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=Text=
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{{#Wiki_filter:,   PRI(DURITY (ACCELERATED RIDS PROCESSING 1
{{#Wiki_filter:, PRI(DURITY 1
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
(ACCELERATED RIDS PROCESSING REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9411210284                 DOC.DATE:     94/11/11     NOTARIZED: YES       DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana                         M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana                         M 05000316 AUTH. NAME               AUTHOR AFFILIATION FITZPATRICK,E.         Indiana Michigan Power Co. (formerly Indiana 6 Michigan Ele RECIP.NAME               RECIPIENT AFFILIATION MARTIN,J.B.                 Document Control Branch (Document Control Desk)
ACCESSION NBR:9411210284 DOC.DATE: 94/11/11 NOTARIZED: YES FACIL:50-315 Donald C.
Cook Nuclear Power Plant, Unit 1, Indiana M
50-316 Donald C.
Cook Nuclear Power Plant, Unit 2, Indiana M
AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.
Indiana Michigan Power Co. (formerly Indiana 6 Mich RECIP.NAME RECIPIENT AFFILIATION MARTIN,J.B.
Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Forwards revised commitments re lube oil analysis program &
Forwards revised commitments re lube oil analysis program info requested by staff re actions to be taken in event oil samples indicate potential pump degradation.
info requested by staff re actions to be taken in event oil samples indicate potential pump degradation.
DISTRIBUTION CODE:
DISTRIBUTION CODE: AOOID               COPIES RECEIVED:LTR           I ENCL   I SIZE:
AOOID COPIES RECEIVED:LTR I ENCL I
TITLE: OR Submittal: General Distribution NOTES:
SIZE:
RECIPIENT                 COPIES                RECIPIENT          COPIES ID  CODE/NAME                LTTR ENCL          ID CODE/NAME       LTTR ENCL PD3-1 LA                         1      1      PD3-1 PD                1    1 HICKMAN,J                         1      1 INTERNA     FILE CENTER       01           1      1      NRR/DE/EELB RR/DRCH/HICB                     1      1      NRR/DRPW NRR/DSSA/SPLB                     1     1       NRR/DSSA/SRXB NUDOCS-ABSTRACT                    1      1      OGC/HDS2 EXTERNAL: NOAC                                1     1       NRC PDR NOTE TO ALL "RlDS" RE CI PI ENTS:
TITLE: OR Submittal:
PLEASE HELP US TO REDUCE KVASTE! CONTACT THE DOC! 'MENT CONTROL DESK, ROOÃI P! -37 (EXT. 504-2083 ) TO ELI XIIVATE YOUR NAXIE PRO~I DISTRIBUTION LISTS I:OR DOC!.'MENTS YOU DON"I'EED!
General Distribution NOTES:
TOTAL NUMBER OF COPIES REQUIRED: LTTR                       13   ENCL       12
DOCKET 05000315 05000316 igan Ele RECIPIENT ID CODE/NAME PD3-1 LA HICKMAN,J INTERNA FILE CENTER 01 RR/DRCH/HICB NRR/DSSA/SPLB NUDOCS-ABSTRACT EXTERNAL: NOAC COPIES LTTR ENCL 1
1 1
1 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD3-1 PD NRR/DE/EELB NRR/DRPW NRR/DSSA/SRXB OGC/HDS2 NRC PDR COPIES LTTR ENCL 1
1 NOTE TO ALL"RlDS" RE CI PI ENTS:
PLEASE HELP US TO REDUCE KVASTE!CONTACTTHE DOC! 'MENTCONTROL DESK, ROOÃI P! -37 (EXT. 504-2083 ) TO ELIXIIVATE YOUR NAXIE PRO~I DISTRIBUTIONLISTS I:OR DOC!.'MENTS YOU DON"I'EED!
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 13 ENCL 12


indiana Michigan I
indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 I
Power Company P.O. Box 16631 Columbus, OH 43216 AEP:NRC:1184Fl Donald C. Cook Nuclear Plant Units       1 and 2 Docket Nos. 50-315 and 50-316 License Nos. DPR-58 and DPR-74 NRC INSPECTION REPORTS NOS. 50-315/93016 (DRP)
AEP:NRC:1184Fl Donald C.
AND 50-316/93016 (DRP):       REVISED COMMITMENTS REGARDING LUBE     OIL ANALYSIS PROGRAM U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555 Attn: J.       B. Martin November     ll, 1994
Cook Nuclear Plant Units 1 and 2
Docket Nos.
50-315 and 50-316 License Nos.
DPR-58 and DPR-74 NRC INSPECTION REPORTS NOS. 50-315/93016 (DRP)
AND 50-316/93016 (DRP):
REVISED COMMITMENTS REGARDING LUBE OIL ANALYSIS PROGRAM U.
S. Nuclear Regulatory Commission Document Control Desk Washington, D.
C.
20555 Attn:
J.
B. Martin November ll, 1994


==Dear Mr.     Martin:==
==Dear Mr. Martin:==
 
Our letter AEP:NRC:1184F, dated September 16, 1993, responded to a violation involving degradation of an auxiliary feedwater pump bearing.
Our letter AEP:NRC:1184F, dated September 16, 1993, responded to a violation involving degradation of an auxiliary feedwater pump bearing. The letter contained a commitment to establish a plant wide     oil sampling ynd analysis program. Pursuant to discussions with your staff on September 19, 1994, at your offices in Lisle, IL, the attachment to this letter contains revised commitments regarding this program, and also contains>information requested by your       staff regarding actions to be taken in the event oil samples indicate potential pump degradation.
The letter contained a commitment to establish a plant wide oil sampling ynd analysis program.
This   letter is   submitted pursuant to   10 CFR 50.54(f), and, as such, an oath statement     is attached.
Pursuant to discussions with your staff on September 19, 1994, at your offices in Lisle, IL, the attachment to this letter contains revised commitments regarding this program, and also contains>information requested by your staff regarding actions to be taken in the event oil samples indicate potential pump degradation.
This letter is submitted pursuant to 10 CFR 50.54(f),
: and, as
: such, an oath statement is attached.
Sincerely, EF Vice President ar Attachment 7700p~
Sincerely, EF Vice President ar Attachment 7700p~
9411210284 941111                                                                 pyO/
9411210284 941111 PDR ADOCK 05000315 P
ADOCK 05000315 PDR P                       PDR     ij )                                               t I(
PDR ij )
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Mr. J. B. Martin                       AEP'NRC 1184F1 CC:   A. A. Blind G. Charnoff NFEM Section Chief NRC Resident Inspector, Bridgman J. R. Padgett W. T. Russell, NRC - Washington, D.C.
Mr. J.
B. Martin AEP'NRC 1184F1 CC:
A. A. Blind G. Charnoff NFEM Section Chief NRC Resident Inspector, Bridgman J.
R. Padgett W. T. Russell, NRC - Washington, D.C.


STATE OF OHIO)
STATE OF OHIO)
COUNTY OF FRANKLIN)
COUNTY OF FRANKLIN)
E. E. Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing Revised Commitments Regarding Lube Oil Analysis Program, and knows the contents thereof; and that said contents are true to the best             of his knowledge and belief.
E. E. Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing Revised Commitments Regarding Lube Oil Analysis Program, and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.
Subscribed and sworn to before   me this ~i~
Subscribed and sworn to before me this ~i~
day of                                 19
day of 19
                                            ~9'OTAR PUBLIC RITE D. HILL NOTARY PUDLIC. STATE OF OHIO
~9'OTAR PUBLIC RITE D. HILL NOTARY PUDLIC. STATE OF OHIO


ATTAQBKNT TO AEP:NRC: 1184F1 REVISED COMMITMENTS REGARDING LUBE OIL SAMPLING AND ANALYSIS PROGRAM AND ACTIONS TO BE TAKEN IF OIL ANALYSIS INDICATES POSSIBLE DEGRADATION
ATTAQBKNT TO AEP:NRC: 1184F1 REVISED COMMITMENTS REGARDING LUBE OIL SAMPLING AND ANALYSIS PROGRAM AND ACTIONS TO BE TAKEN IF OIL ANALYSIS INDICATES POSSIBLE DEGRADATION


    ~
. ~
l
l


ATTACHMENT TO AEP: NRC: 1184F1                               Page 1 BACKGROUND Our letter AEP:NRC:1184, dated September 16, 1993, responded to a violation concerning failure of an auxiliary feedwater pump bearing. At the time, the principal contributor to the degradation of the bearing was thought to be the presence of water in the bearing oil reservoir. As part of that violation response, we committed to establishing a plant wide oil sampling and analysis program.
ATTACHMENT TO AEP: NRC: 1184F1 Page 1
Subsequent to   this failure,   a task force was formed to make recommendations     to enhance   the operation and design of the auxiliary feedwater pumps. The task force activities included a thorough review of the bearing failure event. It was concluded from this review that an improperly ad]usted balance drum was the primary cause of the bearing failure. Water contamination of the oil was cited as a contributing factor, as this condition may have reduced the ability of the bearing set to withstand the higher-than-normal thrust loads resulting from the misad]usted balance drum. The task force recommendations included modifying the thrust bearing assembly to reduce its sensitivity to abnormal thrust loads, and improving the stuffing, box design to minimize pump leakage,   These modifications were completed on the Unit 2 pumps during the 1994 Unit 2 refueling outage, and will be completed in Unit 1 during a'future outage.
BACKGROUND Our letter AEP:NRC:1184, dated September 16,
On September   19, 1994, discussions were held with your staff regarding the status of the oil sampling and analysis program.
: 1993, responded to a violation concerning failure of an auxiliary feedwater pump bearing.
As a result of those discussions, we were requested to clarify our docketed commitments regarding the program, including actions we would take in the event that the oil analysis results indicate possible pump degradation. The requested information is provided below.
At the
REVISED OIL SAMPLING AND ANALYSIS PROGRAM COMMITMENTS An oil sampling and analysis program has been established for all six auxiliary feedwater   pumps. These pumps are being sampled on a 12 week frequency, or sooner for emergent reasons.         Since April, 1993, approximately 80 samples have been obtained from these pumps. A plant wide program has also been developed and is in the process of being implemented. This program will augment existing vibration monitoring and IST pump performance programs to provide a more comprehensive view of equipment condition. The following provides additional details regarding our current
: time, the principal contributor to the degradation of the bearing was thought to be the presence of
- water in the bearing oil reservoir.
As part of that violation
: response, we committed to establishing a plant wide oil sampling and analysis program.
Subsequent to this failure, a task force was formed to make recommendations to enhance the operation and design of the auxiliary feedwater pumps.
The task force activities included a thorough review of the bearing failure event.
It was concluded from this review that an improperly ad]usted balance drum was the primary cause of the bearing failure.
Water contamination of the oil was cited as a contributing factor, as this condition may have reduced the ability of the bearing set to withstand the higher-than-normal thrust loads resulting from the misad]usted balance drum.
The task force recommendations included modifying the thrust bearing assembly to reduce its sensitivity to abnormal thrust loads, and improving the stuffing, box design to minimize pump leakage, These modifications were completed on the Unit 2 pumps during the 1994 Unit 2 refueling
: outage, and will be completed in Unit 1 during a'future outage.
On September 19,
: 1994, discussions were held with your staff regarding the status of the oil sampling and analysis program.
As a result of those discussions, we were requested to clarify our docketed commitments regarding the program, including actions we would take in the event that the oil analysis results indicate possible pump degradation.
The requested information is provided below.
REVISED OIL SAMPLING AND ANALYSIS PROGRAM COMMITMENTS An oil sampling and analysis program has been established for all six auxiliary feedwater pumps.
These pumps are being sampled on a
12 week frequency, or sooner for emergent reasons.
Since April, 1993, approximately 80 samples have been obtained from these pumps.
A plant wide program has also been developed and is in the process of being implemented.
This program will augment existing vibration monitoring and IST pump performance programs to provide a more comprehensive view of equipment condition.
The following provides additional details regarding our current
 
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ATTACHMENT TO AEP:NRC:1184F1 Page 2
ATTACHMENT TO AEP:NRC:1184F1                                   Page 2 intentions in this area. The program may change       as information on program effectiveness and value are obtained,     and as improved technologies become available.
intentions in this area.
For equipment already selected for inclusion in the program, recurring task action requests have been written to init5ate the detailed planning for acquisition and processing     of samples.         Planning   will include identification of specific sample locations and determination of conditions required to safely obtain representative samples. This planning evolution will also finalize the initial scope of the program to be committed to production. Determination of program scope will include consideration of equipment safety function, feasibility of obtaining a meaningful sample, and the costs/benefits of sampling. Job orders will be written and made ready for scheduling by December 31, 1994.
The program may change as information on program effectiveness and value are obtained, and as improved technologies become available.
: 2. Job orders   will be scheduled as follows:
For equipment already selected for inclusion in the program, recurring task action requests have been written to init5ate the detailed planning for acquisition and processing of samples.
: a. Samples which   will require the associated generating unit to be shut down will be drawn prior to the end of the next scheduled refueling outage (Unit 1 1995, Unit   2 1996).
Planning will include identification of specific sample locations and determination of conditions required to safely obtain representative samples.
: b. Samples which do not require a refueling outage will be drawn before the end of the second 1995 functional equipment group cycle applicable to that equipment.
This planning evolution will also finalize the initial scope of the program to be committed to production.
: 3. The program was   revised to. delineate responsibilities and procedures for engineering review of results and initiation of follow-up/corrective actions. This revision was in place by October 31, 1994. Our existing corrective action system will be used to guide our actions in the event the oil sample indicates degradation. A condition report will be written upon finding and confirming an unexpected failure.
Determination of program scope willinclude consideration of equipment safety function, feasibility of obtaining a meaningful
Also as agreed     in our September 19,     1994, meeting,   we will periodically update the Senior Resident     on our progress with this plan.
: sample, and the costs/benefits of sampling.
Job orders will be written and made ready for scheduling by December 31, 1994.
2.
Job orders will be scheduled as follows:
a.
Samples which willrequire the associated generating unit to be shut down will be drawn prior to the end of the next scheduled refueling outage (Unit 1 1995, Unit 2 1996).
b.
Samples which do not require a refueling outage will be drawn before the end of the second 1995 functional equipment group cycle applicable to that equipment.
3.
The program was revised to. delineate responsibilities and procedures for engineering review of results and initiation of follow-up/corrective actions.
This revision was in place by October 31, 1994.
Our existing corrective action system will be used to guide our actions in the event the oil sample indicates degradation.
A condition report will be written upon finding and confirming an unexpected failure.
Also as agreed in our September 19,
: 1994, meeting, we will periodically update the Senior Resident on our progress with this plan.


0}}
0}}

Latest revision as of 15:12, 7 January 2025

Forwards Revised Commitments Re Lube Oil Analysis Program & Info Requested by Staff Re Actions to Be Taken in Event Oil Samples Indicate Potential Pump Degradation
ML17332A402
Person / Time
Site: Cook  
Issue date: 11/11/1994
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: Martin J
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1184F1, NUDOCS 9411210284
Download: ML17332A402 (10)


Text

, PRI(DURITY 1

(ACCELERATED RIDS PROCESSING REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9411210284 DOC.DATE: 94/11/11 NOTARIZED: YES FACIL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana M

50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Indiana M

AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.

Indiana Michigan Power Co. (formerly Indiana 6 Mich RECIP.NAME RECIPIENT AFFILIATION MARTIN,J.B.

Document Control Branch (Document Control Desk)

SUBJECT:

Forwards revised commitments re lube oil analysis program info requested by staff re actions to be taken in event oil samples indicate potential pump degradation.

DISTRIBUTION CODE:

AOOID COPIES RECEIVED:LTR I ENCL I

SIZE:

TITLE: OR Submittal:

General Distribution NOTES:

DOCKET 05000315 05000316 igan Ele RECIPIENT ID CODE/NAME PD3-1 LA HICKMAN,J INTERNA FILE CENTER 01 RR/DRCH/HICB NRR/DSSA/SPLB NUDOCS-ABSTRACT EXTERNAL: NOAC COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME PD3-1 PD NRR/DE/EELB NRR/DRPW NRR/DSSA/SRXB OGC/HDS2 NRC PDR COPIES LTTR ENCL 1

1 NOTE TO ALL"RlDS" RE CI PI ENTS:

PLEASE HELP US TO REDUCE KVASTE!CONTACTTHE DOC! 'MENTCONTROL DESK, ROOÃI P! -37 (EXT. 504-2083 ) TO ELIXIIVATE YOUR NAXIE PRO~I DISTRIBUTIONLISTS I:OR DOC!.'MENTS YOU DON"I'EED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 13 ENCL 12

indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 I

AEP:NRC:1184Fl Donald C.

Cook Nuclear Plant Units 1 and 2

Docket Nos.

50-315 and 50-316 License Nos.

DPR-58 and DPR-74 NRC INSPECTION REPORTS NOS. 50-315/93016 (DRP)

AND 50-316/93016 (DRP):

REVISED COMMITMENTS REGARDING LUBE OIL ANALYSIS PROGRAM U.

S. Nuclear Regulatory Commission Document Control Desk Washington, D.

C.

20555 Attn:

J.

B. Martin November ll, 1994

Dear Mr. Martin:

Our letter AEP:NRC:1184F, dated September 16, 1993, responded to a violation involving degradation of an auxiliary feedwater pump bearing.

The letter contained a commitment to establish a plant wide oil sampling ynd analysis program.

Pursuant to discussions with your staff on September 19, 1994, at your offices in Lisle, IL, the attachment to this letter contains revised commitments regarding this program, and also contains>information requested by your staff regarding actions to be taken in the event oil samples indicate potential pump degradation.

This letter is submitted pursuant to 10 CFR 50.54(f),

and, as
such, an oath statement is attached.

Sincerely, EF Vice President ar Attachment 7700p~

9411210284 941111 PDR ADOCK 05000315 P

PDR ij )

pyO/

t I(

Mr. J.

B. Martin AEP'NRC 1184F1 CC:

A. A. Blind G. Charnoff NFEM Section Chief NRC Resident Inspector, Bridgman J.

R. Padgett W. T. Russell, NRC - Washington, D.C.

STATE OF OHIO)

COUNTY OF FRANKLIN)

E. E. Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing Revised Commitments Regarding Lube Oil Analysis Program, and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.

Subscribed and sworn to before me this ~i~

day of 19

~9'OTAR PUBLIC RITE D. HILL NOTARY PUDLIC. STATE OF OHIO

ATTAQBKNT TO AEP:NRC: 1184F1 REVISED COMMITMENTS REGARDING LUBE OIL SAMPLING AND ANALYSIS PROGRAM AND ACTIONS TO BE TAKEN IF OIL ANALYSIS INDICATES POSSIBLE DEGRADATION

. ~

l

ATTACHMENT TO AEP: NRC: 1184F1 Page 1

BACKGROUND Our letter AEP:NRC:1184, dated September 16,

1993, responded to a violation concerning failure of an auxiliary feedwater pump bearing.

At the

time, the principal contributor to the degradation of the bearing was thought to be the presence of

- water in the bearing oil reservoir.

As part of that violation

response, we committed to establishing a plant wide oil sampling and analysis program.

Subsequent to this failure, a task force was formed to make recommendations to enhance the operation and design of the auxiliary feedwater pumps.

The task force activities included a thorough review of the bearing failure event.

It was concluded from this review that an improperly ad]usted balance drum was the primary cause of the bearing failure.

Water contamination of the oil was cited as a contributing factor, as this condition may have reduced the ability of the bearing set to withstand the higher-than-normal thrust loads resulting from the misad]usted balance drum.

The task force recommendations included modifying the thrust bearing assembly to reduce its sensitivity to abnormal thrust loads, and improving the stuffing, box design to minimize pump leakage, These modifications were completed on the Unit 2 pumps during the 1994 Unit 2 refueling

outage, and will be completed in Unit 1 during a'future outage.

On September 19,

1994, discussions were held with your staff regarding the status of the oil sampling and analysis program.

As a result of those discussions, we were requested to clarify our docketed commitments regarding the program, including actions we would take in the event that the oil analysis results indicate possible pump degradation.

The requested information is provided below.

REVISED OIL SAMPLING AND ANALYSIS PROGRAM COMMITMENTS An oil sampling and analysis program has been established for all six auxiliary feedwater pumps.

These pumps are being sampled on a

12 week frequency, or sooner for emergent reasons.

Since April, 1993, approximately 80 samples have been obtained from these pumps.

A plant wide program has also been developed and is in the process of being implemented.

This program will augment existing vibration monitoring and IST pump performance programs to provide a more comprehensive view of equipment condition.

The following provides additional details regarding our current

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~-

~

ATTACHMENT TO AEP:NRC:1184F1 Page 2

intentions in this area.

The program may change as information on program effectiveness and value are obtained, and as improved technologies become available.

For equipment already selected for inclusion in the program, recurring task action requests have been written to init5ate the detailed planning for acquisition and processing of samples.

Planning will include identification of specific sample locations and determination of conditions required to safely obtain representative samples.

This planning evolution will also finalize the initial scope of the program to be committed to production.

Determination of program scope willinclude consideration of equipment safety function, feasibility of obtaining a meaningful

sample, and the costs/benefits of sampling.

Job orders will be written and made ready for scheduling by December 31, 1994.

2.

Job orders will be scheduled as follows:

a.

Samples which willrequire the associated generating unit to be shut down will be drawn prior to the end of the next scheduled refueling outage (Unit 1 1995, Unit 2 1996).

b.

Samples which do not require a refueling outage will be drawn before the end of the second 1995 functional equipment group cycle applicable to that equipment.

3.

The program was revised to. delineate responsibilities and procedures for engineering review of results and initiation of follow-up/corrective actions.

This revision was in place by October 31, 1994.

Our existing corrective action system will be used to guide our actions in the event the oil sample indicates degradation.

A condition report will be written upon finding and confirming an unexpected failure.

Also as agreed in our September 19,

1994, meeting, we will periodically update the Senior Resident on our progress with this plan.

0