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{{Adams
#REDIRECT [[05000311/LER-1981-059, Forwards LER 81-059/03L-0.Detailed Event Analysis Encl]]
| number = ML20010B897
| issue date = 08/07/1981
| title = Forwards LER 81-059/03L-0.Detailed Event Analysis Encl
| author name = Uderitz R
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name = Grier B
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000311
| license number =
| contact person =
| document report number = NUDOCS 8108180446
| package number = ML20010B898
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| page count = 3
}}
 
=Text=
{{#Wiki_filter:(_
1 LER
          ~
O PSEG Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 August 7, 1981 co      O)
                                                                                        <    ,        A Mr. Boyce H. Grier                                                        9-        I-Director of USNRc                                                        2      AUG 171981 m                      1 Office of Inspectioa and Enforcement                                      {g            ,,      p                l Region 1                                                                            spavasue 631 Park Avenue King of Prussia, Pennsylvania                    19406                        4                /
 
==Dear Mr. Grier:==
 
G3 h'
LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-59/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 81-59/03L. This report is required within thirty (30) days of the occurrence.
Sincerely yours, M/ MY                                                    :
R. A. Uderitz General Manager -
Nucle;r Production
,        CC:    Director, Office of Inspection
!                  and Enforcement (30 copies)
Director, Office of Management Information and Program Control (3 copies)
: 5. ''1 8103100446 810807" PDR ADOCK 05000311 S                  PDR The Energy People 95 2001 (4W4181
 
I                                          .
Rep 6rt Number:    81-59/03L                                ,
Report Date:      August 7, 1981 Occurrence Date:  7-9-81 Facility:          Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey                08038 IDENTIFICATION OF OCCURRENCE:
Pressurizer Overpressure Protection System Channel 2 - Inoperable.
This report was initiated by Incident Report 81-242.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 4 - Rx Power 0% - Unit Load 0 MWe DESCRIPTION OF OCCURRENCE:
During cooldown on July 9, 1981, the Pressurizer Overpressure Protec-tion System (POPS) . channel 2 was declared inoperable due to previous closure of isolation valve 2PR7 because of known leak through on the pressurizer power operated relief valve (PORV) 2PR2. Action statement 3.4.10.3.a was entered when Reactor Coolant System (RCS) temperature decreased to 312*F at 1957 hours, July 9, 1981.
This occurrence constituted operation in a degraded mode in accordance with technical specification 6.9.1.9.b.
DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:
1 PORV 2PR2 was previously identified to be leaking through, and was isolated by closing 2PR7. When RCS temperature was decreased to 312*F, POPS channel 2 was declared inoperable because it was isolated.
ANALYSIS OF OCCURRENCE:
Technical Specification 3.4.10.3.a requires:
With one POPS inoperable, restore the inoperable POPS to operable status within 7 days or depressurize and vent the RCS through a 3.14 square inch. vent within the next 8 hours.
CORRECTIVE ACTION:
At 0715, July 12, 1981, Unit 2 was raised above 312*F, terminating action statement 3.4.10.3.a. Action statement 3.4.5.a was entered immediately because 2PR7 was closed and the power removed.
Valve 2PR2 will be repaired and tested during the next refueling outage.
A supplemental report will be submitted at that time.
: 5.          -
l                      LER 81-59/03L                                                              8/7/8' '
1                            -
FAILURE DATA:
Valve 2PR2 Copes-Vulcan 1
i' j                      Prepared By      F. Dickey                        ,
04-c, -
j                                                    ManagMr - Salem Ge6erating Station SORC Meeting No.      81-71
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Latest revision as of 07:11, 21 December 2024