ML061430229: Difference between revisions

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{{Adams
#REDIRECT [[PNO-III-06-014, Kewaunee, Procedure Adherence Problems During Reactor Startup]]
| number = ML061430229
| issue date = 05/23/2006
| title = PNO-III-06-014, Kewaunee, Procedure Adherence Problems During Reactor Startup
| author name = Peterson H
| author affiliation = NRC/RGN-III
| addressee name =
| addressee affiliation =
| docket = 05000305
| license number = DPR-043
| contact person =
| document report number = PNO-III-06-014
| document type = NRC Preliminary Notification of Event/Occurrence
| page count = 1
}}
 
=Text=
{{#Wiki_filter:May 23, 2006PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-III-06-014This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or publicinterest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date. FacilityKewauneeDominion Energy Kewaunee, Inc.
City, State: Kewaunee, WI Docket:  50-305 License:  DPR-43Licensee Emergency Classification Notification of Unusual Event Alert      Site Area Emergency General Emergency X  Not Applicable               
 
==SUBJECT:==
PROCEDURE ADHERENCE PROBLEMS DURING REACTOR STARTUPDESCRIPTION:
On May 17, 2006, an operating crew at Kewaunee experienced procedure implementationissues while performing reactor startup activities to take the reactor critical following the unplanned maintenance outage that began on April 26, 2006. Information on the unplannedmaintenance outage was provided in PNO-III-06-012 and PNO-III-06-012A. The licensee determined that the operating crew performed the startup procedural steps out ofsequence; however, no safety limits were exceeded and therefore the startup activity was continued. Subsequently, on the evening of May 17, 2006, the licensee had to shutdown thereactor due to equipment problems on the main turbine turning gear. The licensee initiated an event review team to determine the cause of the procedure implementation problem and todetermine corrective actions.An NRC Special Inspection Team reviewed the circumstances surrounding the event and thelicensee's evaluation of the cause. The licensee's post event actions, including operator remediation, procedure reviews and revisions, additional training of operators prior to startup, and additional oversight by management during reactor startup activities, were determined to be adequate by the NRC team. The results of the NRC's special inspection will be issued in aninspection report in about 45 days. The licensee adequately performed startup activities and made the reactor critical at 9:26 pm(CDT) May 22, 2006. The NRC resident inspectors were in the control room observing operatoractions throughout the startup.The State of Wisconsin will be informed. The information in this preliminary notification hasbeen reviewed with licensee management.This information is current as of 8:00 a.m. (CDT) on May 23, 2006.
CONTACT:Hironori Peterson630/829-9707}}

Latest revision as of 08:22, 18 September 2019