ENS 52790: Difference between revisions
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| event date = 04/28/2017 05:00 EDT | | event date = 04/28/2017 05:00 EDT | ||
| last update date = 06/06/2017 | | last update date = 06/06/2017 | ||
| title = 60-Day Optional Telephonic Notification | | title = 60-Day Optional Telephonic Notification for an Invalid Auxiliary Feedwater Actuation | ||
| event text = This 60-day telephone notification is being submitted in accordance with paragraphs 10 CFR 50.73(a)(1) and 50.73(a)(2)(iv)(A) to report an invalid Auxiliary Feedwater (AFW) actuation at Watts Bar Nuclear Plant (WBN) Unit 1. | | event text = This 60-day telephone notification is being submitted in accordance with paragraphs 10 CFR 50.73(a)(1) and 50.73(a)(2)(iv)(A) to report an invalid Auxiliary Feedwater (AFW) actuation at Watts Bar Nuclear Plant (WBN) Unit 1. | ||
On April 28, 2017 at approximately 0500 Eastern Daylight Time (EDT), Unit 1 maintenance personnel were performing 1-IMI-3.005, '18 Month Calibration of Anticipated Transient Without Scram System Actuation Circuitry (AMSAC),' when an AMSAC actuation signal was received. Both Motor Driven Auxiliary Feedwater Pumps (MDAFWPs) were already in service when this actuation occurred. The Turbine Driven Auxiliary Feedwater Pump (TDAFWP) did not start as it had been removed from service. Additionally, steam generator blowdown isolated as required. During this event, AMSAC actuation was complete and equipment functioned as expected by its operating state. | On April 28, 2017 at approximately 0500 Eastern Daylight Time (EDT), Unit 1 maintenance personnel were performing 1-IMI-3.005, '18 Month Calibration of Anticipated Transient Without Scram System Actuation Circuitry (AMSAC),' when an AMSAC actuation signal was received. Both Motor Driven Auxiliary Feedwater Pumps (MDAFWPs) were already in service when this actuation occurred. The Turbine Driven Auxiliary Feedwater Pump (TDAFWP) did not start as it had been removed from service. Additionally, steam generator blowdown isolated as required. During this event, AMSAC actuation was complete and equipment functioned as expected by its operating state. |
Latest revision as of 21:42, 1 March 2018
Where | |
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Watts Bar Tennessee (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+935.5 h38.979 days <br />5.568 weeks <br />1.281 months <br />) | |
Opened: | David Allen 08:30 Jun 6, 2017 |
NRC Officer: | Steve Sandin |
Last Updated: | Jun 6, 2017 |
52790 - NRC Website
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