ENS 44439: Difference between revisions

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| event date = 06/28/2008 19:04 CDT
| event date = 06/28/2008 19:04 CDT
| last update date = 08/25/2008
| last update date = 08/25/2008
| title = 60-Day Optional Report For An Invalid Actuation Of Unit 1 Tdafw Pump
| title = 60-Day Optional Report for an Invalid Actuation of Unit 1 Tdafw Pump
| event text = This report describes an invalid actuation of the Unit 1 Turbine Driven Auxiliary Feedwater (TDAFW) pump that occurred on June 28, 2008. This report is being made in accordance with 10CFR50.73(a)(1), which states, in part, 'In the case of an invalid actuation reported under 10CFR50.73(a)(2)(iv), other than actuation of the Reactor Protection System (RPS) when the reactor is critical, the licensee may, at its option, provide a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER.'
| event text = This report describes an invalid actuation of the Unit 1 Turbine Driven Auxiliary Feedwater (TDAFW) pump that occurred on June 28, 2008. This report is being made in accordance with 10CFR50.73(a)(1), which states, in part, 'In the case of an invalid actuation reported under 10CFR50.73(a)(2)(iv), other than actuation of the Reactor Protection System (RPS) when the reactor is critical, the licensee may, at its option, provide a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER.'
On June 28, 2008, Comanche Peak Nuclear Power Plant Unit 1 was in Mode 1 operating at 100% power.  At 1904 CDT, the steam supply valve from Main Steam Line 1-04 to the TDAFW pump opened due to a failed diaphragm. Turbine load was subsequently reduced from 1207MWe to 1150MWe per Operations procedures. The upstream isolation valve for the steam supply to the TDAFW pump was closed and the TDAFW pump was stopped. Unit 1 was returned to full power at 2120 CDT and the failed diaphragm was subsequently replaced.
On June 28, 2008, Comanche Peak Nuclear Power Plant Unit 1 was in Mode 1 operating at 100% power.  At 1904 CDT, the steam supply valve from Main Steam Line 1-04 to the TDAFW pump opened due to a failed diaphragm. Turbine load was subsequently reduced from 1207MWe to 1150MWe per Operations procedures. The upstream isolation valve for the steam supply to the TDAFW pump was closed and the TDAFW pump was stopped. Unit 1 was returned to full power at 2120 CDT and the failed diaphragm was subsequently replaced.

Latest revision as of 22:13, 1 March 2018

ENS 44439 +/-
Where
Comanche Peak Luminant icon.png
Texas (NRC Region 4)
Reporting
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation
Time - Person (Reporting Time:+1384.38 h57.683 days <br />8.24 weeks <br />1.896 months <br />)
Opened: Gary Merka
16:27 Aug 25, 2008
NRC Officer: Howie Crouch
Last Updated: Aug 25, 2008
44439 - NRC Website
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