ENS 46094: Difference between revisions

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| event date = 07/14/2010 19:34 EDT
| event date = 07/14/2010 19:34 EDT
| last update date = 07/15/2010
| last update date = 07/15/2010
| title = Tech Spec Shutdown Due To Through Wall Flaws In S/G Sample Line, Secondary Side
| title = Tech Spec Shutdown Due to Through Wall Flaws in S/G Sample Line, Secondary Side
| event text = At 1834 hours on 7/14/10, the Unit 1 'C' Reactor Coolant Loop was declared inoperable due to small unisolable leaks on the 'C' Steam Generator secondary side surface sample line. Two small through-wall flaws were identified in the piping upstream of 1 -SS-217, 'C' Steam Generator surface sample line manual isolation valve. The piping is Class 2 and the non-conforming condition could not be evaluated with the steam generator pressurized. Based on the condition of the piping and the inability to evaluate the flaw, the 'C'  Steam Generator was declared inoperable per Technical Requirements Manual 3.4.6, ASME Code Class 1, 2 and 3 Components. Subsequently, Technical Specification 3.4.4 was entered to place Unit 1 in Mode 3 within 6 hours.
| event text = At 1834 hours on 7/14/10, the Unit 1 'C' Reactor Coolant Loop was declared inoperable due to small unisolable leaks on the 'C' Steam Generator secondary side surface sample line. Two small through-wall flaws were identified in the piping upstream of 1 -SS-217, 'C' Steam Generator surface sample line manual isolation valve. The piping is Class 2 and the non-conforming condition could not be evaluated with the steam generator pressurized. Based on the condition of the piping and the inability to evaluate the flaw, the 'C'  Steam Generator was declared inoperable per Technical Requirements Manual 3.4.6, ASME Code Class 1, 2 and 3 Components. Subsequently, Technical Specification 3.4.4 was entered to place Unit 1 in Mode 3 within 6 hours.
At 1934 hours on 7/14/10, North Anna Unit 1 initiated a shutdown in accordance with Technical Specification 3.4.4. The unit will be shutdown and the line will be evaluated and repaired.
At 1934 hours on 7/14/10, North Anna Unit 1 initiated a shutdown in accordance with Technical Specification 3.4.4. The unit will be shutdown and the line will be evaluated and repaired.

Latest revision as of 22:09, 1 March 2018

ENS 46094 +/-
Where
North Anna Dominion icon.png
Virginia (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-3.68 h-0.153 days <br />-0.0219 weeks <br />-0.00504 months <br />)
Opened: Page Kemp
19:53 Jul 14, 2010
NRC Officer: John Knoke
Last Updated: Jul 15, 2010
46094 - NRC Website
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