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BomTAN EDISON COMPANY orwenac arricco son savtefou starry SoSfoN MAasACHug TTE03199 A. V. M O RISI l
BomTAN EDISON COMPANY orwenac arricco son savtefou starry SoSfoN MAasACHug TTE03199 A. V. M O RISI                                                                                       l MANAGER f
MANAGER f
NUCLEAR OPERATIONS SUPPORT DEFh4TMENT October 7,1982 BECo. Ltr. #82-266             ,
NUCLEAR OPERATIONS SUPPORT DEFh4TMENT October 7,1982 BECo. Ltr. #82-266 l
l Mr. Ronald C. Haynes, Director                                                                                   !
Mr. Ronald C. Haynes, Director Office of Inspection and Enforcement Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA.
Office of Inspection and Enforcement                                                                             !
19406 License No. DPR-35 Docket No. 50-293
Region I U.S. Nuclear Regulatory Commission 631 Park Avenue                                                                                                 '
King of Prussia, PA.         19406 License No. DPR-35 Docket No. 50-293


==Subject:==
==Subject:==
Line 30: Line 28:


==Dear Sir:==
==Dear Sir:==
In.the second response contained in Reference (A), Bo-ton Edison committed to                                   i complete IE Bulletin 80-06 related surveillance testing prior to start-up from Refueling Outage #5 (RF0 5). At start-up from RF0 5 we believed this commit-ment had been fully satisfied.
i In.the second response contained in Reference (A), Bo-ton Edison committed to complete IE Bulletin 80-06 related surveillance testing prior to start-up from Refueling Outage #5 (RF0 5). At start-up from RF0 5 we believed this commit-ment had been fully satisfied.
However, after Pilgrim returned to service an additional review was conducted                                   i to ensure the adecuacy and completeness of the Bulletin 80-06 tests. This re-view determined that a modified station surveillance procedure, Temporary                                       l Proced_ure 81-64, PCIS Valve Testing (TP81-64) had the following inadequacies:
However, after Pilgrim returned to service an additional review was conducted i
;        (1) it inadvertantly overlooked the testing of the H2 Analyzer Isolation Valves; l       (2) it did not identify the individual Standby Gas Treatment System Isolation
to ensure the adecuacy and completeness of the Bulletin 80-06 tests. This re-view determined that a modified station surveillance procedure, Temporary l
(       Valves; (3) it incorrectly indicated that the 02 Analyzer Valves are closed after                                 i reset, when the valves are actually open.                                                                       ,
Proced_ure 81-64, PCIS Valve Testing (TP81-64) had the following inadequacies:
To correct the identified inadequacies, the Operations Review Comittee approved two new temporary procedures, TP82-38, Balance of Plant isolation "A" and TP82-39,                               (
(1) it inadvertantly overlooked the testing of the H2 Analyzer Isolation Valves; l
      . Balance of Plant Isolation "B" . During the unscheduled shutdown commencing August
(2) it did not identify the individual Standby Gas Treatment System Isolation
!      13, 1982, th ! additional testing was conducted. This cesting revealed that wiring                               '
(
l      to the H2 Analyzer valves was incorrect. We developed and' implemented corrective                               :
Valves; (3) it incorrectly indicated that the 02 Analyzer Valves are closed after i
i      actions, developed appropriate new test procedures and conducted a test of the logic.
reset, when the valves are actually open.
The logic tested consistent with its wiring schemes, satisfactorily concluding this
To correct the identified inadequacies, the Operations Review Comittee approved two new temporary procedures, TP82-38, Balance of Plant isolation "A" and TP82-39,
                                              ~
(
t L
Balance of Plant Isolation "B". During the unscheduled shutdown commencing August 13, 1982, th ! additional testing was conducted.
!      test. LER 82-025/01T-0 has been issued to satisfy reporting requirements.                                        .
This cesting revealed that wiring l
I 0        3
to the H2 Analyzer valves was incorrect. We developed and' implemented corrective i
        '  82101{0{21 PDR A O               pnR         >
actions, developed appropriate new test procedures and conducted a test of the logic.
G                                                                                                    ,II
L The logic tested consistent with its wiring schemes, satisfactorily concluding this
                                                                                                                \'
~
t test.
LER 82-025/01T-0 has been issued to satisfy reporting requirements.
I 82101{0{21 PDR A O 0
3 pnR G
,II
\\'


BDCTON EOCON COMPANY Mr. Ronald C. Haynes, Director October _7, 1982 Page 2 We believe the actions contained in this submittal satisfactorily address the issue; should you wish further information after reviewing it, please contact us.
BDCTON EOCON COMPANY Mr. Ronald C. Haynes, Director October _7, 1982 Page 2 We believe the actions contained in this submittal satisfactorily address the issue; should you wish further information after reviewing it, please contact us.
Very truly yours, l
Very truly yours, I
l I}}
.}}

Latest revision as of 19:28, 16 December 2024

Completes Response to IE Bulletin 30-06, ESF Reset Controls. Review of Actions Taken in Compliance W/Bulletin Revealed Deficiencies in Temporary Procedure 81-6A Re Valve Testing.New Test Procedures Developed
ML20065L796
Person / Time
Site: Pilgrim
Issue date: 10/07/1982
From: Morisi A
BOSTON EDISON CO.
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
REF-SSINS-6820 82-266, IEB-80-06, IEB-80-6, NUDOCS 8210190721
Download: ML20065L796 (2)


Text

wr 9.

BomTAN EDISON COMPANY orwenac arricco son savtefou starry SoSfoN MAasACHug TTE03199 A. V. M O RISI l

MANAGER f

NUCLEAR OPERATIONS SUPPORT DEFh4TMENT October 7,1982 BECo. Ltr. #82-266 l

Mr. Ronald C. Haynes, Director Office of Inspection and Enforcement Region I U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prussia, PA.

19406 License No. DPR-35 Docket No. 50-293

Subject:

IE Bulletin 80-06 Reference (A). Boston Edison Letter dated June 27, 1980 from Mr. G. Carl Andognini to Mr. Boyce H. Grier (B): LER 82-025/01T-0

Dear Sir:

i In.the second response contained in Reference (A), Bo-ton Edison committed to complete IE Bulletin 80-06 related surveillance testing prior to start-up from Refueling Outage #5 (RF0 5). At start-up from RF0 5 we believed this commit-ment had been fully satisfied.

However, after Pilgrim returned to service an additional review was conducted i

to ensure the adecuacy and completeness of the Bulletin 80-06 tests. This re-view determined that a modified station surveillance procedure, Temporary l

Proced_ure 81-64, PCIS Valve Testing (TP81-64) had the following inadequacies:

(1) it inadvertantly overlooked the testing of the H2 Analyzer Isolation Valves; l

(2) it did not identify the individual Standby Gas Treatment System Isolation

(

Valves; (3) it incorrectly indicated that the 02 Analyzer Valves are closed after i

reset, when the valves are actually open.

To correct the identified inadequacies, the Operations Review Comittee approved two new temporary procedures, TP82-38, Balance of Plant isolation "A" and TP82-39,

(

Balance of Plant Isolation "B". During the unscheduled shutdown commencing August 13, 1982, th ! additional testing was conducted.

This cesting revealed that wiring l

to the H2 Analyzer valves was incorrect. We developed and' implemented corrective i

actions, developed appropriate new test procedures and conducted a test of the logic.

L The logic tested consistent with its wiring schemes, satisfactorily concluding this

~

t test.

LER 82-025/01T-0 has been issued to satisfy reporting requirements.

I 82101{0{21 PDR A O 0

3 pnR G

,II

\\'

BDCTON EOCON COMPANY Mr. Ronald C. Haynes, Director October _7, 1982 Page 2 We believe the actions contained in this submittal satisfactorily address the issue; should you wish further information after reviewing it, please contact us.

Very truly yours, I

.