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=Text=
=Text=
{{#Wiki_filter:,
{{#Wiki_filter:-1
                          .-
'
                              ,
.-
                                  '
,
                                                                                                                          -1
,
                    4.
4.
              '
A
A
    , _
May 23, 1989
                                                              May 23, 1989                                                   )
)
  '
'
                                                                                                                            i
, _
                Portland General Electric Company                                                                           ]
i
                121 SW Salmon Street, TB-17
Portland General Electric Company
          ~
]
              ,
'
                                                                                                                            j
~
                Portland, Oregon 97204                                                                                     ]
121 SW Salmon Street, TB-17
                                                                                                                            1
j
                                                                                                                              l
,
                : Attention: Mr. David W. Cockfield
Portland, Oregon 97204
                                Vice President, Nuclear
]
    1          Gentlemen:                                                                                               'i
1
                This refers to your letter ofc April 14, 1989, responding to our Notice of
l
                Violation contained in Nuclear Regulatory Commission Inspection Report
: Attention: Mr. David W. Cockfield
                50-344/89-01. The report identified two violations with multiple examples,
Vice President, Nuclear
                and you acknowledged the violations.
Gentlemen:
  '
'i
                Y'our response'to Violation B.2., a Quality-Assurance (QA) failure to
1
                  identify and record procedural noncompliance, does not appear to address
This refers to your letter ofc April 14, 1989, responding to our Notice of
                  the superviscr/ management contribution to this event. This violation
Violation contained in Nuclear Regulatory Commission Inspection Report
                  involved a Quality Control Inspector, a new employee, who apparently did not
50-344/89-01. The report identified two violations with multiple examples,
                  fully understand management's expectations with regards to procedural-
and you acknowledged the violations.
                compliance. .Your. improvement programs, over the past two years and as-
'
                outlined in our May 10, 1989 enforcement conference,. include clarifying
Y'our response'to Violation B.2., a Quality-Assurance (QA) failure to
                mangement expectations and assuring ' accountability of supervisors. and managers'.
identify and record procedural noncompliance, does not appear to address
                Although your; discussions in the May 10, 1989 enforcement conference
the superviscr/ management contribution to this event. This violation
                  highlighted your actions in this area, your response to this violation does
involved a Quality Control Inspector, a new employee, who apparently did not
                  not address why.~QA supervision and management did not assure that expectations-
fully understand management's expectations with regards to procedural-
                were understood.and that the individual was adequately prepared. Therefore,
compliance. .Your. improvement programs, over the past two years and as-
                  please amend'your response to include your evaluation of the adequacy of
outlined in our May 10, 1989 enforcement conference,. include clarifying
                management / supervision involvement in scoping and assignment of work
mangement expectations and assuring ' accountability of supervisors. and managers'.
                - activities. Also include in your amended response the corrective actions
Although your; discussions in the May 10, 1989 enforcement conference
                  associated with your findings and your plans for implementing your corrective
highlighted your actions in this area, your response to this violation does
                ' actions. Please provide your response'within 30 days of the date of this
not address why.~QA supervision and management did not assure that expectations-
                  letter.
were understood.and that the individual was adequately prepared.
                  The response directed by this letter is not subject to the clearance
Therefore,
                  procedures of the Office of Management and Budget as required by the Paperwork
please amend'your response to include your evaluation of the adequacy of
                  Reduction Act of 1980, PL 96-511.
management / supervision involvement in scoping and assignment of work
                  Should you have any questions concerning this matter, we will be pleased to
- activities. Also include in your amended response the corrective actions
!                 discuss them with you.
associated with your findings and your plans for implementing your corrective
                                                            /S/
' actions. Please provide your response'within 30 days of the date of this
                                                        R. P. Zimmerman, Acting Director
letter.
                                                        Division of Reactor Safety and Projects
The response directed by this letter is not subject to the clearance
                        8906050202
procedures of the Office of Management and Budget as required by the Paperwork
                          DR           890523
Reduction Act of 1980, PL 96-511.
                                ADOCK 05000344
Should you have any questions concerning this matter, we will be pleased to
                                                    *
!
                                                                                              h
discuss them with you.
                                            PNU
/S/
                                                                                                  ,\
R. P. Zimmerman, Acting Director
      t;
Division of Reactor Safety and Projects
                                                                                            - __   _ _ _ _ _ . . _ _ _ s
8906050202 890523
h
*
DR
ADOCK 05000344
PNU
,\\
t;
-
__
_ _ _ _ _ . . _ _ _
s


                                                                                          _
_
                                                                                                      _ - . ._
_ - . ._
                                                                                                                1
1
                            '
'
;      ,
.
          ,
,
                  .
;
                        ,
,
                    *
            .
                                                            .
                                                                                                              1
                                                                                                                i
,
,
  .
*
                                                          2       May 23, 1989
.
    ,
.
                                                                                                                  i
1
              bec w/ copy of letter dated 4/14/89:
i
              Docket File                                                                                     -]
,
              Resident Inspector                                                                                 .
.
              Project Inspector                                                                               ,
2
              G. Cook                                                                                         j
May 23, 1989
              A. Johnson                                                                                       i '
,
              B. Faulkenberry
i
              J. Martin.
bec w/ copy of letter dated 4/14/89:
              LFMB
Docket File
              State of Oregon
-]
              bcc w/o copy of letter dated 4/14/89:
Resident Inspector
              M. Smith
.
Project Inspector
,
G. Cook
j
A. Johnson
i
'
B. Faulkenberry
J. Martin.
LFMB
State of Oregon
bcc w/o copy of letter dated 4/14/89:
M. Smith
i
i
lI
lI
j
j
        '
'
              'RV/jk
'RV/jk
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                                            Y
A{quESTCOPY
                A{quESTCOPY       REQUEST     '  REQUEST CLPY "
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                [JES / N0         YES / N0
'
                                        V     i   SE ' TO PDR
'
                                                ' _ES / N0     J
"
              MENDONCA Afl     CHAFFEE A ZIMMERMAN S &
[JES / N0
              5/20/89           5/2889       5/e/89
YES / N0
                                                                                  . _ _ _ - _ _ - _ _
YES /CE)
V
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SE ' TO PDR
' _ES / N0
J
MENDONCA Afl
CHAFFEE A ZIMMERMAN S &
5/20/89
5/2889
5/e/89
. _ _ _ - _ _ - _ _


    _
_
                  . - _
. - _
                                                                                .-
.-
                              O               .
O
  -
.
      . .-
. .-
            .
j
                        g.                                                 _
.
                                                                              .
.
                                                                                                                                                                                        er   j
g.
                                                                                            PortlandGeneralElechicCcripeniy
-
                                  ,-                                        - g                                                                        ,
er
                                                                                                                                                          ,
_
                                                                                                                                                                        .
,
                                                                                                                                                                                ,J[,l!
.
                                                                                          David W. Cockfield Vice President, Nuclear
,J[,l!
                                                                                                                                                                              [               p
P
                                                                                                                                        April 14, 1989
,-
                                                                                                                                        Trojan Nuclear Plant                               h
- g
                                                                                                                                        Docket 50-344                             g
ortlandGeneralElechicCcripeniy
                                                                                                                                        License NPF-1
,
                                                                                                                                                                              /
David W. Cockfield Vice President, Nuclear
                                                                            U.S. Nuclear Regulatory Commission
[
                                                                            ATTN: Document Control Desk
p
                                                                            Washington DC 20555
April 14, 1989
                                                                            Dear Sir:
Trojan Nuclear Plant
                                                                                                            Reply to a Notice of Violation
h
                                                                            Your letter of Merch 15, 1989 transmitted a Notice of Violation associated
Docket 50-344
                                                                            with Nuclear Regulatory Commission Inspection Report 50-344/89-01.
g
                                                                            Attached is our response to that Notice of Violation.
License NPF-1
                                                                                                                                Sincerely,
/
                                                                                                                                                    /
U.S. Nuclear Regulatory Commission
                                                                      > Attachment                                                                                   c
ATTN: Document Control Desk
                                                                                                                                                                ]
Washington DC 20555
                                                                            c:    VNr.JohnB. Martin                                                             '
Dear Sir:
                                                                                                                                                                                      .~ ]
Reply to a Notice of Violation
                                                                                    Regional Administrator, Region V                             ./                   <
Your letter of Merch 15, 1989 transmitted a Notice of Violation associated
                                                                                                                                                                        !'' ' -    J'
with Nuclear Regulatory Commission Inspection Report 50-344/89-01.
                                                                                                                                                                                          '
Attached is our response to that Notice of Violation.
                                                                                    U.S. Nuclear Regulatory Commission                         t h'h                                1
Sincerely,
                                                                                    Mr. William T. Dixon                                             .      1               -
/
                                                                                    State of Oregon
> Attachment
                                                                                    Department of Ener6Y                                         '
c
                                                                                                                                                  j[
VNr.JohnB. Martin
                                                                                                                                                              '''
]
                                                                                                                                                                    '
!'' ' -
                                                                                                                                                                        ,' j  '
.~ ]
                                                                                                                                                                  '
c:
                                                                                                                                                          .              ,
'
                                                                                                                                                      /,-           -
Regional Administrator, Region V
                                                                                    Mr. R. C. Barr                                                 '/'
./
                                                                                                                                                      ,
J'
                                                                                    NRC Resident Inspector
'
                                                                                    Trojan Nuclear Plant
<
                                                                                                                                          c,
h'h
                                                                                                                                            '
1
:                                                                                                                                         -
U.S. Nuclear Regulatory Commission
                                                                                                                                  ,\
t
                                                                                                                                  u
Mr. William T. Dixon
                                                                                                                      6 . Q\d
1
                                                                                                                            -
-
                                                                                        ,j   nn   .n
.
                                                                                                                -
State of Oregon
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j[
                                                                                          121 SW Samon Sree* Poaana Oregon 9720i
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-       _ - _ - _ _ - _ _ - _ _ _ - _ - - - _ _ _ _ _ _ _ _ _ - _ - _ _ - _
'
Department of Ener6Y
.
,
'
' ' '
'
'
/,-
-
Mr. R. C. Barr
'/'
,
NRC Resident Inspector
Trojan Nuclear Plant
c,
'
:
,\\
-
6 . Q\\d
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-
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121 SW Samon Sree* Poaana Oregon 9720i
-
_ - _ - _ _ - _ _ - _ _ _ - _ - - - _ _ _ _ _ _ _ _ _ - _ - _ _ - _


    __ _ _ _ _ - - - _
__ _ _ _ _ - - - _
-                           -
-
                                                :
-
                            ..
:
              -        .        *'Trp5cn vueleer Plcnt                                                                                                     Document C3ntrol Dack
;
  .                         ,,     ; Dock;t 50-344                                                                                                         Attechment-
..
                          '
*'Trp5cn vueleer Plcnt
                                      License NPF-1                                                                                                           April 14, 1989
Document C3ntrol Dack
                                                                                                                                                              Page 1 of 7
-
                                                                                                                        REPLY TO A NOTICE OF VIOLATION
.
                                      VIOLATION A
,,
                                                                                                                                                                                      1
; Dock;t 50-344
                                      Title 10 to the Code of Federal Regulations Part 50.9 (10 CFR 50.9)                                                                             I
Attechment-
                                      states, in part:
.
                                                                                                          "Information provided to the Commission by . . . a
License NPF-1
                                                                                                          licensee . shall be complete and accurate in all
April 14, 1989
                                                                                                          material respects."
'
                                    Contrary to the above, on February 2, 1989, the inspectors found that
Page 1 of 7
                                    Plant Operations Test (PDT) Procedure 26-2, Revision 24. " Process
REPLY TO A NOTICE OF VIOLATION
                                    Radiation Monitor Calibration," had not been changed as stated in
VIOLATION A
                                    Licensee Event Report (LER) 88-49, Revision 0, " Partial Containment
1
                                    Isolations Result From Signal Spike and Operator Error," dated
Title 10 to the Code of Federal Regulations Part 50.9 (10 CFR 50.9)
                                    January 26, 1989.
I
                                    This is a Severity Level IV violation (Supplement 1).
states, in part:
                                    REPLY TO VIOLATION A
"Information provided to the Commission by . . . a
                                    Portland Ceneral Electric (PCE) Company acknowledges the violation.
licensee .
                                      1.                             Reason for Violation:
shall be complete and accurate in all
                                                                      The reason for the violation was personnel error. The statement in
.
                                                                      LER 88-49 was based upon input provided by the Chemistry Branch
material respects."
                                                                      Manager. This input was incorrect due to miscommunication between
Contrary to the above, on February 2, 1989, the inspectors found that
                                                                      .the Chemistry Branch Manager and a'=amhae of his staff and the mann-
Plant Operations Test (PDT) Procedure 26-2, Revision 24. " Process
                                                        p*s failurw to. verify that_the change to 70T-26-2.was complete.
Radiation Monitor Calibration," had not been changed as stated in
                                      2.                             Corrective Steps Taken and Results Achieved:
Licensee Event Report (LER) 88-49, Revision 0, " Partial Containment
                                                                      a.                                 On February 2,1989, a temporary change to POT-26-2 was immedi-
Isolations Result From Signal Spike and Operator Error," dated
                                                                                                          ately implemented which appropriately revised the procedure as
January 26, 1989.
                                                                                                          described in LER 88-49.
This is a Severity Level IV violation (Supplement 1).
                                                                      b.                                 On March 23, 1989, Revision 25 to POT-26-2 was approved, which
REPLY TO VIOLATION A
                                                                                                          incorporated the temporary changes.
Portland Ceneral Electric (PCE) Company acknowledges the violation.
                                                                      c.                                The procedure providing guidance for writing LERs, Nuclear
1.
                                                                                                          Safety and Regulation Instruction (NSRI) 900-2Q entitled                     I
Reason for Violation:
                                                                                                          " Licensee Event Report Preparation and Review," was changed on
The reason for the violation was personnel error. The statement in
                                                                                                          February 11, 1989 to specifically require obtaining the proce-
LER 88-49 was based upon input provided by the Chemistry Branch
                                                                                                          dure revision number and date when making statements in an LER
Manager. This input was incorrect due to miscommunication between
                                                                                                          that a procedure has been changed.
.the Chemistry Branch Manager and a'=amhae of his staff and the mann-
                                                                                                                                                                                        !
p*s failurw to. verify that_the change to 70T-26-2.was complete.
                                                                                                                                                                                        i
2.
--                                     - _ _ - _ _ - _ _ _ _ _ _ - _ _ - _ - - - _ _ _ _ - - - _ _ . _ _                             -- - _ - _ _ _ _ - --   .__ _           _ _ 1
Corrective Steps Taken and Results Achieved:
a.
On February 2,1989, a temporary change to POT-26-2 was immedi-
ately implemented which appropriately revised the procedure as
described in LER 88-49.
b.
On March 23, 1989, Revision 25 to POT-26-2 was approved, which
incorporated the temporary changes.
The procedure providing guidance for writing LERs, Nuclear
c.
Safety and Regulation Instruction (NSRI) 900-2Q entitled
I
" Licensee Event Report Preparation and Review," was changed on
February 11, 1989 to specifically require obtaining the proce-
dure revision number and date when making statements in an LER
that a procedure has been changed.
i
--
- _ _ - _ _ - _ _ _ _ _ _ - _ _ - _ - - - _ _ _ _ - - - _ _ . _ _
--
- _ - _ _ _ _ - --
.__
_
_
_
1


_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _   _ _ _ _ _ _                                                           _ _ _ _ _ _ _ _ _ _     _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                                                                                                                                                          _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ ,
_ _ _ _ _ _
        .
_ _ _ _ _ _ _ _ _ _
                          -
_
                                      ,-
_ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ ,
                      *
.
                        $.         .
-
                                                -
,-
          -       *
$.
                                Tro'jan Nur,lo:r Plcnt                                                                                                                                         D; cum:nt Cantrol D2sk
.
      -
*
                        ,.~;D ck;t 50 344
-
                                                                                                                                                                                                Attachment
Tro'jan Nur,lo:r Plcnt
                    '
D; cum:nt Cantrol D2sk
                                !icense BTPF-1                                                                                                                                                 April 14, 1989
-
                                                                                                                                                                                                Page 2 of 7
*
                                                                                                                                                                                                                                                                                        I
,.~;D ck;t 50 344
                                          d.       The importance of ensuring that information provided to the NRC                                                                                                                                                                     i
Attachment
                                                  be complete and accurate was reemphasized with the appropriate
-
                                                  personnel involved. In addition, a February 15, 1989 memorandum
!icense BTPF-1
                                                  was issued by the Vice President Nuclear to all managers and
April 14, 1989
                                                  supervisors stressing the importance of ensuring that
'
                                                  information be verified as accurate and complete.
Page 2 of 7
                                  3.     Corrective Steps That Will be Taken to Avoid Further. Violations:
I
                                        .All cerrective steps have been completed. Continued management
d.
                                          attention will be provided to ensure that these corrective steps are
The importance of ensuring that information provided to the NRC
                                          effective.
i
                                  4.     Date When Full Compliance Will Be Achieved:
be complete and accurate was reemphasized with the appropriate
                                          Full compliance has been achieved.
personnel involved. In addition, a February 15, 1989 memorandum
                                                                                                                                                                                                                            .
was issued by the Vice President Nuclear to all managers and
                                                                                      _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - - -                                                                             -_-_-
supervisors stressing the importance of ensuring that
information be verified as accurate and complete.
3.
Corrective Steps That Will be Taken to Avoid Further. Violations:
.All cerrective steps have been completed. Continued management
attention will be provided to ensure that these corrective steps are
effective.
4.
Date When Full Compliance Will Be Achieved:
Full compliance has been achieved.
.
_ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - - -
-_-_-


      _ _ _ _ _ _ - -       ._ _
_ _ _ _ _ _ - -
    >
._ _
                                    .
>
                        ..
.
                - ..        ' 'Trpjr.n Cue 10 r Pltnt                                           Document Contral'D30k
..
l. .
' 'Trpjr.n Cue 10 r Pltnt
                          ., , , Dock;t 50-344 -                                               Attcchment
Document Contral'D30k
l                               License NPF-1                                                   April 14, 1989
- ..
                      '
., , , Dock;t 50-344 -
(                                                                                                Page 3 of 7
Attcchment
l.
.
l
License NPF-1
April 14, 1989
(
Page 3 of 7
'
1
VIOLATION B
1
1
                                VIOLATION B
1
1
1                                Title 10 to the Code of Federal Regulations, Part 50 (10 CFR 50), Appen-
Title 10 to the Code of Federal Regulations, Part 50 (10 CFR 50), Appen-
l                               dix B, Criterion V, states, in part:
l
                                            " Activities affecting quality shall be prescribed by
dix B, Criterion V, states, in part:
i                                           documented instructions, procedures, or drawings of a
" Activities affecting quality shall be prescribed by
                                            type appropriate to the circumstances and shall be
i
                                            accomplished in accordance with these instructions,
documented instructions, procedures, or drawings of a
                                            procedures, or drawings."
type appropriate to the circumstances and shall be
                                  1.   Periodic Instrument and Control Test (PICT)-5-2, " Steam Generator
accomplished in accordance with these instructions,
                                      Level, Protection Set II," Revision 12, approved August 26, 1988,
procedures, or drawings."
                                      requires, in part, the use of multiple photocells associated with
1.
                                      the comparator logic tester and the use of a simulated test signal                                               !
Periodic Instrument and Control Test (PICT)-5-2, " Steam Generator
                                                                                                                                                      '
Level, Protection Set II," Revision 12, approved August 26, 1988,
                                      initially set at five volts, decreased to one volt while recording
requires, in part, the use of multiple photocells associated with
                                      applicable bistable actions, and then increased while recording
the comparator logic tester and the use of a simulated test signal
                                      applicable bistable actions.
!
                                                                                                                                                      I
'
                                      Contrary to the above, on February 2,1989, test personnel performed
initially set at five volts, decreased to one volt while recording
                                      the test in a manner inconsistent with the procedure, in that only
applicable bistable actions, and then increased while recording
                                      one photocell associated with the comparator logic tester was used
applicable bistable actions.
                                      and the simulated test signal was ramped down and up in a staggered
I
                                      fashion to obtain data for each bistable action until the signal was
Contrary to the above, on February 2,1989, test personnel performed
                                      decreased to one volt.
the test in a manner inconsistent with the procedure, in that only
                                      1his is a Severity Level V violation (Supplement I).
one photocell associated with the comparator logic tester was used
                                  2.   Licensee Quality Inspection Procedure (QIP) IS, "QI observations of
and the simulated test signal was ramped down and up in a staggered
                                      I&C Calibration Activities," Revision 0, approved January 4, 1989,
fashion to obtain data for each bistable action until the signal was
                                      specifies in part, that the quality control inspector shall note
decreased to one volt.
                                      Whether work -was Performed in accordance .with spps _d instzw+ 4 ans,
1his is a Severity Level V violation (Supplement I).
                                                                                            .
2.
                                      procedures, and/or technical manuals to assure that Plant proce-
Licensee Quality Inspection Procedure (QIP) IS, "QI observations of
                                      dures, work package instructions, and installation standards are
I&C Calibration Activities," Revision 0, approved January 4, 1989,
                                      followed.
specifies in part, that the quality control inspector shall note
                                      Contrary to the above, on February 2, 1989, a quality control
Whether work -was Performed in accordance .with spps _d instzw+ 4 ans,
                                      inspector failed to note and document failures to follow approved
.
                                      procedures during the performance of channel functional testing of
procedures, and/or technical manuals to assure that Plant proce-
                                      steam generator water level instrumentation per licensee procedure
dures, work package instructions, and installation standards are
                                      PICT-5-2.
followed.
                                      This is a Severity Level IV violation (Supplement I).
Contrary to the above, on February 2, 1989, a quality control
                                  3.   Licensee Plant Safety Procedure (PS) 3-30. Revision 17, Section IV
inspector failed to note and document failures to follow approved
                                      Item E. states: "It is the responsibility of the person accepting
procedures during the performance of channel functional testing of
                                      the equipment clearance to check the equipment clearance and assure
steam generator water level instrumentation per licensee procedure
                                      himself that the equipment is satisfactorily tagged and the equip-
PICT-5-2.
                                      ment is deenergized and cleared fnr work before starting work."
This is a Severity Level IV violation (Supplement I).
                                      Further, licensee procedure Administrative Order (AO) 3-9,
3.
                                                                                              _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - - _ -
Licensee Plant Safety Procedure (PS) 3-30. Revision 17, Section IV
Item E. states:
"It is the responsibility of the person accepting
the equipment clearance to check the equipment clearance and assure
himself that the equipment is satisfactorily tagged and the equip-
ment is deenergized and cleared fnr work before starting work."
Further, licensee procedure Administrative Order (AO) 3-9,
_ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - - _ -


              __ ___                                 _
__ ___
                                                                                .
_
                                                                                              _
.
                                                                                                                    -
_
                                                                                  *
-
*
r
r
' '' . EU                                                                     .
. EU
                                      .
' '
                                                  .             -
.
                                                                                                              ,;                                                                     )
,;
                                                                                  ,
)
            *   "' "
'
                                                                  Trajhn Nucicar P1hnt.                                                                       Dscument Control D3Ek
.
          F                                                                                                                                                                         i
-
                                                  d ''' Docket l50-344.                                                                                       Attachment           !
,
                                  .                                License NPF-1                                                                               April'14, 1989       !
.
                                                                                                                                                              Page 4.of 7
*
                  '
Trajhn Nucicar P1hnt.
Dscument Control D3Ek
"' "
F
d ''' Docket l50-344.
Attachment
!
i
License NPF-1
April'14, 1989
!
.
Page 4.of 7
(h?
(h?
                                                                                              Revision 26, Section.I. Item 4. states: "The assigned craftsman /
'
                                                                                              technician performs the maintenance prescribed by the MR work
Revision 26, Section.I. Item 4. states: "The assigned craftsman /
        '
l-
l-
'
'
                                                                                              instructions and documents itsl completion in the work performed
technician performs the maintenance prescribed by the MR work
                                                                                              section of the MR."
'
                                                                                            Contrary to the above, on February 12,-1988, a Maintenance craftsman
instructions and documents itsl completion in the work performed
                                                                                            replaced;the charcoal'adsorber in the "B" Train of.the containment
section of the MR."
                                                                                            Hydrogen Vent System that was not tagged out or cleared for work,
Contrary to the above, on February 12,-1988, a Maintenance craftsman
                                                                                            and failed to replace the charcos1 adsorber of'the "A" Containment
replaced;the charcoal'adsorber in the "B" Train of.the containment
                                                                                            Hydrogen Vent System specified in KR werk instructions.
Hydrogen Vent System that was not tagged out or cleared for work,
                                                                                            This is a Severity Level IV violation (Supplement I).
and failed to replace the charcos1 adsorber of'the
                                                                REPLY TO VIOLATION B.1
"A" Containment
                                                                PGE acknowledges the violation.
Hydrogen Vent System specified in KR werk instructions.
                                                                    1. . Reason for: the Violation:
This is a Severity Level IV violation (Supplement I).
                                                                                            The reason for this violation is personnel error. Personnel failed
REPLY TO VIOLATION B.1
                                                                                            to follow the procedure exactly as written, and assumed that actions
PGE acknowledges the violation.
                                                                                                        .
1. . Reason for: the Violation:
                                                                                            that were technically equivalent to the steps in the procedure could
The reason for this violation is personnel error. Personnel failed
                                                                                          be' substituted without making a procedure revision or deviation.
to follow the procedure exactly as written, and assumed that actions
                                                                                          Subsequent review found that the problem of not connecting the
.
                                                                                          comparator photocell to the light specified in the procedure was
that were technically equivalent to the steps in the procedure could
                                                                                          common to other procedures.               In addition, the practice of raising.
be' substituted without making a procedure revision or deviation.
                                                                                          and lowering the test signal When all photocells were not operable
Subsequent review found that the problem of not connecting the
                                                                                          was a common past practice.
comparator photocell to the light specified in the procedure was
                                                                  J.                     Corzwet.ive<. steps 2aken 6Jiasult.s Aahad:
common to other procedures.
                                                                                          All PICTs were reviewed to determine where a similar problem
In addition, the practice of raising.
                                                                                          existed. A procedure deviation was made to all applicable proce-
and lowering the test signal When all photocells were not operable
                                                                                          dures to correct the photocell location and to permit the test
was a common past practice.
                                                                                          signal to either ramp continuously up and down, or to be stepped.at'
J.
                                                                                          the discretion of the technician performing the test. This action
Corzwet.ive<. steps 2aken 6Jiasult.s Aahad:
                                                                                          was completed on February 27, 1989.
All PICTs were reviewed to determine where a similar problem
                                                                                        Management expectations for limitations on procedure flexibill,ty
existed. A procedure deviation was made to all applicable proce-
                                                                                        were discussed with Maintenance electrical and instrumentation and
dures to correct the photocell location and to permit the test
                                                                                          control (I&C) personnel and their supervisors. Personac1 were
signal to either ramp continuously up and down, or to be stepped.at'
                                                                                        advised that technical or electrical equivalency is not sufficient
the discretion of the technician performing the test. This action
                                                                                        justification for not following the procedure as written. If an
was completed on February 27, 1989.
                                                                                        equivalent method is to be used, the procedure or work instruction
Management expectations for limitations on procedure flexibill,ty
                                                                                        must be changed to reflect it.                   This was also discussed with
were discussed with Maintenance electrical and instrumentation and
      ,
control (I&C) personnel and their supervisors. Personac1 were
                                                                                        temporary Maintenance employees that are being used for the
advised that technical or electrical equivalency is not sufficient
                                                                                        1989 outage.
justification for not following the procedure as written.
                    _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _           _ _ _ _ _ _ _
If an
equivalent method is to be used, the procedure or work instruction
must be changed to reflect it.
This was also discussed with
temporary Maintenance employees that are being used for the
,
1989 outage.
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _


                                                                                                        _               _ _ _ _ - _ - -
_
                                                                                                    _.
_ _ _ _ - _ - -
            .,, ,         .
_.
. , ,
.
,
Trhjcn Nuclocr Pirnt
* * *
Document Control Desk
-, i Dockbt 50-344
'
'
  * * *
Attachment
                  Trhjcn Nuclocr Pirnt                                                            Document Control Desk
License NPF-1
              -, i Dockbt 50-344
April 14, 1989-
                                                                                                    Attachment
,
          ,        License NPF-1                                                                   April 14, 1989-
Page 5 of 7
                                                                                                    Page 5 of 7
3.
                    3. Corrective Steps That Will Be Taken to Avoid Further Violations:
Corrective Steps That Will Be Taken to Avoid Further Violations:
                        The lessons learned from this event will be incorporated into the
The lessons learned from this event will be incorporated into the
                        Periodic Maintenance Retraining Program. This will be completed
Periodic Maintenance Retraining Program. This will be completed
                        before the next session scheduled to begin in September 1989.
before the next session scheduled to begin in September 1989.
                    4. Date We oFull Compliance Will Be Achieved:
4.
                        Full compliance has been achieved.
Date We Full Compliance Will Be Achieved:
        .
o
                                                  - - .     _       . _ _ _ _ _ _ _ _ - _ _ _ _ _             -______-
Full compliance has been achieved.
.
- - .
_
. _ _ _ _ _ _ _ _ - _ _ _ _ _
-______-


                                                                                                  _ _ _ _ __ ____ _ _ ___-__ _ _ - __
_ _ _ _ __ ____ _ _ ___-__ _ _ - __
c-
c-
                      ,
,
          . .
. .
                  4
4
    '       ..         .
'
      < *
..
                    Trojcn Nuclocr PICnt
.
  *                                                                                                              D cument Contr31 De:k
*
                -
Trojcn Nuclocr PICnt
                    Docket 50-344                                                                               Attachment
D cument Contr31 De:k
        .
<
                    License NPF-1                                                                               April 14, 1989
*
                                                                                                                  page 6 of 7
Docket 50-344
                    REPLY TO VIOLATION B.2
Attachment
                    PGE acknowledges the violation.
-
                      1.   Reason for the Violation:
.
                            The reason for this violation is personnel error. The quality
License NPF-1
                            control inspector failed to recognize the procedural noncompliance
April 14, 1989
                            because he had not adequately reviewed the PICT-5-2 procedure ahead
page 6 of 7
                            of time and did not have a copy of the procedure with him while
REPLY TO VIOLATION B.2
                            observing the channel functional testing. The inspector was
PGE acknowledges the violation.
                          notified of his assignment to perform the observation only a few
1.
                          minutes before the testing was to begin.
Reason for the Violation:
                      2.   Corrective Steps Taken and Results Achieved:
The reason for this violation is personnel error. The quality
                          a.    Management expectations of the role of quality control inspec-
control inspector failed to recognize the procedural noncompliance
                                  tions in verifying procedural compliance were discussed with all
because he had not adequately reviewed the PICT-5-2 procedure ahead
                                inspectors. It was emphasized that verification of procedural
of time and did not have a copy of the procedure with him while
                                compliance requires that the inspector be familiar with the
observing the channel functional testing. The inspector was
                                procedure and have a copy with him during the observation.
notified of his assignment to perform the observation only a few
                                Subsequent PICT observations performed by quality control
minutes before the testing was to begin.
                                inspectors have been observed by management to enmare that
2.
                                expectations are implemented,
Corrective Steps Taken and Results Achieved:
                          b.   Scheduling of PICT observations has been improved. Inspectors
Management expectations of the role of quality control inspec-
                                are now assigned to specific PICT observations well in advance,
a.
                                allowing adequate preparation time.
tions in verifying procedural compliance were discussed with all
                    3.   Corrective Steps That Will Be Taken to Avoid Further Violations:
inspectors.
                          me 41ectrical quality control inspectors-will Participate in :the
It was emphasized that verification of procedural
                                classroom training sessions of the I&C technician quarterly
compliance requires that the inspector be familiar with the
                                training program to improve the inspectors' knowledge of I&C
procedure and have a copy with him during the observation.
                                activities. Participation in this training is scheduled to
Subsequent PICT observations performed by quality control
                                begin in September 1989.
inspectors have been observed by management to enmare that
                          b,   All electrical quality control inspectors will attend formal
expectations are implemented,
                                observation training by August 1, 1989.
b.
  *
Scheduling of PICT observations has been improved.
                    4.   Date When Full Compliance Will Be Achieved:
Inspectors
                          Full compliance has been achieved.
are now assigned to specific PICT observations well in advance,
                                                                                  _ - _ _ _ _ _ - _ _ _ _ - _ _ _                     _ - - _ _ -
allowing adequate preparation time.
3.
Corrective Steps That Will Be Taken to Avoid Further Violations:
me 41ectrical quality control inspectors-will Participate in :the
classroom training sessions of the I&C technician quarterly
training program to improve the inspectors' knowledge of I&C
activities. Participation in this training is scheduled to
begin in September 1989.
b,
All electrical quality control inspectors will attend formal
observation training by August 1, 1989.
4.
Date When Full Compliance Will Be Achieved:
*
Full compliance has been achieved.
_ - _ _ _ _ _ - _ _ _ _ - _ _ _
_ - - _ _ -


                                                                                            _
_
                                                                                                      . _ _ _ _ _ - - -
. _ _ _ _ _ - - -
    ,
,
                  .
.
                '
'
          *
Trajtn Wuclcrr plcnt
                  Trajtn Wuclcrr plcnt
Document Contesl De:k
  '
*
      .
.
                                                                                    Document Contesl De:k
'
            . . Dr.cket 50-344                                                       Attachment
. . Dr.cket 50-344
        .        License NPF-1                                                     April 14, 1989
Attachment
                                                                                    Page 7 of 7
License NPF-1
                  REPLY TO VIOLATION B.3
April 14, 1989
                  PGE acknowledges the violation.
.
                  1.   Reason for the Violation:
Page 7 of 7
                        The reason for this violation is personnel error. The replacement
REPLY TO VIOLATION B.3
                        of the charcoal adsorber for the "A" Containment Hydrogen Vent
PGE acknowledges the violation.
                        System was to have been performed under a clearance accepted by the
1.
                        system engineer. The system engineer had verified that the equip-
Reason for the Violation:
                      ment was tagged, deenergized, and cleared for work. However,
The reason for this violation is personnel error. The replacement
                        miscommunication between the system engineer and the maintenance
of the charcoal adsorber for the
                        craftsman resulted in the craftsman replacing the "B" charcoal
"A" Containment Hydrogen Vent
                        adsorber. In addition, the craftsman did not have a copy of the
System was to have been performed under a clearance accepted by the
                      Maintenance Request (MR) with him when performing the work, and
system engineer. The system engineer had verified that the equip-
                        relied solely on verbal instructions from the system engineer.
ment was tagged, deenergized, and cleared for work. However,
                  2. Corrective Steps Taken and Results Achieved:
miscommunication between the system engineer and the maintenance
                      a.     Upon discovery on February 23, 1988 that the "B" charcoal
craftsman resulted in the craftsman replacing the "B" charcoal
                              adsorber had been replaced, the "B" Containment Hydrogen Vent
adsorber.
                              System was placed in an inoperable status. On July 1, 1988,
In addition, the craftsman did not have a copy of the
                              during the annual refueling outage, the required operability
Maintenance Request (MR) with him when performing the work, and
                              testing was performed on the   "B" charcoal adsorber with
relied solely on verbal instructions from the system engineer.
                              satisfactory results. The system was returned to operable
2.
                              status.
Corrective Steps Taken and Results Achieved:
                      b.     The craftsman received additional instruction on the need to
a.
                              carefully read and follow instructions when performing work
Upon discovery on February 23, 1988 that the "B" charcoal
                              under an MR. The engineer received additional training on the                               ~
adsorber had been replaced, the
                          ' necessity.cf being certain that verbal or written J.nstzw+ 4-
"B" Containment Hydrogen Vent
                            .
System was placed in an inoperable status. On July 1, 1988,
                            -3re c.ltar, templete and, Where requittni, .nference irpecific
during the annual refueling outage, the required operability
                              component identification numbers.
testing was performed on the
                      c.     Maintenance personnel have received training on AD 3-9,
"B" charcoal adsorber with
                              " Maintenance Requests," specifically relating to verbal instruc-
satisfactory results. The system was returned to operable
                              tions.   Emphasis was placed on properly documenting verbal
status.
                              instructions.
b.
                      d.   Maintenance personnel are now required to have a " field copy" of
The craftsman received additional instruction on the need to
carefully read and follow instructions when performing work
under an MR.
The engineer received additional training on the
~
' necessity.cf being certain that verbal or written J.nstzw+ 4-
.
-3re c.ltar, templete and, Where requittni, .nference irpecific
component identification numbers.
c.
Maintenance personnel have received training on AD 3-9,
" Maintenance Requests," specifically relating to verbal instruc-
tions.
Emphasis was placed on properly documenting verbal
instructions.
d.
Maintenance personnel are now required to have a " field copy" of
the MR at the worksite to assure that the procedures are
,
)
followed and there is no confusion as to the instructions,
procedures or intent of the MR.
3.
Corrective Steps That Will Be Taken to Avoid Further Violations:
All corrective steps have been completed.
4.
Date When Full Compliance Will Be Achieved:
,
,
                              the MR at the worksite to assure that the procedures are
)                            followed and there is no confusion as to the instructions,
                            procedures or intent of the MR.
                  3.  Corrective Steps That Will Be Taken to Avoid Further Violations:
                      All corrective steps have been completed.
,                4.  Date When Full Compliance Will Be Achieved:
1
1
                      Full compliance has been achieved.
Full compliance has been achieved.
                DLN/mr/3008W.0489
DLN/mr/3008W.0489
                                                                                                                        1
1
                                                                            _-____--____________-__--_-_________________a
_-____--____________-__--_-_________________a
}}
}}

Latest revision as of 19:33, 1 December 2024

Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-344/89-01.Response to Violation B.2 Re QA Does Not Appear to Address Supervisor /Mgt Contribution to Event.Amend to Response Requested
ML20247M957
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 05/23/1989
From: Zimmerman R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Cockfield D
PORTLAND GENERAL ELECTRIC CO.
References
NUDOCS 8906050202
Download: ML20247M957 (2)


See also: IR 05000344/1989001

Text

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May 23, 1989

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Portland General Electric Company

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121 SW Salmon Street, TB-17

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Portland, Oregon 97204

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Attention: Mr. David W. Cockfield

Vice President, Nuclear

Gentlemen:

'i

1

This refers to your letter ofc April 14, 1989, responding to our Notice of

Violation contained in Nuclear Regulatory Commission Inspection Report

50-344/89-01. The report identified two violations with multiple examples,

and you acknowledged the violations.

'

Y'our response'to Violation B.2., a Quality-Assurance (QA) failure to

identify and record procedural noncompliance, does not appear to address

the superviscr/ management contribution to this event. This violation

involved a Quality Control Inspector, a new employee, who apparently did not

fully understand management's expectations with regards to procedural-

compliance. .Your. improvement programs, over the past two years and as-

outlined in our May 10, 1989 enforcement conference,. include clarifying

mangement expectations and assuring ' accountability of supervisors. and managers'.

Although your; discussions in the May 10, 1989 enforcement conference

highlighted your actions in this area, your response to this violation does

not address why.~QA supervision and management did not assure that expectations-

were understood.and that the individual was adequately prepared.

Therefore,

please amend'your response to include your evaluation of the adequacy of

management / supervision involvement in scoping and assignment of work

- activities. Also include in your amended response the corrective actions

associated with your findings and your plans for implementing your corrective

' actions. Please provide your response'within 30 days of the date of this

letter.

The response directed by this letter is not subject to the clearance

procedures of the Office of Management and Budget as required by the Paperwork

Reduction Act of 1980, PL 96-511.

Should you have any questions concerning this matter, we will be pleased to

!

discuss them with you.

/S/

R. P. Zimmerman, Acting Director

Division of Reactor Safety and Projects

8906050202 890523

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May 23, 1989

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bec w/ copy of letter dated 4/14/89:

Docket File

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Resident Inspector

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Project Inspector

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David W. Cockfield Vice President, Nuclear

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April 14, 1989

Trojan Nuclear Plant

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Docket 50-344

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License NPF-1

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U.S. Nuclear Regulatory Commission

ATTN: Document Control Desk

Washington DC 20555

Dear Sir:

Reply to a Notice of Violation

Your letter of Merch 15, 1989 transmitted a Notice of Violation associated

with Nuclear Regulatory Commission Inspection Report 50-344/89-01.

Attached is our response to that Notice of Violation.

Sincerely,

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VNr.JohnB. Martin

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Regional Administrator, Region V

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U.S. Nuclear Regulatory Commission

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Mr. William T. Dixon

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State of Oregon

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Department of Ener6Y

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Mr. R. C. Barr

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NRC Resident Inspector

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Document C3ntrol Dack

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Dock;t 50-344

Attechment-

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License NPF-1

April 14, 1989

'

Page 1 of 7

REPLY TO A NOTICE OF VIOLATION

VIOLATION A

1

Title 10 to the Code of Federal Regulations Part 50.9 (10 CFR 50.9)

I

states, in part:

"Information provided to the Commission by . . . a

licensee .

shall be complete and accurate in all

.

material respects."

Contrary to the above, on February 2, 1989, the inspectors found that

Plant Operations Test (PDT) Procedure 26-2, Revision 24. " Process

Radiation Monitor Calibration," had not been changed as stated in

Licensee Event Report (LER) 88-49, Revision 0, " Partial Containment

Isolations Result From Signal Spike and Operator Error," dated

January 26, 1989.

This is a Severity Level IV violation (Supplement 1).

REPLY TO VIOLATION A

Portland Ceneral Electric (PCE) Company acknowledges the violation.

1.

Reason for Violation:

The reason for the violation was personnel error. The statement in

LER 88-49 was based upon input provided by the Chemistry Branch

Manager. This input was incorrect due to miscommunication between

.the Chemistry Branch Manager and a'=amhae of his staff and the mann-

p*s failurw to. verify that_the change to 70T-26-2.was complete.

2.

Corrective Steps Taken and Results Achieved:

a.

On February 2,1989, a temporary change to POT-26-2 was immedi-

ately implemented which appropriately revised the procedure as

described in LER 88-49.

b.

On March 23, 1989, Revision 25 to POT-26-2 was approved, which

incorporated the temporary changes.

The procedure providing guidance for writing LERs, Nuclear

c.

Safety and Regulation Instruction (NSRI) 900-2Q entitled

I

" Licensee Event Report Preparation and Review," was changed on

February 11, 1989 to specifically require obtaining the proce-

dure revision number and date when making statements in an LER

that a procedure has been changed.

i

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_ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ ,

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Tro'jan Nur,lo:r Plcnt

D; cum:nt Cantrol D2sk

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Attachment

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!icense BTPF-1

April 14, 1989

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Page 2 of 7

I

d.

The importance of ensuring that information provided to the NRC

i

be complete and accurate was reemphasized with the appropriate

personnel involved. In addition, a February 15, 1989 memorandum

was issued by the Vice President Nuclear to all managers and

supervisors stressing the importance of ensuring that

information be verified as accurate and complete.

3.

Corrective Steps That Will be Taken to Avoid Further. Violations:

.All cerrective steps have been completed. Continued management

attention will be provided to ensure that these corrective steps are

effective.

4.

Date When Full Compliance Will Be Achieved:

Full compliance has been achieved.

.

_ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - - -

-_-_-

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' 'Trpjr.n Cue 10 r Pltnt

Document Contral'D30k

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Attcchment

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License NPF-1

April 14, 1989

(

Page 3 of 7

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1

VIOLATION B

1

1

Title 10 to the Code of Federal Regulations, Part 50 (10 CFR 50), Appen-

l

dix B, Criterion V, states, in part:

" Activities affecting quality shall be prescribed by

i

documented instructions, procedures, or drawings of a

type appropriate to the circumstances and shall be

accomplished in accordance with these instructions,

procedures, or drawings."

1.

Periodic Instrument and Control Test (PICT)-5-2, " Steam Generator

Level, Protection Set II," Revision 12, approved August 26, 1988,

requires, in part, the use of multiple photocells associated with

the comparator logic tester and the use of a simulated test signal

!

'

initially set at five volts, decreased to one volt while recording

applicable bistable actions, and then increased while recording

applicable bistable actions.

I

Contrary to the above, on February 2,1989, test personnel performed

the test in a manner inconsistent with the procedure, in that only

one photocell associated with the comparator logic tester was used

and the simulated test signal was ramped down and up in a staggered

fashion to obtain data for each bistable action until the signal was

decreased to one volt.

1his is a Severity Level V violation (Supplement I).

2.

Licensee Quality Inspection Procedure (QIP) IS, "QI observations of

I&C Calibration Activities," Revision 0, approved January 4, 1989,

specifies in part, that the quality control inspector shall note

Whether work -was Performed in accordance .with spps _d instzw+ 4 ans,

.

procedures, and/or technical manuals to assure that Plant proce-

dures, work package instructions, and installation standards are

followed.

Contrary to the above, on February 2, 1989, a quality control

inspector failed to note and document failures to follow approved

procedures during the performance of channel functional testing of

steam generator water level instrumentation per licensee procedure

PICT-5-2.

This is a Severity Level IV violation (Supplement I).

3.

Licensee Plant Safety Procedure (PS) 3-30. Revision 17,Section IV

Item E. states:

"It is the responsibility of the person accepting

the equipment clearance to check the equipment clearance and assure

himself that the equipment is satisfactorily tagged and the equip-

ment is deenergized and cleared fnr work before starting work."

Further, licensee procedure Administrative Order (AO) 3-9,

_ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - - _ -

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Trajhn Nucicar P1hnt.

Dscument Control D3Ek

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Attachment

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License NPF-1

April'14, 1989

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Page 4.of 7

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Revision 26, Section.I. Item 4. states: "The assigned craftsman /

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technician performs the maintenance prescribed by the MR work

'

instructions and documents itsl completion in the work performed

section of the MR."

Contrary to the above, on February 12,-1988, a Maintenance craftsman

replaced;the charcoal'adsorber in the "B" Train of.the containment

Hydrogen Vent System that was not tagged out or cleared for work,

and failed to replace the charcos1 adsorber of'the

"A" Containment

Hydrogen Vent System specified in KR werk instructions.

This is a Severity Level IV violation (Supplement I).

REPLY TO VIOLATION B.1

PGE acknowledges the violation.

1. . Reason for: the Violation:

The reason for this violation is personnel error. Personnel failed

to follow the procedure exactly as written, and assumed that actions

.

that were technically equivalent to the steps in the procedure could

be' substituted without making a procedure revision or deviation.

Subsequent review found that the problem of not connecting the

comparator photocell to the light specified in the procedure was

common to other procedures.

In addition, the practice of raising.

and lowering the test signal When all photocells were not operable

was a common past practice.

J.

Corzwet.ive<. steps 2aken 6Jiasult.s Aahad:

All PICTs were reviewed to determine where a similar problem

existed. A procedure deviation was made to all applicable proce-

dures to correct the photocell location and to permit the test

signal to either ramp continuously up and down, or to be stepped.at'

the discretion of the technician performing the test. This action

was completed on February 27, 1989.

Management expectations for limitations on procedure flexibill,ty

were discussed with Maintenance electrical and instrumentation and

control (I&C) personnel and their supervisors. Personac1 were

advised that technical or electrical equivalency is not sufficient

justification for not following the procedure as written.

If an

equivalent method is to be used, the procedure or work instruction

must be changed to reflect it.

This was also discussed with

temporary Maintenance employees that are being used for the

,

1989 outage.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _

_

_ _ _ _ - _ - -

_.

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Trhjcn Nuclocr Pirnt

  • * *

Document Control Desk

-, i Dockbt 50-344

'

Attachment

License NPF-1

April 14, 1989-

,

Page 5 of 7

3.

Corrective Steps That Will Be Taken to Avoid Further Violations:

The lessons learned from this event will be incorporated into the

Periodic Maintenance Retraining Program. This will be completed

before the next session scheduled to begin in September 1989.

4.

Date We Full Compliance Will Be Achieved:

o

Full compliance has been achieved.

.

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-______-

_ _ _ _ __ ____ _ _ ___-__ _ _ - __

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Trojcn Nuclocr PICnt

D cument Contr31 De:k

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Docket 50-344

Attachment

-

.

License NPF-1

April 14, 1989

page 6 of 7

REPLY TO VIOLATION B.2

PGE acknowledges the violation.

1.

Reason for the Violation:

The reason for this violation is personnel error. The quality

control inspector failed to recognize the procedural noncompliance

because he had not adequately reviewed the PICT-5-2 procedure ahead

of time and did not have a copy of the procedure with him while

observing the channel functional testing. The inspector was

notified of his assignment to perform the observation only a few

minutes before the testing was to begin.

2.

Corrective Steps Taken and Results Achieved:

Management expectations of the role of quality control inspec-

a.

tions in verifying procedural compliance were discussed with all

inspectors.

It was emphasized that verification of procedural

compliance requires that the inspector be familiar with the

procedure and have a copy with him during the observation.

Subsequent PICT observations performed by quality control

inspectors have been observed by management to enmare that

expectations are implemented,

b.

Scheduling of PICT observations has been improved.

Inspectors

are now assigned to specific PICT observations well in advance,

allowing adequate preparation time.

3.

Corrective Steps That Will Be Taken to Avoid Further Violations:

me 41ectrical quality control inspectors-will Participate in :the

classroom training sessions of the I&C technician quarterly

training program to improve the inspectors' knowledge of I&C

activities. Participation in this training is scheduled to

begin in September 1989.

b,

All electrical quality control inspectors will attend formal

observation training by August 1, 1989.

4.

Date When Full Compliance Will Be Achieved:

Full compliance has been achieved.

_ - _ _ _ _ _ - _ _ _ _ - _ _ _

_ - - _ _ -

_

. _ _ _ _ _ - - -

,

.

'

Trajtn Wuclcrr plcnt

Document Contesl De:k

.

'

. . Dr.cket 50-344

Attachment

License NPF-1

April 14, 1989

.

Page 7 of 7

REPLY TO VIOLATION B.3

PGE acknowledges the violation.

1.

Reason for the Violation:

The reason for this violation is personnel error. The replacement

of the charcoal adsorber for the

"A" Containment Hydrogen Vent

System was to have been performed under a clearance accepted by the

system engineer. The system engineer had verified that the equip-

ment was tagged, deenergized, and cleared for work. However,

miscommunication between the system engineer and the maintenance

craftsman resulted in the craftsman replacing the "B" charcoal

adsorber.

In addition, the craftsman did not have a copy of the

Maintenance Request (MR) with him when performing the work, and

relied solely on verbal instructions from the system engineer.

2.

Corrective Steps Taken and Results Achieved:

a.

Upon discovery on February 23, 1988 that the "B" charcoal

adsorber had been replaced, the

"B" Containment Hydrogen Vent

System was placed in an inoperable status. On July 1, 1988,

during the annual refueling outage, the required operability

testing was performed on the

"B" charcoal adsorber with

satisfactory results. The system was returned to operable

status.

b.

The craftsman received additional instruction on the need to

carefully read and follow instructions when performing work

under an MR.

The engineer received additional training on the

~

' necessity.cf being certain that verbal or written J.nstzw+ 4-

.

-3re c.ltar, templete and, Where requittni, .nference irpecific

component identification numbers.

c.

Maintenance personnel have received training on AD 3-9,

" Maintenance Requests," specifically relating to verbal instruc-

tions.

Emphasis was placed on properly documenting verbal

instructions.

d.

Maintenance personnel are now required to have a " field copy" of

the MR at the worksite to assure that the procedures are

,

)

followed and there is no confusion as to the instructions,

procedures or intent of the MR.

3.

Corrective Steps That Will Be Taken to Avoid Further Violations:

All corrective steps have been completed.

4.

Date When Full Compliance Will Be Achieved:

,

1

Full compliance has been achieved.

DLN/mr/3008W.0489

1

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