ML17303B053: Difference between revisions

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| contact person =  
| contact person =  
| document report number = 192-00367-JGH-T, 192-367-JGH-T, 3-SR-88-002, 3-SR-88-2, NUDOCS 8804210329
| document report number = 192-00367-JGH-T, 192-367-JGH-T, 3-SR-88-002, 3-SR-88-2, NUDOCS 8804210329
| document type = REPORTABLE OCCURRENCE REPORT (SEE ALSO AO,LER), TEXT-SAFETY REPORT
| document type = REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER), TEXT-SAFETY REPORT
| page count = 6
| page count = 6
}}
}}


=Text=
=Text=
{{#Wiki_filter:j                                   I
{{#Wiki_filter:j I
      'gCELERATED           DISOIBUTION         DEMONSTRION                           SYSTEM P
P 'gCELERATED DISOIBUTION DEMONSTRION SYSTEM
,'l.
,'l.
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8804210329     DOC.DATE: 88/04/18   NOTARIZED: NO                     DOCKET FACIL:STN-50-530 Palo Verde Nuclear Station,     Unit 3, Arizona Publi 05000530 AUTH. NAME         AUTHOR AFFILIATION HAYNES,J.G.       Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME         RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
ACCESSION NBR:8804210329 DOC.DATE: 88/04/18 NOTARIZED: NO DOCKET FACIL:STN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530 AUTH.NAME AUTHOR AFFILIATION HAYNES,J.G.
Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Special Rept 3-SR-88-002:on 880328,radiation monitoring unit inoperable for greater than 72 h.
Special Rept 3-SR-88-002:on 880328,radiation monitoring unit inoperable for greater than 72 h.
SIZE:
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR I
DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR I ENCL P
ENCL P SIZE:
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.
D NOTES:Standardized plant.                                                             05000530 S
NOTES:Standardized plant.
RECIPIENT       COPIES          RECIPIENT                      COPIES 1'
RECIPIENT ID CODE/NAME PD5 LA LICITRA,E INTERNAL ACRS MICHELSON AEOD/DOA AEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 RGN5 FILE 01 EXTERNAL: EG&G GROH,M H ST LOBBY WARD NRC PDR NSIC MAYS,G NOTES:
ID CODE/NAME     LTTR ENCL      ID  CODE/NAME                  LTTR ENCL PD5 LA             .1    1, 1'    PD5 PD                            1    1 LICITRA,E           1          DAVIS,M                            1    1 INTERNAL ACRS MICHELSON               1    ACRS MOELLER                      2    2 AEOD/DOA             1    1    AEOD/DSP/NAS                      1    1 AEOD/DS P/ROAB       2    2    AEOD/DSP/TPAB                      1    1 ARM/DCTS/DAB         1    1    DEDRO                              1    1 NRR/DEST/ADS   7E   1    0    NRR/DEST/CEB 8H                    1    1 NRR/DEST/ESB  8D   1    1    NRR/DEST/ICSB 7                    1    1 NRR/DEST/MEB  9H    1    1    NRR/DEST/MTB 9H                    1   1 NRR/DEST/PSB  8D    1    1    NRR/DEST/RSB 8E                    1,  1 NRR/DEST/SGB  8D    1    1    NRR/DLPQ/HFB 10                    1    1 NRR/DLPQ/QAB  10   1    1    NRR/DOEA/EAB 11                   1    1 NRR/DREP/RAB  10    1    1    NRR/DREP/RPB 10                   2    2 1    1                      'RR/PMAS/ILRB12 1    1 1    1    RES TELFORD,J                     1    1 1    1    RES/DRPS   DIR                     1    1 RGN5    FILE  01    1    1 EXTERNAL: EG&G GROH,M            4    4    FORD BLDG HOY,A                   1   1 H ST LOBBY WARD      1     1     LPDR                              1   1 NRC PDR              1     1     NSIC HARRIS,J                      1   1 NSIC MAYS,G          1     1 NOTES:                            1   1 D
COPIES LTTR ENCL
S j
.1 1,
A TOTAL NUMBER OF COPIES REQUIRED: LTTR     47   ENCL   46
1 1'
1 1
1 2
2 1
1 1
0 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 4
4 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD5 PD DAVIS,M ACRS MOELLER AEOD/DSP/NAS AEOD/DSP/TPAB DEDRO NRR/DEST/CEB 8H NRR/DEST/ICSB 7
NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10
'RR/PMAS/ILRB12 RES TELFORD,J RES/DRPS DIR FORD BLDG HOY,A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1
1 1
1 2
2 1
1 1
1 1
1 1
1 1
1 1
1 1,
1 1
1 1
1 2
2 1
1 1
1 1
1 1
1 1
1 1
1 D
05000530 S
1' D
Sj A
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 47 ENCL 46


Arizona Nuclear Power Project P.O. BOX 52034 ~ PHOENIX. ARIZONA 85072-2034 192-00367-JGH/TDS/DAJ April 18, 1988 U. S. Nuclear   Regulatory Commission NRC Documen'ontrol     Desk Washington, D.C.     20555
Arizona Nuclear Power Project P.O. BOX 52034
 
~
==Dear  Sirs:==
PHOENIX. ARIZONA85072-2034 192-00367-JGH/TDS/DAJ April 18, 1988 U. S. Nuclear Regulatory Commission NRC Documen'ontrol Desk Washington, D.C.
20555


==Dear Sirs:==
==Subject:==
==Subject:==
Palo Verde Nuclear Generating Station (PVNGS)
Palo Verde Nuclear Generating Station (PVNGS)
Unit   3 Docket No. STN 50-530 (License No. NPF-74)
Unit 3 Docket No.
Special Report 3-SR-88-002 File: 88-020-404 Attached please find Special Report 3-SR-88-002 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2. This report discusses a radiation monitoring unit inoperable for greater than 72 hours.
STN 50-530 (License No. NPF-74)
If you have any questions,       please contact T. D. Shriver, Compliance Manager at (602) 393-2521.
Special Report 3-SR-88-002 File:
Very   trul yours, J. G. Hay<(es Vice President Nuclear Production JGH/TDS/DAJ/kj Attachment cc:   0. M. DeMichele           (all   w/a)
88-020-404 Attached please find Special Report 3-SR-88-002 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2.
E. E. Van Brunt,     Jr.
This report discusses a radiation monitoring unit inoperable for greater than 72 hours.
J. B. Martin T. J. Po 1 i ch E. A. Licitra A. C. Gehr INPO   Records Center
If you have any questions, please contact T.
                                                                                  ~pg.'Z
D. Shriver, Compliance Manager at (602) 393-2521.
                                                                                      ] )
Very trul
8804210329 880418 PDR   ADOCK 05000530 S                     DCD
: yours, JGH/TDS/DAJ/kj Attachment cc:
0.
M. DeMichele (all w/a)
E.
E.
Van Brunt, Jr.
J.
B. Martin T. J.
Po 1 ich E.
A. Licitra A. C. Gehr INPO Records Center J.
G.
Hay<(es Vice President Nuclear Production
~pg.'Z
] )
8804210329 880418 PDR ADOCK 05000530 S
DCD


ALO VERDE NUCLEAR GENERATING S     ION Radiation Monitoring Unit Inoperable for Greater Than 72 Hours License No. NPF-74 Docket No. STN 50-530 Special Report No. 3-SR-88-002 This Special Report is being submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2 to report an event in which a Radioactive Gaseous Effluent Monitor (Fuel Building Ventilation System High Range Monitor RU-146) was inoperable for greater than 72 hours. The 72 hour limit for returning the monitor to operability was exceeded at approximately 0100 MST on March 31, 1988. Pursuant to Technical Specification 3.3.3.8 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Fuel Building Ventilation System when needed.
ALO VERDE NUCLEAR GENERATING S ION Radiation Monitoring Unit Inoperable for Greater Than 72 Hours License No. NPF-74 Docket No.
At 0100 MST on March 28, 1988, Palo Verde Unit 3 was in Mode 1 (POWER OPERATION) when the. Fuel Building Ventilation System High Range Monitor RU-146 was declared inoperable due to unsatisfactory performance of the source check while performing surveillance test 75ST-9ZZ08 (Effluent Monitor Monthly Source Check).
STN 50-530 Special Report No. 3-SR-88-002 This Special Report is being submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2 to report an event in which a Radioactive Gaseous Effluent Monitor (Fuel Building Ventilation System High Range Monitor RU-146) was inoperable for greater than 72 hours.
An authorized work document was issued to troubleshoot/rework/replace components to correct the cause of the monitor not passing the check source surveillance on channel 2. During troubleshooting a Detector High Voltage Failure alarm and a Detector Failure alarm were received. The high voltage was found to be approximately 2.5 times greater than the normal value. The high voltage board was replaced with a replacement high voltage board and the voltage adjusted to a normal value. The detector is believed to have failed
The 72 hour limit for returning the monitor to operability was exceeded at approximately 0100 MST on March 31, 1988.
'due to the excessive high voltage from the faulty high voltage board. The detector was replaced with a new detector and surveillance test 36ST-9Sgll (RU-145/RU-146 Calibration Test) was satisfactorily performed on RU-146 channel 2. An Engineering Evaluation Request has been submitted to perform a root cause of failure analysis on the malfunctioning components.
Pursuant to Technical Specification 3.3.3.8 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Fuel Building Ventilation System when needed.
After satisfactory completion of appropriate surveillance tests RU-146 was declared operable at 1357 MST on April 1, 1988. The monitor was out of service for'approximately   4 days and 13 hours.}}
At 0100 MST on March 28,
: 1988, Palo Verde Unit 3 was in Mode 1
(POWER OPERATION) when the. Fuel Building Ventilation System High Range Monitor RU-146 was declared inoperable due to unsatisfactory performance of the source check while performing surveillance test 75ST-9ZZ08 (Effluent Monitor Monthly Source Check).
An authorized work document was issued to troubleshoot/rework/replace components to correct the cause of the monitor not passing the check source surveillance on channel 2.
During troubleshooting a Detector High Voltage Failure alarm and a Detector Failure alarm were received.
The high voltage was found to be approximately 2.5 times greater than the normal value.
The high voltage board was replaced with a replacement high voltage board and the voltage adjusted to a normal value.
The detector is believed to have failed
'due to the excessive high voltage from the faulty high voltage board.
The detector was replaced with a new detector and surveillance test 36ST-9Sgll (RU-145/RU-146 Calibration Test) was satisfactorily performed on RU-146 channel 2.
An Engineering Evaluation Request has been submitted to perform a
root cause of failure analysis on the malfunctioning components.
After satisfactory completion of appropriate surveillance tests RU-146 was declared operable at 1357 MST on April 1, 1988.
The monitor was out of service for'approximately 4 days and 13 hours.}}

Latest revision as of 02:55, 8 January 2025

Special Rept 3-SR-88-002:on 880328,radiation Monitoring Unit Inoperable for Greater than 72 H Due to Unsatisfactory Performance of Source Check.Caused by Excessive High Voltage from Faulty High Voltage Board.Detector Replaced
ML17303B053
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 04/18/1988
From: Haynes J
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
192-00367-JGH-T, 192-367-JGH-T, 3-SR-88-002, 3-SR-88-2, NUDOCS 8804210329
Download: ML17303B053 (6)


Text

j I

P 'gCELERATED DISOIBUTION DEMONSTRION SYSTEM

,'l.

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8804210329 DOC.DATE: 88/04/18 NOTARIZED: NO DOCKET FACIL:STN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530 AUTH.NAME AUTHOR AFFILIATION HAYNES,J.G.

Arizona Nuclear Power Project (formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Special Rept 3-SR-88-002:on 880328,radiation monitoring unit inoperable for greater than 72 h.

DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR I

ENCL P SIZE:

TITLE: 50.73 Licensee Event Report (LER), Incident Rpt, etc.

NOTES:Standardized plant.

RECIPIENT ID CODE/NAME PD5 LA LICITRA,E INTERNAL ACRS MICHELSON AEOD/DOA AEOD/DSP/ROAB ARM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/QAB 10 NRR/DREP/RAB 10 RGN5 FILE 01 EXTERNAL: EG&G GROH,M H ST LOBBY WARD NRC PDR NSIC MAYS,G NOTES:

COPIES LTTR ENCL

.1 1,

1 1'

1 1

1 2

2 1

1 1

0 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 4

4 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME PD5 PD DAVIS,M ACRS MOELLER AEOD/DSP/NAS AEOD/DSP/TPAB DEDRO NRR/DEST/CEB 8H NRR/DEST/ICSB 7

NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NRR/DREP/RPB 10

'RR/PMAS/ILRB12 RES TELFORD,J RES/DRPS DIR FORD BLDG HOY,A LPDR NSIC HARRIS,J COPIES LTTR ENCL 1

1 1

1 2

2 1

1 1

1 1

1 1

1 1

1 1

1 1,

1 1

1 1

1 2

2 1

1 1

1 1

1 1

1 1

1 1

1 D

05000530 S

1' D

Sj A

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 47 ENCL 46

Arizona Nuclear Power Project P.O. BOX 52034

~

PHOENIX. ARIZONA85072-2034 192-00367-JGH/TDS/DAJ April 18, 1988 U. S. Nuclear Regulatory Commission NRC Documen'ontrol Desk Washington, D.C.

20555

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Unit 3 Docket No.

STN 50-530 (License No. NPF-74)

Special Report 3-SR-88-002 File:

88-020-404 Attached please find Special Report 3-SR-88-002 prepared and submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2.

This report discusses a radiation monitoring unit inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

If you have any questions, please contact T.

D. Shriver, Compliance Manager at (602) 393-2521.

Very trul

yours, JGH/TDS/DAJ/kj Attachment cc:

0.

M. DeMichele (all w/a)

E.

E.

Van Brunt, Jr.

J.

B. Martin T. J.

Po 1 ich E.

A. Licitra A. C. Gehr INPO Records Center J.

G.

Hay<(es Vice President Nuclear Production

~pg.'Z

] )

8804210329 880418 PDR ADOCK 05000530 S

DCD

ALO VERDE NUCLEAR GENERATING S ION Radiation Monitoring Unit Inoperable for Greater Than 72 Hours License No. NPF-74 Docket No.

STN 50-530 Special Report No. 3-SR-88-002 This Special Report is being submitted pursuant to Technical Specification 3.3.3.8 ACTION 42b and Technical Specification 6.9.2 to report an event in which a Radioactive Gaseous Effluent Monitor (Fuel Building Ventilation System High Range Monitor RU-146) was inoperable for greater than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> limit for returning the monitor to operability was exceeded at approximately 0100 MST on March 31, 1988.

Pursuant to Technical Specification 3.3.3.8 ACTION 42a the Preplanned Alternate Sampling Program was initiated to monitor the Fuel Building Ventilation System when needed.

At 0100 MST on March 28,

1988, Palo Verde Unit 3 was in Mode 1

(POWER OPERATION) when the. Fuel Building Ventilation System High Range Monitor RU-146 was declared inoperable due to unsatisfactory performance of the source check while performing surveillance test 75ST-9ZZ08 (Effluent Monitor Monthly Source Check).

An authorized work document was issued to troubleshoot/rework/replace components to correct the cause of the monitor not passing the check source surveillance on channel 2.

During troubleshooting a Detector High Voltage Failure alarm and a Detector Failure alarm were received.

The high voltage was found to be approximately 2.5 times greater than the normal value.

The high voltage board was replaced with a replacement high voltage board and the voltage adjusted to a normal value.

The detector is believed to have failed

'due to the excessive high voltage from the faulty high voltage board.

The detector was replaced with a new detector and surveillance test 36ST-9Sgll (RU-145/RU-146 Calibration Test) was satisfactorily performed on RU-146 channel 2.

An Engineering Evaluation Request has been submitted to perform a

root cause of failure analysis on the malfunctioning components.

After satisfactory completion of appropriate surveillance tests RU-146 was declared operable at 1357 MST on April 1, 1988.

The monitor was out of service for'approximately 4 days and 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />.