ENS 44268: Difference between revisions

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| event date = 06/04/2008 17:30 EDT
| event date = 06/04/2008 17:30 EDT
| last update date = 06/04/2008
| last update date = 06/04/2008
| title = Manual Reactor Trip Following Loss Of Main Feedwater Pump
| title = Manual Reactor Trip Following Loss of Main Feedwater Pump
| event text = On 6/4/2008 at 17:30 hrs an unplanned manual reactor trip was initiated on St. Lucie Unit 2 from 100% power due to a trip of the 2B Heater Drain pump leading to a trip of the 2A Main Feedwater Pump and decreasing S/G levels.  The Reactor was manually tripped due to decreasing Steam Generator levels.
| event text = On 6/4/2008 at 17:30 hrs an unplanned manual reactor trip was initiated on St. Lucie Unit 2 from 100% power due to a trip of the 2B Heater Drain pump leading to a trip of the 2A Main Feedwater Pump and decreasing S/G levels.  The Reactor was manually tripped due to decreasing Steam Generator levels.
Following the reactor trip, EOP-1, Standard Post Trip Actions, and EOP-2, Reactor Trip Recovery procedures were completed and Unit 2 was stabilized in Mode 3.  All control rods fully inserted. The S/G Safety Valves lifted and the last valve reseated at 950 psig.  Feedwater to the S/G was supplied by the 2B Main FW Pumps and then the Auxiliary Feedwater Pumps.  Unit 2 electrical requirements are provided from offsite power.  All safe shutdown equipment operated as expected. There were no major equipment failures. Unit 1 was not affected by this event. The Grid is stable.
Following the reactor trip, EOP-1, Standard Post Trip Actions, and EOP-2, Reactor Trip Recovery procedures were completed and Unit 2 was stabilized in Mode 3.  All control rods fully inserted. The S/G Safety Valves lifted and the last valve reseated at 950 psig.  Feedwater to the S/G was supplied by the 2B Main FW Pumps and then the Auxiliary Feedwater Pumps.  Unit 2 electrical requirements are provided from offsite power.  All safe shutdown equipment operated as expected. There were no major equipment failures. Unit 1 was not affected by this event. The Grid is stable.

Latest revision as of 22:14, 1 March 2018

ENS 44268 +/-
Where
Saint Lucie NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-0.33 h-0.0138 days <br />-0.00196 weeks <br />-4.52034e-4 months <br />)
Opened: Calvin Ward
21:10 Jun 4, 2008
NRC Officer: Bill Huffman
Last Updated: Jun 4, 2008
44268 - NRC Website
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