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{{#Wiki_filter:Exeton Generation, TRM 3.3.7.2LG-14-031 February 26, 2014U.S. Nuclear Regulatory Commission Attn.: Document Control DeskWashington, DC 20555-0001 Limerick Generating
: Station, Units 1 and 2Facility Operating License Nos. NPF-39 and NPF-85NRC Docket Nos. 50-352 and 50-353
==Subject:==
Special Report -Seismic Monitoring Instrumentation Inoperability Channel XE-VA-102
==References:==
: 1. Special Report- Seismic Monitoring Instrumentation Inoperability, dated 01/16/13This Special Report is being submitted pursuant to the requirements of Limerick Generating Station (LGS), Unit 1 and Unit 2 Updated Final Safety Analysis Report (UFSAR) section3.7.4.5, Technical Specification 6.9.2, and Technical Requirements Manual 3.3.7.2 whichstates '"With one or more of the seismic monitoring instruments inoperable for more than 30days, a Special Report shall be prepared and submitted to the Nuclear Regulatory Commission pursuant to Specification 6.9.2 of the Technical Specifications within the next tendays outlining the cause of the malfunction and the plans for restoring the instrument(s) tooperable status."On Friday January 17, 2014 Unit 1 and 2 were operating at 100% power with functional testing (ST-2-036-426-0) of the seismic monitoring instrumentation in progress.
During thetest, the seismic monitor sensor array (XE-VA-1
: 02) for the Primary Containment Foundation Sensor did not provide the Main Control Room (MCR) alarm or the local indicating light.The XE-VA-102 array has three channels which measure longitudinal
: movement, verticalmovement, and transverse movement.
The transverse channel of XE-VA-1 02 will trigger XR-VA-102/103 to log/record data, but will not actuate the MCR alarm or the light as expected.
Accordingly, Operations declared the recorder inoperable.
The other two XE-VA-1 02channels for the horizontal and vertical directions function and will trigger, log/record data andprovide the MCR alarm and the local indicating light.Initial troubleshooting has not determined the cause. Additional troubleshooting will berequired to identify the cause of the inoperable sensor XE-VA-1 02 and recorder XR-VA-102/103 for XE-VA-1 02. The sensor and recorder will be repaired, tested, and returned tooperable status by the end of 1 R15 refueling outage (April 2014).
If you have any questions or require additional information, please do not hesitate to contactus.Sincwerelly,
...."Thomas J. Dougherty Vice President
-Limerick Generating StationExelon Generation
: Company, LLC
==Attachment:==
List of commitments cc: Administrator, Region I, NRCNRC Senior Resident Inspector, Limerick SUMMARY OF REGULATORY COMMITMENTS The following table identifies commitments made in this document.
(Any other actionsdiscussed In the submittal represent intended or planned actions.
They are described tothe NRC for the NRC's information and are not regulatory commitments.)
COMMITTED COMMITMENT TYPECOMMITMENT DATE OR"OUTAGE ONE-TIME PROGRAMMATIC ACTION (Yes/No)(Yes/No)The inoperable seismicmonitor sensor array (XE-VA- Outage Yes No102) that is located in the Unit1 HPCI Room will berepaired, tested, and returnedto operable status by the endof the 1 R15 refueling outage(April 2014).The inoperable seismicmonitor recorder XR-VA- Outage Yes No102/103 for XE-VE-1 02 will berepaired, tested, and returnedto operable status by the endof the 1 R15 refueling outage(April 2014).}}

Revision as of 08:52, 2 July 2018

Limerick Generating Station, Units 1 and 2 - Special Report - Seismic Monitoring Instrumentation Inoperability Channel XE-VA- 102
ML14069A171
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 02/26/2014
From: Dougherty T J
Exelon Generation Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LG-14-031
Download: ML14069A171 (3)


Text

Exeton Generation, TRM 3.3.7.2LG-14-031 February 26, 2014U.S. Nuclear Regulatory Commission Attn.: Document Control DeskWashington, DC 20555-0001 Limerick Generating

Station, Units 1 and 2Facility Operating License Nos. NPF-39 and NPF-85NRC Docket Nos. 50-352 and 50-353

Subject:

Special Report -Seismic Monitoring Instrumentation Inoperability Channel XE-VA-102

References:

1. Special Report- Seismic Monitoring Instrumentation Inoperability, dated 01/16/13This Special Report is being submitted pursuant to the requirements of Limerick Generating Station (LGS), Unit 1 and Unit 2 Updated Final Safety Analysis Report (UFSAR) section3.7.4.5, Technical Specification 6.9.2, and Technical Requirements Manual 3.3.7.2 whichstates '"With one or more of the seismic monitoring instruments inoperable for more than 30days, a Special Report shall be prepared and submitted to the Nuclear Regulatory Commission pursuant to Specification 6.9.2 of the Technical Specifications within the next tendays outlining the cause of the malfunction and the plans for restoring the instrument(s) tooperable status."On Friday January 17, 2014 Unit 1 and 2 were operating at 100% power with functional testing (ST-2-036-426-0) of the seismic monitoring instrumentation in progress.

During thetest, the seismic monitor sensor array (XE-VA-1

02) for the Primary Containment Foundation Sensor did not provide the Main Control Room (MCR) alarm or the local indicating light.The XE-VA-102 array has three channels which measure longitudinal
movement, verticalmovement, and transverse movement.

The transverse channel of XE-VA-1 02 will trigger XR-VA-102/103 to log/record data, but will not actuate the MCR alarm or the light as expected.

Accordingly, Operations declared the recorder inoperable.

The other two XE-VA-1 02channels for the horizontal and vertical directions function and will trigger, log/record data andprovide the MCR alarm and the local indicating light.Initial troubleshooting has not determined the cause. Additional troubleshooting will berequired to identify the cause of the inoperable sensor XE-VA-1 02 and recorder XR-VA-102/103 for XE-VA-1 02. The sensor and recorder will be repaired, tested, and returned tooperable status by the end of 1 R15 refueling outage (April 2014).

If you have any questions or require additional information, please do not hesitate to contactus.Sincwerelly,

...."Thomas J. Dougherty Vice President

-Limerick Generating StationExelon Generation

Company, LLC

Attachment:

List of commitments cc: Administrator, Region I, NRCNRC Senior Resident Inspector, Limerick SUMMARY OF REGULATORY COMMITMENTS The following table identifies commitments made in this document.

(Any other actionsdiscussed In the submittal represent intended or planned actions.

They are described tothe NRC for the NRC's information and are not regulatory commitments.)

COMMITTED COMMITMENT TYPECOMMITMENT DATE OR"OUTAGE ONE-TIME PROGRAMMATIC ACTION (Yes/No)(Yes/No)The inoperable seismicmonitor sensor array (XE-VA- Outage Yes No102) that is located in the Unit1 HPCI Room will berepaired, tested, and returnedto operable status by the endof the 1 R15 refueling outage(April 2014).The inoperable seismicmonitor recorder XR-VA- Outage Yes No102/103 for XE-VE-1 02 will berepaired, tested, and returnedto operable status by the endof the 1 R15 refueling outage(April 2014).