ENS 41246: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by Mark Hawes)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 12/05/2004 21:35 EST
| event date = 12/05/2004 21:35 EST
| last update date = 12/06/2004
| last update date = 12/06/2004
| title = Automatic Turbine Trip/Reactor Trip Due To Moisture Separator Reheater (Msr) High Level Trip Signal.
| title = Automatic Turbine Trip/Reactor Trip Due to Moisture Separator Reheater (Msr) High Level Trip Signal.
| event text = Reactor Trip caused by Turbine trip. Turbine trip caused by a Moisture Separator Reheater 1B high level.  Maintenance personnel were working in vicinity of level switches at time of trip.  Root cause investigation in progress.  All systems operated as designed on Reactor trip.
| event text = Reactor Trip caused by Turbine trip. Turbine trip caused by a Moisture Separator Reheater 1B high level.  Maintenance personnel were working in vicinity of level switches at time of trip.  Root cause investigation in progress.  All systems operated as designed on Reactor trip.
Maintenance personnel working in the vicinity of Moisture Separator Reheater 1B were setting up radiography equipment when the MSR 1B high level trip was generated.  All rods fully inserted. Both Motor Driven Auxiliary Feedwater pumps actuated as expected.  All Emergency Core Cooling Systems and the Emergency Diesel Generators are fully operable if needed.  Catawba Unit 2 is operating at 100% power and the electrical grid is stable.
Maintenance personnel working in the vicinity of Moisture Separator Reheater 1B were setting up radiography equipment when the MSR 1B high level trip was generated.  All rods fully inserted. Both Motor Driven Auxiliary Feedwater pumps actuated as expected.  All Emergency Core Cooling Systems and the Emergency Diesel Generators are fully operable if needed.  Catawba Unit 2 is operating at 100% power and the electrical grid is stable.

Latest revision as of 22:22, 1 March 2018

ENS 41246 +/-
Where
Catawba Duke Energy icon.png
South Carolina (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.3 h-0.0958 days <br />-0.0137 weeks <br />-0.00315 months <br />)
Opened: Jeff Nieberding
00:17 Dec 6, 2004
NRC Officer: John Mackinnon
Last Updated: Dec 6, 2004
41246 - NRC Website
Loading map...