ENS 49417: Difference between revisions

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| event date = 10/07/2013 18:04 CDT
| event date = 10/07/2013 18:04 CDT
| last update date = 10/13/2013
| last update date = 10/13/2013
| title = Vent Stack And Area Radiation Monitors Taken Out Of Service For Maintenance
| title = Vent Stack and Area Radiation Monitors Taken Out of Service for Maintenance
| event text = This is a report of a loss of emergency assessment capability as required by 10CFR50.72(b)(3)(xiii).
| event text = This is a report of a loss of emergency assessment capability as required by 10CFR50.72(b)(3)(xiii).
On October 7, 2013 at 1804 CDT, with Unit 1 in Mode 6 during a refueling outage, power was interrupted to all Unit 1 vent stack radiation monitors and area radiation monitors as part of a pre-planned activity to connect the radiation monitors to an alternate temporary power supply to support deenergizing the normal power source for preventative maintenance.  The connection to the alternate supply was completed and power was restored to the vent stack radiation monitors and area radiation monitors at 1833 CDT.  While the radiation monitors were without power, pre-planned compensatory measures were implemented where possible to monitor vent stack discharge and to minimize activities that posed a potential for release.
On October 7, 2013 at 1804 CDT, with Unit 1 in Mode 6 during a refueling outage, power was interrupted to all Unit 1 vent stack radiation monitors and area radiation monitors as part of a pre-planned activity to connect the radiation monitors to an alternate temporary power supply to support deenergizing the normal power source for preventative maintenance.  The connection to the alternate supply was completed and power was restored to the vent stack radiation monitors and area radiation monitors at 1833 CDT.  While the radiation monitors were without power, pre-planned compensatory measures were implemented where possible to monitor vent stack discharge and to minimize activities that posed a potential for release.

Latest revision as of 21:59, 1 March 2018

ENS 49417 +/-
Where
Farley Southern Nuclear icon.png
Alabama (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Time - Person (Reporting Time:+-2.47 h-0.103 days <br />-0.0147 weeks <br />-0.00338 months <br />)
Opened: Matt Stanley
20:36 Oct 7, 2013
NRC Officer: Dong Park
Last Updated: Oct 13, 2013
49417 - NRC Website
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