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=Text=
=Text=
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O IIT Oconec Unit 2 DATE 8/8/75 DOCKET NO.
O   .
50-270 PREPARED BY
                                                                                  -
: k. 0..Sharpe OPERATING STATUS 1.
  .
REPORTING PERIOD: July 1, 1975 THROUGH July 31, 1975 GROSS HOURS IN REPORTING PERIOD:
IIT   Oconec Unit 2 DATE   8/8/75 DOCKET NO.           50-270 PREPARED BY           k. 0..Sharpe OPERATING STATUS
744.00 2.
: 1. REPORTING PERIOD: July 1, 1975               THROUGH             July 31, 1975 GROSS HOURS IN REPORTING PERIOD:                 744.00
CURRENTLY AUTHORIZED POWER LEVEL (MWt): 2568 NET CAPABILITY (MWe-Net):
: 2. CURRENTLY AUTHORIZED POWER LEVEL (MWt): 2568 NET CAPABILITY (MWe-Net):             871
871 3.
: 3. POWER LEVEL TO WHICH RESTRICTED (IF ANY):(MWe-Net)                         None
POWER LEVEL TO WHICH RESTRICTED (IF ANY):(MWe-Net)
: 4. REASONS FOR RESTRICTION (IF ANY) hiis Month             Year to Date       Cumulative
None 4.
: 5. NUMBER OF HOURS THE REACTOR WAS
REASONS FOR RESTRICTION (IF ANY) hiis Month Year to Date Cumulative 5.
'
NUMBER OF HOURS THE REACTOR WAS CRITICAL 561.7 3599.2 5545.3 i
CRITICAL                                     561.7                 3599.2           5545.3 i
6.
: 6. REACTOR RESERVE SHUTDOWN HOURS               -                      -                -
REACTOR RESERVE SHUTDOWN HOURS 7.
: 7. HOURS GENERATOR ON-LINE                       551.6     _
HOURS GENERATOR ON-LINE 551.6 3489.9 5365.3 8.
3489.9           5365.3
UNIT RESERVE SHUTDOWN HOURS 9.
: 8. UNIT RESERVE SHUTDOWN HOURS                   -                      -                -
GROSS THERMAL ENERGY GENERATED (MWH) 1363641 8285879 12592777 10.
: 9. GROSS THERMAL ENERGY GENERATED (MWH) 1363641                         8285879           12592777
GROSS ELECTRICAL ENERGY GENERATED (MWH) 459160 2823460 4292436 11.
: 10. GROSS ELECTRICAL ENERGY GENERATED                                                                     '
NET ELECTRICAL ENERGY GENERATED (MWH) 435753 2679407 4066933 12.
(MWH)                                       459160     _
REACTOR SERVICE FACTOR 75.5 70.8 70.9 4
2823460           4292436
13.
'
REACTOR AVAILABILITY FACTOR 74.1 68.8 68.9 14.
: 11. NET ELECTRICAL ENERGY GENERATED (MWH)                                         435753                 2679407           4066933 4      12. REACTOR SERVICE FACTOR                       75.5                   70.8             70.9
UNIT SERVICE FACTOR 74.1 68.6 68.6 l
: 13. REACTOR AVAILABILITY FACTOR                   74.1                   68.8             68.9
15.
,      14. UNIT SERVICE FACTOR                           74.1                   68.6             68.6 l       15. UNIT AVAILABILITY FACTOR                       74.1                   68.6             68.6 i
UNIT AVAILABILITY FACTOR 74.1 68.6 68.6 i
: 16. UNIT CAPACITY FACTOR (Using Net               67.2                 60.5             59.7 Capability)
16.
: 17. UNIT CAPACITY FACTOR (Using Design Mwe)                             66.0                 59.4             58.6
UNIT CAPACITY FACTOR (Using Net 67.2 60.5 59.7 Capability) 17.
: 18. UNIT FORCED OUTAGE RATE                       25.9                 31.0             31.1
UNIT CAPACITY FACTOR (Using Design Mwe) 66.0 59.4 58.6 18.
: 19. SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE & DURATION OF EACH:)
UNIT FORCED OUTAGE RATE 25.9 31.0 31.1 19.
.
SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE & DURATION OF EACH:)
: 20. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
20.
    -
IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:
REACTOR SERVICE FACTOR = HOURS REACTOR WAS CRITICAT. X 100 110URS IN REPORTING PERIOD REACTOR AVAILABILIW FACTOR = HollRS RFACTOR UAS AVAIIAnl.E TO OPERATE X 100 Il0URS IN REPORTING PERIOD 11 NIT SERVICE l' ACTOR   = HolrPS GEMERATOR ON 1.1NE HOURS IN REPORTING PERIOD                 912180
REACTOR SERVICE FACTOR = HOURS REACTOR WAS CRITICAT. X 100 110URS IN REPORTING PERIOD REACTOR AVAILABILIW FACTOR = HollRS RFACTOR UAS AVAIIAnl.E TO OPERATE X 100 Il0URS IN REPORTING PERIOD 11 NIT SERVICE l' ACTOR
            '
= HolrPS GEMERATOR ON 1.1NE HOURS IN REPORTING PERIOD 912180 UNIT AVAIIARTLin FACTOR = 110URS ITNIT WAS AVAITABI.E TO CENERATE X 100 HOURS IN REPORTING PERIOD l
UNIT AVAIIARTLin FACTOR = 110URS ITNIT WAS AVAITABI.E TO CENERATE X 100 HOURS IN REPORTING PERIOD l
= NET ELECTRICAL POWER CENERATED UNIT CAPACITY FACTOR.
UNIT CAPACITY FACTOR.    = NET ELECTRICAL POWER CENERATED
[N *L Capability or Design (Mwe-Net.)] X 1100Rd IN REPOKTfld,-
[N *L Capability or Design (Mwe-Net.)] X 1100Rd IN REPOKTfld,-
PERTOn L_                       UNIT FORCD OUTACE RATE - FOP.Crl],0tQA,G,E_ljojfjlS                     --
PERTOn L_
_      .100   1
UNIT FORCD OUTACE RATE - FOP.Crl],0tQA,G,E_ljojfjlS
.100 1


                                                                                                                                                                      .
D CKET No. _50-270 Oconee Unit 2 UNIT SHUTDOWNS UNIT NAMii DATli 8/8/75 REPORT MONTil July, 1975 TYPE METHOD OF F FORCED DURATION SHUTTING DOWN NO.
                                                                                                                                                                        '
DATE S-SCHEDULED (HOURS)
                                                      .
REASON (1)
                                                                                                                                                                          .
THE REACTOR (2)
D CKET No. _50-270 UNIT SHUTDOWNS                                 UNIT NAMii Oconee Unit 2
CORRECTIVE ACTIONS /COMMFNTS 11 750701 F
                                                                                                                                                                          .
192.37 A
DATli 8/8/75 REPORT MONTil         July, 1975 TYPE               ,
1 Unit shutdown to investigate low reactor coolant pump motor oil level and to perform surveillance tests.
METHOD OF                                                       -
F FORCED   DURATION                       SHUTTING DOWN NO. DATE   S-SCHEDULED   (HOURS)   REASON (1)         THE REACTOR (2)         CORRECTIVE ACTIONS /COMMFNTS 11   750701       F       192.37         A                     1         Unit shutdown to investigate low reactor coolant pump motor oil level and to perform surveillance tests.
                                                                                                                                                                  .
I I
I I
                                                                                                                                                              .
(I) REASON (2) METIIOD A -EQUIPMENT I ALLURE (EXPLAIN) 3-MANUAL 3
(I) REASON                   *
B-MAINT. OR TEST.
(2) METIIOD A -EQUIPMENT I ALLURE (EXPLAIN)     3-MANUAL             3 B- MAINT. OR TEST.                   2-MANUAL C- RLEUELING                           SCR AM D-REGULATORY RESTRICTION             3- AUTOM ATIC E-OPER ATOR TRAINING AND               SCRAM LICENSL EXAMINATION F-ADMINISTRATIVE G-OPER ATION AL ER ROR                           '
2-MANUAL C-RLEUELING SCR AM D-REGULATORY RESTRICTION 3-AUTOM ATIC E-OPER ATOR TRAINING AND SCRAM LICENSL EXAMINATION F-ADMINISTRATIVE G-OPER ATION AL ER ROR (EXPLAIN)
(EXPLAIN)
II-OlllLR IEXPLAIN)
II-OlllLR IEXPLAIN)
                                                                                                                              .  .
                                                                                                                            .


==SUMMARY==
==SUMMARY==
:
Unit returned to service on July 9, 1975 and operated base loaded for remainder of the month.
Unit returned to service on July 9, 1975 and operated base loaded for remainder of the month.
                                                                                                    .
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                        _                    _ _ _ _


                                      ---                          --
          '
                                                                            -
      . .
    .
50-270 DOCKET NO.
50-270 DOCKET NO.
UNIT oeonee UnitJ DATE 8/8/75
UNIT oeonee UnitJ DATE 8/8/75 AVERAGE DAILY UNIT POWER LEVEL MONTH July, 1975 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-net)
  .
DAY (MWe net) 823 17 1
AVERAGE DAILY UNIT POWER LEVEL
823 18 2
                                                                          .
819 3
July, 1975 MONTH AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY                 (MWe net)           .
19 20 814 4
DAY                   (MWe-net)
815 21 5
                                          -
815 6
17                 823 1
22 812 23 7
                                          -
812 24 8
18 823 2
813 498 25 g
819
788 684 26 l
                                          -
10 801 818 27 11 808 822 28 12 824 29 806 13 802 14 825 30 806 825 31 15
19 3
'825 16 DAILY UNrr POWER LEVEL FORM INSTRUCTIONS On this form, list tite average daily unit power level in MWe-net for each day in the reporting month.
                                          -
20                 814 4
                                          -
21                 815 5
                                          -
22                  815 6
                                          -                        23                 812 7
812 8
                                          -                        24 813 g                      498                         25
                                '
788                           l 10 684                         26                                               l
                                                                                                                    '
818                           27               801 11 822                           28               808 12 824                           29               806 13 30              802 14                       825 825                           31               806 15 16                      '825 DAILY UNrr POWER LEVEL FORM INSTRUCTIONS
'  -        On this form, list tite average daily unit power level in MWe-net for each day in the reporting month.
Compute to the nearest whole megawatt.
Compute to the nearest whole megawatt.
These figures will be used to plot a graph for each reporting month. Note that by using maximum dependable capacity for the net electrical rating of the unit. there may be occasions when the daily average power level' exceeds the 100'"o line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.}}
These figures will be used to plot a graph for each reporting month. Note that by using maximum dependable capacity for the net electrical rating of the unit. there may be occasions when the daily average power level' exceeds the 100'"o line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.}}

Latest revision as of 21:54, 1 January 2025

Monthly Operating Rept for Jul 1975
ML19317E693
Person / Time
Site: Oconee  
Issue date: 08/08/1975
From: Sharpe R
DUKE POWER CO.
To:
Shared Package
ML19317E691 List:
References
NUDOCS 7912180849
Download: ML19317E693 (3)


Text

-

O IIT Oconec Unit 2 DATE 8/8/75 DOCKET NO.

50-270 PREPARED BY

k. 0..Sharpe OPERATING STATUS 1.

REPORTING PERIOD: July 1, 1975 THROUGH July 31, 1975 GROSS HOURS IN REPORTING PERIOD:

744.00 2.

CURRENTLY AUTHORIZED POWER LEVEL (MWt): 2568 NET CAPABILITY (MWe-Net):

871 3.

POWER LEVEL TO WHICH RESTRICTED (IF ANY):(MWe-Net)

None 4.

REASONS FOR RESTRICTION (IF ANY) hiis Month Year to Date Cumulative 5.

NUMBER OF HOURS THE REACTOR WAS CRITICAL 561.7 3599.2 5545.3 i

6.

REACTOR RESERVE SHUTDOWN HOURS 7.

HOURS GENERATOR ON-LINE 551.6 3489.9 5365.3 8.

UNIT RESERVE SHUTDOWN HOURS 9.

GROSS THERMAL ENERGY GENERATED (MWH) 1363641 8285879 12592777 10.

GROSS ELECTRICAL ENERGY GENERATED (MWH) 459160 2823460 4292436 11.

NET ELECTRICAL ENERGY GENERATED (MWH) 435753 2679407 4066933 12.

REACTOR SERVICE FACTOR 75.5 70.8 70.9 4

13.

REACTOR AVAILABILITY FACTOR 74.1 68.8 68.9 14.

UNIT SERVICE FACTOR 74.1 68.6 68.6 l

15.

UNIT AVAILABILITY FACTOR 74.1 68.6 68.6 i

16.

UNIT CAPACITY FACTOR (Using Net 67.2 60.5 59.7 Capability) 17.

UNIT CAPACITY FACTOR (Using Design Mwe) 66.0 59.4 58.6 18.

UNIT FORCED OUTAGE RATE 25.9 31.0 31.1 19.

SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE & DURATION OF EACH:)

20.

IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

REACTOR SERVICE FACTOR = HOURS REACTOR WAS CRITICAT. X 100 110URS IN REPORTING PERIOD REACTOR AVAILABILIW FACTOR = HollRS RFACTOR UAS AVAIIAnl.E TO OPERATE X 100 Il0URS IN REPORTING PERIOD 11 NIT SERVICE l' ACTOR

= HolrPS GEMERATOR ON 1.1NE HOURS IN REPORTING PERIOD 912180 UNIT AVAIIARTLin FACTOR = 110URS ITNIT WAS AVAITABI.E TO CENERATE X 100 HOURS IN REPORTING PERIOD l

= NET ELECTRICAL POWER CENERATED UNIT CAPACITY FACTOR.

[N *L Capability or Design (Mwe-Net.)] X 1100Rd IN REPOKTfld,-

PERTOn L_

UNIT FORCD OUTACE RATE - FOP.Crl],0tQA,G,E_ljojfjlS

.100 1

D CKET No. _50-270 Oconee Unit 2 UNIT SHUTDOWNS UNIT NAMii DATli 8/8/75 REPORT MONTil July, 1975 TYPE METHOD OF F FORCED DURATION SHUTTING DOWN NO.

DATE S-SCHEDULED (HOURS)

REASON (1)

THE REACTOR (2)

CORRECTIVE ACTIONS /COMMFNTS 11 750701 F

192.37 A

1 Unit shutdown to investigate low reactor coolant pump motor oil level and to perform surveillance tests.

I I

(I) REASON (2) METIIOD A -EQUIPMENT I ALLURE (EXPLAIN) 3-MANUAL 3

B-MAINT. OR TEST.

2-MANUAL C-RLEUELING SCR AM D-REGULATORY RESTRICTION 3-AUTOM ATIC E-OPER ATOR TRAINING AND SCRAM LICENSL EXAMINATION F-ADMINISTRATIVE G-OPER ATION AL ER ROR (EXPLAIN)

II-OlllLR IEXPLAIN)

SUMMARY

Unit returned to service on July 9, 1975 and operated base loaded for remainder of the month.

50-270 DOCKET NO.

UNIT oeonee UnitJ DATE 8/8/75 AVERAGE DAILY UNIT POWER LEVEL MONTH July, 1975 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-net)

DAY (MWe net) 823 17 1

823 18 2

819 3

19 20 814 4

815 21 5

815 6

22 812 23 7

812 24 8

813 498 25 g

788 684 26 l

10 801 818 27 11 808 822 28 12 824 29 806 13 802 14 825 30 806 825 31 15

'825 16 DAILY UNrr POWER LEVEL FORM INSTRUCTIONS On this form, list tite average daily unit power level in MWe-net for each day in the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that by using maximum dependable capacity for the net electrical rating of the unit. there may be occasions when the daily average power level' exceeds the 100'"o line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.