ENS 52918: Difference between revisions

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| event date = 08/20/2017 16:05 PDT
| event date = 08/20/2017 16:05 PDT
| last update date = 08/24/2017
| last update date = 08/24/2017
| title = Manual Reactor Scram Due To A Rise In Main Condenser Back Pressure
| title = Manual Reactor Scram Due to a Rise in Main Condenser Back Pressure
| event text = On August 20, 2017 at 1605 PDT, Columbia Generating Station was manually scrammed from 100 percent power due to a rise of Main Condenser back pressure. Manual scram of the unit is procedurally required upon a loss of Main Condenser back pressure. Preliminary investigations indicate that the Main Condenser air removal suction valve (AR-V-1) closed, resulting in the Condenser back pressure rising to within 1.0 inch Hg of the setpoint with reactor power greater than 25 percent. Further investigations continue. All control rods fully inserted.
| event text = On August 20, 2017 at 1605 PDT, Columbia Generating Station was manually scrammed from 100 percent power due to a rise of Main Condenser back pressure. Manual scram of the unit is procedurally required upon a loss of Main Condenser back pressure. Preliminary investigations indicate that the Main Condenser air removal suction valve (AR-V-1) closed, resulting in the Condenser back pressure rising to within 1.0 inch Hg of the setpoint with reactor power greater than 25 percent. Further investigations continue. All control rods fully inserted.
In addition to the closure of the air removal suction valve, one of two Reactor Feedwater startup flow control valves did not adequately operate to control Reactor vessel level and resulted in a high-level (Level-8) actuation tripping the Reactor Feedwater System. All other systems operated as expected. Reactor water level is currently being controlled manually with the start-up level control isolation valve. AR-V-1 has been manually opened with a jumper and temporary air supply. Reactor decay heat is being removed via bypass valves to the Main Condenser.
In addition to the closure of the air removal suction valve, one of two Reactor Feedwater startup flow control valves did not adequately operate to control Reactor vessel level and resulted in a high-level (Level-8) actuation tripping the Reactor Feedwater System. All other systems operated as expected. Reactor water level is currently being controlled manually with the start-up level control isolation valve. AR-V-1 has been manually opened with a jumper and temporary air supply. Reactor decay heat is being removed via bypass valves to the Main Condenser.

Latest revision as of 21:42, 1 March 2018

ENS 52918 +/-
Where
Columbia Generating Station Energy Northwest icon.png
Washington (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-0.32 h-0.0133 days <br />-0.0019 weeks <br />-4.38336e-4 months <br />)
Opened: Rick Kerrone
22:46 Aug 20, 2017
NRC Officer: Donald Norwood
Last Updated: Aug 24, 2017
52918 - NRC Website
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