ENS 45324: Difference between revisions
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| event date = 07/10/2009 02:38 EDT | | event date = 07/10/2009 02:38 EDT | ||
| last update date = 09/03/2009 | | last update date = 09/03/2009 | ||
| title = Electrical Short Circuit Resulted | | title = Electrical Short Circuit Resulted in Partial High Pressure Injection | ||
| event text = This event is being reported via a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER. In this case, the telephone report is not considered an LER. This report is being made under 10 CFR 50.73(a)(2)(iv)(A). | | event text = This event is being reported via a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER. In this case, the telephone report is not considered an LER. This report is being made under 10 CFR 50.73(a)(2)(iv)(A). | ||
During a maintenance activity to replace an Engineered Safeguards Actuation System (ESAS) relay, one of the two High Pressure Injection (HPI) valves (MU-V-16C) in the 'B' train partially opened. The HPI system consists of the 'A' and 'B' trains, with each train containing two HPI valves. The cause of the partial opening of the HPI valve was inadvertent contact with adjacent energized circuits during the replacement of the ESAS relay. This resulted in a momentary short circuit, which bypassed the normal actuation logic, causing the HPI valve to open approximately 0.17 inches before blowing the control power fuse that stopped the valve movement. The event resulted in the inadvertent transfer of approximately 1000 gallons of water from the Make-up Tank into the Reactor Coolant System (RCS), before the valve could be restored to the closed position. No other valves or components actuated as a result of the inadvertent short circuit. RCS volume and pressure were stabilized and returned to normal. | During a maintenance activity to replace an Engineered Safeguards Actuation System (ESAS) relay, one of the two High Pressure Injection (HPI) valves (MU-V-16C) in the 'B' train partially opened. The HPI system consists of the 'A' and 'B' trains, with each train containing two HPI valves. The cause of the partial opening of the HPI valve was inadvertent contact with adjacent energized circuits during the replacement of the ESAS relay. This resulted in a momentary short circuit, which bypassed the normal actuation logic, causing the HPI valve to open approximately 0.17 inches before blowing the control power fuse that stopped the valve movement. The event resulted in the inadvertent transfer of approximately 1000 gallons of water from the Make-up Tank into the Reactor Coolant System (RCS), before the valve could be restored to the closed position. No other valves or components actuated as a result of the inadvertent short circuit. RCS volume and pressure were stabilized and returned to normal. |
Latest revision as of 22:11, 1 March 2018
Where | |
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Three Mile Island Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1322.43 h55.101 days <br />7.872 weeks <br />1.811 months <br />) | |
Opened: | Adam Miller 09:04 Sep 3, 2009 |
NRC Officer: | Dong Park |
Last Updated: | Sep 3, 2009 |
45324 - NRC Website
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