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6 TENNESSEE - VALLEY AUTHC:4 TTY r~''a o ek CHA1 s ANOCGA,. TENNESSEE ' | |||
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Washington, DC 203h3 | c-L; W;yOg g 4-by; V" | ||
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: f..,e NN Mr. John F. O' Leary, Director Directorate of Licensing | |||
~ Office of Redulation U.S. Atomic Energy Co=11ssion Washington, DC 203h3 | |||
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==Dear Mr. O' Leary:== | ==Dear Mr. O' Leary:== | ||
TEtiNESSEE VALLEY AUTHORITY - BROEIS FERRY HUCLEAR PLANT UNIT 1 - | TEtiNESSEE VALLEY AUTHORITY - BROEIS FERRY HUCLEAR PLANT UNIT 1 - | ||
DOCKET NO. 50-259 - FACILITY OPERATII;G LICENSE DPR ABNORMAL OCCURRENCE REPORT BFAO-7425W The enclosed report is to provide details concerning HPCI system which failed to deliver water to the reactor when initiated on low water level follouing a reactor seren. This event occurred on Browns Ferry Huclear Plant unit 1 on May 5, 1^//4, and is submitted'in accordance with Appendi:: A to Regulatory Guide 1.16, Revision 1, October 1973. | DOCKET NO. 50-259 - FACILITY OPERATII;G LICENSE DPR ABNORMAL OCCURRENCE REPORT BFAO-7425W The enclosed report is to provide details concerning HPCI system which failed to deliver water to the reactor when initiated on low water level follouing a reactor seren. This event occurred on Browns Ferry Huclear Plant unit 1 on May 5, 1^//4, and is submitted'in accordance with Appendi:: A to Regulatory Guide 1.16, Revision 1, October 1973. | ||
Very truly yours, TENNESSEE VALLEY AUTHORITY | Very truly yours, TENNESSEE VALLEY AUTHORITY | ||
: d. <T.m E. F. Thonas | : d. <T.m E. F. Thonas | ||
~ Director of Pouer Production t | |||
Enclosure CC (Enclosure): | Enclosure CC (Enclosure): | ||
Mr. Normen C. Moseley, Director Region II Regulatory Operations Office, USAEC 230 Peachtree Street, ml., Suite 618 Atlanta, Georgia 30303 | Mr. Normen C. Moseley, Director Region II Regulatory Operations Office, USAEC 230 Peachtree Street, ml., Suite 618 Atlanta, Georgia 30303 | ||
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8305050411 740515 PDR ADOCK 05000259 | \\ | ||
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ABNORI/AL OCCURRI2 ICE REPORT Report Ilo.: | |||
BFAO-7425W | |||
~ Report Date: May 15', 1974 Occurrence Date: I?ay 5,1974 Facility: | |||
Browns Ferry ITuclear Plant unit 1 Identification of Occurrence HPCI system failed to deliver water to the reactor when initiated on low water level following a reactor scram. | |||
Conditions Prior to Occurrence Startup testing affecting the feedvater system was being conducted. The testing caused feedwater system fluctuations and low reactor water level with a consequent scram. The unit was operating at approximately 92-percent power at the time of scran. | Conditions Prior to Occurrence Startup testing affecting the feedvater system was being conducted. The testing caused feedwater system fluctuations and low reactor water level with a consequent scram. The unit was operating at approximately 92-percent power at the time of scran. | ||
Description of Occurrence The HPCI system was initiated by low water level following a scram at 8:43 a.=. on | Description of Occurrence The HPCI system was initiated by low water level following a scram at 8:43 a.=. on | ||
'May 5,1974. The system atte=pted to start but tripped off. | |||
It was placed on manual control and was started. | |||
It was utilized satisfactorily in the manual mode to assist in regulating vessel water level. Vnen no longer needed for service, it was shut down. | |||
* Fonowing shutdown, it was noticed that the inverter power supply fuse alarm was annunciated. The system was declared inoperable at 10:55 a.m. | * Fonowing shutdown, it was noticed that the inverter power supply fuse alarm was annunciated. The system was declared inoperable at 10:55 a.m. | ||
Designation of Atmarent Cause of Occurrence An investigation was conducted to determine the cause of the IECI trip. No absolute cause was determined. One possibility was an overspeed trip of the machine; however, overspeeding could not be confirmed. | Designation of Atmarent Cause of Occurrence An investigation was conducted to determine the cause of the IECI trip. No absolute cause was determined. One possibility was an overspeed trip of the machine; however, overspeeding could not be confirmed. | ||
Analysis of Occurrence During the brief interval between the HPCI trip and manual actuation and the period involving the failed fuse, all remaining safety systems were available. | Analysis of Occurrence During the brief interval between the HPCI trip and manual actuation and the period involving the failed fuse, all remaining safety systems were available. | ||
Vessel water level was controlled at all times by other systems, and there were l | Vessel water level was controlled at all times by other systems, and there were l | ||
no adverse consequences experienced. | |||
Corrective Action l | Corrective Action l | ||
The inverter power supply was checked and nothing was found amiss. The output | The inverter power supply was checked and nothing was found amiss. The output 1 cads from the power supply were lifted, and the circuit was checked for grounds l | ||
1 cads from the power supply were lifted, and the circuit was checked for grounds | or shorted conditions with all results satisfactory. The leads were connected and a new fuse satisfactorily installed. | ||
The power supply reacted satisfactorily to checks; and the system was declared operabic at 12:20 p.m. on May 5, 1974. | |||
.The power supply will be instru=ented in order to further determine the cause of the fuse failure. | |||
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Corrective f.ction (continued) | 6 f | ||
subsequent scram after startup on 1:cy 6,1974, at 8:26 p.r. | 2 Corrective f.ction (continued) l The HPCI operated satisfactorily when auto =atically initiated following'a subsequent scram after startup on 1:cy 6,1974, at 8:26 p.r. | ||
Fcilure Data | Fcilure Data i | ||
Failures of 'a similar nature have been reported in BFAo-739W, BFAo-7318W, BFAO-7329W, and BFAO-7336W. | |||
BFAO-7329W, and BFAO-7336W. | |||
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Latest revision as of 04:32, 14 December 2024
| ML20084H811 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 05/15/1974 |
| From: | Eric Thomas TENNESSEE VALLEY AUTHORITY |
| To: | Oleary J US ATOMIC ENERGY COMMISSION (AEC) |
| Shared Package | |
| ML20084H813 | List: |
| References | |
| BFAO-7425W, NUDOCS 8305050411 | |
| Download: ML20084H811 (3) | |
Text
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' b.
6 TENNESSEE - VALLEY AUTHC:4 TTY r~a o ek CHA1 s ANOCGA,. TENNESSEE '
3740'1 LJ
-\\
('A
- D L2-r L_
ammmen,,w)y
-~m May 15, 1974 h
f; Oh*n"x5Nl lei $
,?
/.,M V..
W b
.r.0 l^-
c-L; W;yOg g 4-by; V"
~
- f..,e NN Mr. John F. O' Leary, Director Directorate of Licensing
~ Office of Redulation U.S. Atomic Energy Co=11ssion Washington, DC 203h3
.~s
Dear Mr. O' Leary:
TEtiNESSEE VALLEY AUTHORITY - BROEIS FERRY HUCLEAR PLANT UNIT 1 -
DOCKET NO. 50-259 - FACILITY OPERATII;G LICENSE DPR ABNORMAL OCCURRENCE REPORT BFAO-7425W The enclosed report is to provide details concerning HPCI system which failed to deliver water to the reactor when initiated on low water level follouing a reactor seren. This event occurred on Browns Ferry Huclear Plant unit 1 on May 5, 1^//4, and is submitted'in accordance with Appendi:: A to Regulatory Guide 1.16, Revision 1, October 1973.
Very truly yours, TENNESSEE VALLEY AUTHORITY
- d. <T.m E. F. Thonas
~ Director of Pouer Production t
Enclosure CC (Enclosure):
Mr. Normen C. Moseley, Director Region II Regulatory Operations Office, USAEC 230 Peachtree Street, ml., Suite 618 Atlanta, Georgia 30303
[c/ j.
e
(!'h(
- ,J '
\\
8305050411 740515 PDR ADOCK 05000259 4 F. ? 9.
s PDR con suramon *
?
.,s m
n V.
Q i
ABNORI/AL OCCURRI2 ICE REPORT Report Ilo.:
BFAO-7425W
~ Report Date: May 15', 1974 Occurrence Date: I?ay 5,1974 Facility:
Browns Ferry ITuclear Plant unit 1 Identification of Occurrence HPCI system failed to deliver water to the reactor when initiated on low water level following a reactor scram.
Conditions Prior to Occurrence Startup testing affecting the feedvater system was being conducted. The testing caused feedwater system fluctuations and low reactor water level with a consequent scram. The unit was operating at approximately 92-percent power at the time of scran.
Description of Occurrence The HPCI system was initiated by low water level following a scram at 8:43 a.=. on
'May 5,1974. The system atte=pted to start but tripped off.
It was placed on manual control and was started.
It was utilized satisfactorily in the manual mode to assist in regulating vessel water level. Vnen no longer needed for service, it was shut down.
- Fonowing shutdown, it was noticed that the inverter power supply fuse alarm was annunciated. The system was declared inoperable at 10:55 a.m.
Designation of Atmarent Cause of Occurrence An investigation was conducted to determine the cause of the IECI trip. No absolute cause was determined. One possibility was an overspeed trip of the machine; however, overspeeding could not be confirmed.
Analysis of Occurrence During the brief interval between the HPCI trip and manual actuation and the period involving the failed fuse, all remaining safety systems were available.
Vessel water level was controlled at all times by other systems, and there were l
no adverse consequences experienced.
Corrective Action l
The inverter power supply was checked and nothing was found amiss. The output 1 cads from the power supply were lifted, and the circuit was checked for grounds l
or shorted conditions with all results satisfactory. The leads were connected and a new fuse satisfactorily installed.
The power supply reacted satisfactorily to checks; and the system was declared operabic at 12:20 p.m. on May 5, 1974.
.The power supply will be instru=ented in order to further determine the cause of the fuse failure.
= ~- -- --
--* - --^-
- r. -
t o
6 f
2 Corrective f.ction (continued) l The HPCI operated satisfactorily when auto =atically initiated following'a subsequent scram after startup on 1:cy 6,1974, at 8:26 p.r.
Fcilure Data i
Failures of 'a similar nature have been reported in BFAo-739W, BFAo-7318W, BFAO-7329W, and BFAO-7336W.
i P
s e
e e
O 4
4 i
e 2-'
e-,
gy.v w
,--y-g
-,7r y,
y ww w
ym,.3ey
.-p.
9 p,.,
,,-g ag g
g=-4y
.y.
e99yeq 74q. 9
,,.wpp_.,4c.
3 g,
s-w,y p 7 3yg 9
.g
-