ||
August 2, 1986 | i August 2, 1986 | ||
UNIT SiltrI1MMNS AND IT)Wl'.R REINK'I' IONS | UNIT SiltrI1MMNS AND IT)Wl'.R REINK'I' IONS IX)CKIN NO. | ||
UNIT NAPE Calvert Cliffs 2 DNrF, August 13, 1986 C(NPI,FTED BY | 50-318 i | ||
c- | UNIT NAPE Calvert Cliffs 2 DNrF, August 13, 1986 C(NPI,FTED BY R. J. Porter REI41RT MDN*lli JULY TEI.Elill)NE (301) 260-4868 2 | ||
ouS E | |||
c-ei | |||
,o j g | |||
y,3 g I,icensee Q | |||
gig t.ause & (.orrec t. s. ve | |||
86-08 | ~ | ||
86-09 | h yg g | ||
I | jgg Event y | ||
J Action t.o No. | |||
Date yJ Reixn t, f/ | |||
Nu o | |||
Prevent, Reciarrence b,= | |||
g s | |||
H nut 5 o | |||
8 86-08 860707 F | |||
0 11 N/A N/A N/A N/A Power was reduced when the load dispacther requested a reduction due to a problem on the Grid. | |||
86-09 860725 F | |||
152.4 A | |||
1 86-05 CB INSTRU The unit was shutdown to repair a failed flexible hose on a seal pressure transmitter for 21B Reactor Coolant Pump. | |||
I 2 | |||
3 4 | |||
p, | |||
,, i - d Reason-M Llu.xi-F.xhibit, G-Inst:1 ct, ions S: Schedtiled A-Equipment, Failure (Explain) 1-Manna] | |||
foi Preparation of Dat a B-Maint.enance or Test. | |||
2-Runial Scram. | |||
Ent.ry Sheets for License C-Refneling 3-Aiitomat ic Scram. | |||
Event Report (I ER) File D-Regislat.ory Restrict, ion 4-Other (Explain) | |||
(N1TREG-0161) | |||
E-Ogxtrator Training & I,icense Examinat, ion F-Administrative 5 Exhibit, t - Same Source G-Operat,jonal Error (Explain) | E-Ogxtrator Training & I,icense Examinat, ion F-Administrative 5 Exhibit, t - Same Source G-Operat,jonal Error (Explain) | ||
Il-Other (Explain) | Il-Other (Explain) | ||
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-318 Calvert Cliffs Unit No. 2 Date: August 13, 1986 Completed by R. Porter Telephone: (301) 260-4868 JULY Average Daily Power Level | AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-318 Calvert Cliffs Unit No. 2 Date: | ||
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt. | August 13, 1986 Completed by R. | ||
Porter Telephone: (301) 260-4868 JULY Average Daily Power Level Average Daily Power Level Day (MWe-Net) | |||
Day (MWe-Net) 1 841 17 838 2 | |||
843 18 838 3 | |||
841 19 837 4 | |||
847 20 837 5 | |||
847 21 833 6 | |||
845 22 838 7 | |||
796 23 837 8 | |||
788 24 837 9 | |||
841 25 412 l | |||
10 841 26 0 | |||
11 840 27 0 | |||
12 839 28 0 | |||
13 838 29 0 | |||
14 837 30 0 | |||
15 836 31 0 | |||
16 839 INSTRUCTIONS: | |||
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. | |||
Compute to the nearest whole megawatt. | |||
==SUMMARY== | ==SUMMARY== | ||
OF UNIT 1 OPERATING EXPERIENCE July 1986 | OF UNIT 1 OPERATING EXPERIENCE July 1986 7/1 Unit 1 began this reporting period at full reactor power (825 MWe). | ||
7/1 | 7/10 At 2055, Unit 1 reduced power to 720 MWe when No. 12 Circulating Water Pump was secured. | ||
7/10 At 2055, Unit 1 reduced power to 720 MWe when No. 12 Circulating Water Pump was secured. The pump had to be secured when shear pins on No. 12 A&B Traveling Screens failed, causing high differential pressure. | The pump had to be secured when shear pins on No. 12 A&B Traveling Screens failed, causing high differential pressure. | ||
7/15 At 2300, Unit.1 began reducing power to 700 MWe for Condenser Water Box cleaning . | 7/15 At 2300, Unit.1 began reducing power to 700 MWe for Condenser Water Box cleaning. | ||
7/16 At 1028, Unit 1 returned to full power (825 MWe). | 7/16 At 1028, Unit 1 returned to full power (825 MWe). | ||
7/20 At 0500, Unit 1 tripped because a failed surge capacitor caused No. 12B Reactor Coolant Pump (RCP) to trip. | 7/20 At 0500, Unit 1 tripped because a failed surge capacitor caused No. 12B Reactor Coolant Pump (RCP) to trip. | ||
| Line 137: | Line 239: | ||
chemistry hold. | chemistry hold. | ||
7/22 At 0430, the chemistry hold was removed and the Unit was at full reactor power (825 MWe) by 1300. | 7/22 At 0430, the chemistry hold was removed and the Unit was at full reactor power (825 MWe) by 1300. | ||
7/26 At 0230, power was reduced to 700 MWe for Condenser Water Box cleaning. At 1230, power was increased to 815 MWe so Moderator Temperature Coefficient (MTC) testing could be performed. | 7/26 At 0230, power was reduced to 700 MWe for Condenser Water Box cleaning. | ||
At 1230, power was increased to 815 MWe so Moderator Temperature Coefficient (MTC) testing could be performed. | |||
7/29 At 2125, MTC testing was completed and the Unit was returned to full power (825 MWe). | 7/29 At 2125, MTC testing was completed and the Unit was returned to full power (825 MWe). | ||
7/31 The Unit was at full reactor power (825 MWe) at the end of this reporting period. | 7/31 The Unit was at full reactor power (825 MWe) at the end of this reporting period. | ||
| Line 144: | Line 247: | ||
==SUMMARY== | ==SUMMARY== | ||
OF UNIT 2 OPERATING EXPERIENCE July 1986 7/1 Unit 2 began this reporting period at full reactor power (825 MWe). | OF UNIT 2 OPERATING EXPERIENCE July 1986 7/1 Unit 2 began this reporting period at full reactor power (825 MWe). | ||
7/7 | 7/7 At 1940, Unit 2 reduced power to 495 MWe because of a tripped transformer at Waugh Chapel. | ||
7/8 | 7/8 At 0150, the transformer was back in service and Unit 2 began increasing power. | ||
At 0530, Unit 2 was at full reactor power (825 MWe). | |||
7/25 At 1345, commenced shutdown of Unit 2 due to unidentified Reactor Coolant System (RCS) leakage greater than 1 GPM. | 7/25 At 1345, commenced shutdown of Unit 2 due to unidentified Reactor Coolant System (RCS) leakage greater than 1 GPM. | ||
7/25 At 1536, the breaker was opened. At 1617, the reactor was shut down. The leakage was found to be due to a failed flexible hose on a seal pressure transmitter. The Unit remained in a shutdown condition to investigate high vibration on #21B RCP. | 7/25 At 1536, the breaker was opened. | ||
At 1617, the reactor was shut down. | |||
The leakage was found to be due to a failed flexible hose on a seal pressure transmitter. | |||
The Unit remained in a shutdown condition to investigate high vibration on #21B RCP. | |||
7/31 Unit 2 was shutdown at the end of this reporting period. | 7/31 Unit 2 was shutdown at the end of this reporting period. | ||
l 4 | l 4 | ||
I | I | ||
e August 6,1986 REFUELING INFORMATION REQUEST | e August 6,1986 REFUELING INFORMATION REQUEST 1. | ||
Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No.1 2. | |||
Scheduled date for next Refueling Shutdown: October 25,1986 3. | |||
Scheduled date for restart following refueling: January 4,1987 4. | |||
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment? | |||
Resumption of operation after refueling will require changes to Technical | Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core. | ||
Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core. | 5. | ||
Scheduled date(s) for submitting proposed licensing action and supporting information. | |||
September 29,1986 | September 29,1986 6. | ||
Important licensing considerations associated with the refueling. | |||
Reload fuel will be similar to that reload fuel inserted into the previous cycle. | Reload fuel will be similar to that reload fuel inserted into the previous cycle. | ||
7. | |||
(a) 217 | The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool. | ||
(a) 217 (b) 1000 Spent Fuel Pools are common to Units 1 and 2 8. | |||
(a) 1830 (b)0 | (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies. | ||
(a) 1830 (b)0 9. | |||
The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load. | |||
April,1991 s | April,1991 s | ||
August 6,1986 REFUELING INFORMATION REQUEST | August 6,1986 REFUELING INFORMATION REQUEST | ||
: 1. Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No. 2. | : 1. Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No. 2. | ||
.2. Scheduled date for next refueling shutdown: March 14,1987. | |||
: 3. Scheduled date for restart following refueling: May 22,1987. | : 3. Scheduled date for restart following refueling: May 22,1987. | ||
: 4. Will refueling or resumption of operation thereafter require a technical specification change or other licensed amendment? | : 4. Will refueling or resumption of operation thereafter require a technical specification change or other licensed amendment? | ||
| Line 181: | Line 289: | ||
Reload fuel will be similar to that reload fuel inserted in the previous cycle. | Reload fuel will be similar to that reload fuel inserted in the previous cycle. | ||
: 7. The number of fuel assemblies (a) in the core and (b) in the Spent Fuel Storage Pool. | : 7. The number of fuel assemblies (a) in the core and (b) in the Spent Fuel Storage Pool. | ||
(a) 217 | (a) 217 (b) 1000 Spent Fuel Pool is common to Units 1 and 2. | ||
: 8. (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been req'uired or is planned, in number of fuel assemblies. | : 8. (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been req'uired or is planned, in number of fuel assemblies. | ||
(a) 1830 (b)0 | (a) 1830 (b)0 | ||
: 9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load. | : 9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load. | ||
April,1991 | April,1991 | ||
.}} | |||
Latest revision as of 16:07, 7 December 2024
| ML20205G858 | |
| Person / Time | |
|---|---|
| Site: | Calvert Cliffs |
| Issue date: | 07/31/1986 |
| From: | Porter R BALTIMORE GAS & ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML20205G840 | List: |
| References | |
| NUDOCS 8608190641 | |
| Download: ML20205G858 (10) | |
Text
OPERATING DATA REPORT Docket No. 50-317 Date:
August 13, 1986 Completed by R.
Porter Telephone: (301) 260-4868 l
OPERATING STATUS
- 1. Unit Name:
Chlvert Cliffs No. 1
- 2. Reporting Period:
JULY
- 3. Licensed Thermal Power (MWT):
2,700
- 4. Nameplate Rating (Gross MWe):
918
- 5. Design Electrical Rating (Net MWe):
845
- 6. Maximum Dependable Capacity (Gross Mwe):
860
- 7. Maximum Dependable Capacity (Net MWe):
825
- 8. Change in Capacity Ratings:
None
- 9. Power Level to Which Restricted (Net MWe):
N/A
- 10. Reasons for Restrictions:
N/A This Month Yr-to-Date Cumulative
- 11. Hours in Reporting Period 744^
5,087 98,460
- 12. Number of Hours Reactor was Critical 706.4 4,882.8 77,748.3
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 3,019.4
- 14. Hours Generator On-Line 704.1 4,849.4 76,208.9
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1,850,976 12,869,980 190,194,173 l
- 17. Gross Electrical Energy Generated (MWH) 607,564 4,324,446 62,927,258
- 18. Net Electrical Energy Generated (MWH) 580,549 4,143,505 60,059,800 l
- 19. Unit Service Factor 94.6 95.3 77.4 l
- 20. Unit Availability Factor 94.6 95.3 77.4
- 21. Unit Capacity Factor (Using MDC Net) 94.6 98.7 74.3
- 22. Unit Capacity Factor (Using DER Net) 92.3 96.4 72.2
- 23. Unit Forced Outage Rate 5.4 4.7 8.8
- 24. Shutdowns Scheduled Over Next Six Months (type, date and duration):
Refueling Outage October 25, 1986 - January 4, 1987
- 25. If Shutdown at End of Report Period, Estimated Date of Startup:
N/A l
8608190641 860813
~"
DR ADOCK 05000317 PDR
..g m
i UNIT SIRTITIOWNS AND IMMR REDUCTIONS DOCKIE NO. 50-317 UNIT NA>E Calvert Cliffs 1 DAll? August '13, 1986 C(M'I.lMD llY R. Porter REI' ORT PS)N'lli JULY TEI.E11K)NE (301) 260_-4868
'7
- c-t uS E
Canse & (. '
e.
,o g g
y,c g I.icensee gag
.orrecLive
~
h gg g
jgy
- Event, y
j-Act,, on t o No.
Dat,e t
H 93 y
jjp Repn L //
diu o
Prevent, Recierrence d
. u>.s v
8 86-06' 860720 F
39.9 A
3 86-04 CB CKTBKR The unit tripped when a surge.
capacitor for 12B Reactor Coolant i
'e Pump failed.
s J
\\
N s
I 3
4 F: Forecci Reason:
on tlaxt:
Exhibi t. G-Inst r,ict. ions S: Schedule <l A-Ecinipment, Failure (Explain) 1-Mannat for Preparat ion 'of Dat,a B-Maintenance or Te.st, 2-Ftinnal Scram.
Ent ry Sheet.s foi Licenv?
C-Refueling 3-Antaxnat,ic Scram.
Event, Report, (LER) Fi.le D-Regulat.ory Rest,rict ion 4-Other (Explain)
(NURFG-0161)
E-Operator Training & License Examinat, ion F-Administrat,ive g
p,,,3,g g _
g.
G-Operat,ional Error (Explain)
I!-Ot.her (Explain)
F_
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-317 Calvert Cliffs Unit No. 1 Date:
August 13, 1986 Completed by R.
Porter Telephone: (301) 260-4868 JULY
{~
Average Daily Power Level Average Daily Power Level Day (MWe-Net) pay (MWe-Net) 1 849 17 849 2
851 18 850 3
849 19 839 r
4 853 20 170 5
854 21 0
6 853 22 592 7
853 23 841 8
850 24 830 9
347 25 828 10 839 26 773 11 846 27 817 12 846 28 817 E-13 846 29 821 14 844 30 836 m
15 841 31 835 16 797
[
INSTRUCTIONS:
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.
Compute to the nearest whole megawatt.
t m
i OPERATING DATA REPORT l
l l
Docket No. 50-318 Date:
August 13, 1986 l
Completed by R. Porter Telephone: (301) 260-4868 5
OPERATING STATUS
- 1. Unit Name:
Calvert Cliffs No. 2
- 2. Reporting Period:
JULY
'3. Licensed Thermal Power (MWT):
2,700
- 4. Nameplate Rating (Gross MWe):
918
- 5. Design Electrical Rating (Net MWe):
845
- 6. Maximum Dependable Capacity (Gross Mwe):
860
- 7. Maximum Dependable Capacity (Net MWe):
825
- 8. Change in Capacity Ratings:
None
- 9. Power Level to Which Restricted (Net MWe):
N/A
- 10. Reasons for Restrictions:
N/A This Month Yr-to-Date Cumulative
- 11. Hours in Reporting Period 744 5,087 01,815
- 12. Number of Hours Reactor was Critical 592.3 4,853.2 68,296.2
- 13. Reactor Reserve Shutdown Hours 0.0 24.3 1,285.0
- 14. Hours Generator On-Line 591.6 4,841.7 67,253.0
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (MWH) 1,557,132 12,449,838 168,931,874
- 17. Gross Electrical Energy Generated (MWH) 515,538 4,202,500 55,724,024
- 18. Net Electrical Energy Generated (MWH) 493,574 4,026,032 53,176,289
- 19. Unit Service Factor 79.5 95.2 82.2
- 20. Unit Availability Factor 79.5 95.2 82.2
- 21. Unit Capacity Factor (Using MDC Net).,
80.4 95.9 78.9
- 22. Unit Capacity Factor (Using DER Net) 78.5 93.7 76.9
- 23. Unit Forced Outage Rate 20.5 4.3 6.0
- 24. Shutdowns Scheduled Over Next Six Months (type, date and duration):
None
- 25. If Shutdown at End of Report Period, Estimated Date of Startup:
i August 2, 1986
UNIT SiltrI1MMNS AND IT)Wl'.R REINK'I' IONS IX)CKIN NO.
50-318 i
UNIT NAPE Calvert Cliffs 2 DNrF, August 13, 1986 C(NPI,FTED BY R. J. Porter REI41RT MDN*lli JULY TEI.Elill)NE (301) 260-4868 2
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y,3 g I,icensee Q
gig t.ause & (.orrec t. s. ve
~
h yg g
jgg Event y
J Action t.o No.
Date yJ Reixn t, f/
Nu o
Prevent, Reciarrence b,=
g s
H nut 5 o
8 86-08 860707 F
0 11 N/A N/A N/A N/A Power was reduced when the load dispacther requested a reduction due to a problem on the Grid.
86-09 860725 F
152.4 A
1 86-05 CB INSTRU The unit was shutdown to repair a failed flexible hose on a seal pressure transmitter for 21B Reactor Coolant Pump.
I 2
3 4
p,
,, i - d Reason-M Llu.xi-F.xhibit, G-Inst:1 ct, ions S: Schedtiled A-Equipment, Failure (Explain) 1-Manna]
foi Preparation of Dat a B-Maint.enance or Test.
2-Runial Scram.
Ent.ry Sheets for License C-Refneling 3-Aiitomat ic Scram.
Event Report (I ER) File D-Regislat.ory Restrict, ion 4-Other (Explain)
E-Ogxtrator Training & I,icense Examinat, ion F-Administrative 5 Exhibit, t - Same Source G-Operat,jonal Error (Explain)
Il-Other (Explain)
AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-318 Calvert Cliffs Unit No. 2 Date:
August 13, 1986 Completed by R.
Porter Telephone: (301) 260-4868 JULY Average Daily Power Level Average Daily Power Level Day (MWe-Net)
Day (MWe-Net) 1 841 17 838 2
843 18 838 3
841 19 837 4
847 20 837 5
847 21 833 6
845 22 838 7
796 23 837 8
788 24 837 9
841 25 412 l
10 841 26 0
11 840 27 0
12 839 28 0
13 838 29 0
14 837 30 0
15 836 31 0
16 839 INSTRUCTIONS:
On this format, list the average daily unit power level in MWe-Net for each day in the reporting month.
Compute to the nearest whole megawatt.
SUMMARY
OF UNIT 1 OPERATING EXPERIENCE July 1986 7/1 Unit 1 began this reporting period at full reactor power (825 MWe).
7/10 At 2055, Unit 1 reduced power to 720 MWe when No. 12 Circulating Water Pump was secured.
The pump had to be secured when shear pins on No. 12 A&B Traveling Screens failed, causing high differential pressure.
7/15 At 2300, Unit.1 began reducing power to 700 MWe for Condenser Water Box cleaning.
7/16 At 1028, Unit 1 returned to full power (825 MWe).
7/20 At 0500, Unit 1 tripped because a failed surge capacitor caused No. 12B Reactor Coolant Pump (RCP) to trip.
7/21 At 1835, the Unit became critical, and the breaker was shut at 2054.
7/21 At 2230, the Unit stopped increasing power due to a 30%
chemistry hold.
7/22 At 0430, the chemistry hold was removed and the Unit was at full reactor power (825 MWe) by 1300.
7/26 At 0230, power was reduced to 700 MWe for Condenser Water Box cleaning.
At 1230, power was increased to 815 MWe so Moderator Temperature Coefficient (MTC) testing could be performed.
7/29 At 2125, MTC testing was completed and the Unit was returned to full power (825 MWe).
7/31 The Unit was at full reactor power (825 MWe) at the end of this reporting period.
I
SUMMARY
OF UNIT 2 OPERATING EXPERIENCE July 1986 7/1 Unit 2 began this reporting period at full reactor power (825 MWe).
7/7 At 1940, Unit 2 reduced power to 495 MWe because of a tripped transformer at Waugh Chapel.
7/8 At 0150, the transformer was back in service and Unit 2 began increasing power.
At 0530, Unit 2 was at full reactor power (825 MWe).
7/25 At 1345, commenced shutdown of Unit 2 due to unidentified Reactor Coolant System (RCS) leakage greater than 1 GPM.
7/25 At 1536, the breaker was opened.
At 1617, the reactor was shut down.
The leakage was found to be due to a failed flexible hose on a seal pressure transmitter.
The Unit remained in a shutdown condition to investigate high vibration on #21B RCP.
7/31 Unit 2 was shutdown at the end of this reporting period.
l 4
I
e August 6,1986 REFUELING INFORMATION REQUEST 1.
Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No.1 2.
Scheduled date for next Refueling Shutdown: October 25,1986 3.
Scheduled date for restart following refueling: January 4,1987 4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment?
Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core.
5.
Scheduled date(s) for submitting proposed licensing action and supporting information.
September 29,1986 6.
Important licensing considerations associated with the refueling.
Reload fuel will be similar to that reload fuel inserted into the previous cycle.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.
(a) 217 (b) 1000 Spent Fuel Pools are common to Units 1 and 2 8.
(a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
(a) 1830 (b)0 9.
The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load.
April,1991 s
August 6,1986 REFUELING INFORMATION REQUEST
- 1. Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No. 2.
.2. Scheduled date for next refueling shutdown: March 14,1987.
- 3. Scheduled date for restart following refueling: May 22,1987.
- 4. Will refueling or resumption of operation thereafter require a technical specification change or other licensed amendment?
Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core.
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information.
February 13,1987
- 6. Important licensing considerations associated with refueling.
Reload fuel will be similar to that reload fuel inserted in the previous cycle.
- 7. The number of fuel assemblies (a) in the core and (b) in the Spent Fuel Storage Pool.
(a) 217 (b) 1000 Spent Fuel Pool is common to Units 1 and 2.
- 8. (a) The present licensed spent fuel pool storage capacity, and (b) the size of any increase in licensed storage capacity that has been req'uired or is planned, in number of fuel assemblies.
(a) 1830 (b)0
- 9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load.
April,1991
.