ENS 50310: Difference between revisions

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| event date = 07/25/2014 11:29 EDT
| event date = 07/25/2014 11:29 EDT
| last update date = 07/26/2014
| last update date = 07/26/2014
| title = Technical Specification Required Shutdown Due To A Safety Injection Valve Defect
| title = Technical Specification Required Shutdown Due to a Safety Injection Valve Defect
| event text = On July 25th, 2014 at 1129 EDT, during investigation of a small leak inside Saint Lucie Unit 2 containment, a defect was identified on a valve (V3811, Safety Injection Tank 281 Outlet Vent Valve). This valve is within the Q-Group A (ASME Class 1 equivalent) boundary of the safety injection line. The leak is currently isolated from the reactor coolant system by a Technical Specification credited isolation check valve. The affected Safety Injection Tank has been declared inoperable and the unit has entered 24 hour shutdown [Technical Specification] action statement 3.5.1.b. Unit shutdown is currently being planned for repair of the flaw.
| event text = On July 25th, 2014 at 1129 EDT, during investigation of a small leak inside Saint Lucie Unit 2 containment, a defect was identified on a valve (V3811, Safety Injection Tank 281 Outlet Vent Valve). This valve is within the Q-Group A (ASME Class 1 equivalent) boundary of the safety injection line. The leak is currently isolated from the reactor coolant system by a Technical Specification credited isolation check valve. The affected Safety Injection Tank has been declared inoperable and the unit has entered 24 hour shutdown [Technical Specification] action statement 3.5.1.b. Unit shutdown is currently being planned for repair of the flaw.
This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(A).
This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(A).

Latest revision as of 20:50, 1 March 2018

ENS 50310 +/-
Where
Saint Lucie NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded

10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-1.45 h-0.0604 days <br />-0.00863 weeks <br />-0.00199 months <br />)
Opened: Tim Kudo
14:02 Jul 25, 2014
NRC Officer: Daniel Mills
Last Updated: Jul 26, 2014
50310 - NRC Website
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