ENS 52436: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by Mark Hawes)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:
| event date = 10/28/2016 01:39 CST
| event date = 10/28/2016 01:39 CST
| last update date = 12/15/2016
| last update date = 12/15/2016
| title = Invalid Actuation Of Containment Isolation Valves
| title = Invalid Actuation of Containment Isolation Valves
| event text = This telephone notification is being made in lieu of a Licensee Event Report in accordance with 10CFR50.73(a)(1) to notify the NRC of on invalid actuation of a group isolation, reportable under 10CFR50.73(a)(2)(iv)(A).
| event text = This telephone notification is being made in lieu of a Licensee Event Report in accordance with 10CFR50.73(a)(1) to notify the NRC of on invalid actuation of a group isolation, reportable under 10CFR50.73(a)(2)(iv)(A).
On October 28, at 0139 Central Daylight Time, electricians were removing a test jack from a terminal on a primary containment isolation system relay due to the test jack being installed on the wrong relay.  During removal of the test jack, a neutral wire came out of the terminal causing multiple relay actuations resulting in a half Group 2 isolation signal on the Division 2 side.  Because of the plant being in Mode 5, refueling, the only isolation valves that closed because of the invalid isolation signal were the Division 2 isolation valves associated with the drywell ventilation monitor and the drywell floor and equipment sumps.
On October 28, at 0139 Central Daylight Time, electricians were removing a test jack from a terminal on a primary containment isolation system relay due to the test jack being installed on the wrong relay.  During removal of the test jack, a neutral wire came out of the terminal causing multiple relay actuations resulting in a half Group 2 isolation signal on the Division 2 side.  Because of the plant being in Mode 5, refueling, the only isolation valves that closed because of the invalid isolation signal were the Division 2 isolation valves associated with the drywell ventilation monitor and the drywell floor and equipment sumps.

Latest revision as of 21:43, 1 March 2018

ENS 52436 +/-
Where
Cooper Entergy icon.png
Nebraska (NRC Region 4)
Reporting
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation
Time - Person (Reporting Time:+1153.73 h48.072 days <br />6.867 weeks <br />1.58 months <br />)
Opened: David Van Der Kamp
10:23 Dec 15, 2016
NRC Officer: Mark Abramovitz
Last Updated: Dec 15, 2016
52436 - NRC Website
Loading map...