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{{#Wiki_filter:.,
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ff,       '%          ,m 3              UNITED STATES J  t      O"           't         ,V NUCLEAR REGULATORY COMMISSION                                     '
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,m UNITED STATES 3
              .. 1       .Ej                      WASHINGTON, D. C. 20555 f
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l g, %......f                                                             .
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l                          SAFETYENALUATIONBYTHEOFFICEOFNUCLEARREACTORREGULATION i
,V NUCLEAR REGULATORY COMMISSION J
SUPPORTING AMENDMENT NO. 25 TO FACILITY OPERATING LICENSE N0. DPR-3 YANKEE ATOMIC ELECTRIC COMPANY
tV'(s.. 1
* YANKEE NUCLEAR POWER STATION (YANKEE-R6WE)
.E WASHINGTON, D. C. 20555 i
DOCKET NO. 50-29 Introduction By application dated May 11, 1976, and supplements dated May 11, 17 and 19, 1976, Yankee Atomic Electric Company [the licensee) proposed a change to the Technical Specifications appended to License No. DPR-3. for the Yankee-Rowe reactor.         The proposal involves a change to the set                                     ;
f g's j
pressure for the Low Pressure Safety Injection Accumulator, specified in s4.
l g, %......f l
Section D.2.c(4), from 410 psig to 337 psig +_10 psig.                                               L$
SAFETYENALUATIONBYTHEOFFICEOFNUCLEARREACTORREGULATION i
t'   'y Discussion During a previous refueling outage, the licensee measured the accumulator                             a t"n
SUPPORTING AMENDMENT NO. 25 TO FACILITY OPERATING LICENSE N0. DPR-3 YANKEE ATOMIC ELECTRIC COMPANY YANKEE NUCLEAR POWER STATION (YANKEE-R6WE)
                                                                                                                > ?
DOCKET NO. 50-29 Introduction By application dated May 11, 1976, and supplements dated May 11, 17 and 19, 1976, Yankee Atomic Electric Company [the licensee) proposed a change to the Technical Specifications appended to License No. DPR-3. for the Yankee-Rowe reactor.
flow rate to confirm minimum ECCS flow.             Recently, in the course of a con-h[
The proposal involves a change to the set pressure for the Low Pressure Safety Injection Accumulator, specified in s
tinuinc review of ECCS design and performance, the licensee discovered that the actual accumulator flow rate was higher than was used in RELAP 4-EM code                         @N ps calculations for ECCS performance for Yankee-Rowe.               The apparent cause of the           dI#
4.
WP lower calculated accumulator flow was a non-conservative input to the LOCA                                 E L
Section D.2.c(4), from 410 psig to 337 psig +_10 psig.
blowdown calculation.                                                                                 ..
L$
M Staff Evaluation N
t'
y, In a meeting en May 13, 1976, the licensee presented to the staff their eval-k uation of the effect of the difference between actual measured and calculated                         M accumulator flow.       They also presented their proposal for correcting this                       f:
'y Discussion During a previous refueling outage, the licensee measured the accumulator t"n a
j.y difference.         g0                                                                               u
> ?
                  .- -          11070 l9c m                                                   w'
flow rate to confirm minimum ECCS flow.
    ;k                                 ,        .
Recently, in the course of a con-h[
                                                            ~
tinuinc review of ECCS design and performance, the licensee discovered that
@N the actual accumulator flow rate was higher than was used in RELAP 4-EM code ps dI#
calculations for ECCS performance for Yankee-Rowe.
The apparent cause of the WPE lower calculated accumulator flow was a non-conservative input to the LOCA L'
blowdown calculation.
..M Staff Evaluation N
y, In a meeting en May 13, 1976, the licensee presented to the staff their eval-k uation of the effect of the difference between actual measured and calculated M
f:
accumulator flow.
They also presented their proposal for correcting this j.y difference.
g0 11070 l9c u
m w
;k
~


n                                                             b                                :
b n
o                                       ~2-e
o e
                                                                                                                                    . g.
~2-
. g.
v.
v.
W The licensee proposed a readjustment of the accumulator pressure downward                                               h n
W The licensee proposed a readjustment of the accumulator pressure downward h
such that accumulator flow would agree with the value in the current                                                   -
n such that accumulator flow would agree with the value in the current licensee's analyses.
licensee's analyses.     The NRC staff agrees that accumulator pressure should                                           h be readjusted downward to be consistent with the licensee's analysis.                                           The   ;t
The NRC staff agrees that accumulator pressure should h
                                                                                                                                        '~
be readjusted downward to be consistent with the licensee's analysis.
staff believes this action is appropriate because of the design of ECCS                                                 y$
The
cooling system of the Yankee-Rowe plant (particularly the accumulator injec-tion system) and because the staff believes that to determine if higher f-accumulator flow rates are conservative would require extensive analysis.                                                     E p
;t
p Such a revision of the accumulator pressure will affect the ECCS perfor-                                                 j p.
'~
mance evaluation for both the large and small breaks.                                           They are discussed         h$
staff believes this action is appropriate because of the design of ECCS y$
in the fo1 5 wing sections.                                                                                             4l$
cooling system of the Yankee-Rowe plant (particularly the accumulator injec-tion system) and because the staff believes that to determine if higher f-accumulator flow rates are conservative would require extensive analysis.
Ep p
Such a revision of the accumulator pressure will affect the ECCS perfor-j p.
mance evaluation for both the large and small breaks.
They are discussed h$
4l$
in the fo1 5 wing sections.
b@
b@
: 1)     Large Breaks                                                                                                       [f 0"i Primary coolant system depressurization is very rapid for large breaks and the time delay caused by initiating accumu. itor flow at 352 psia                                             jg 9
1)
instead of 420 psia is insignificant.                     As such, it will not result in                         g w.
Large Breaks
appreciably different reflood and heatup transients.                                       The staff believes k
[f 0"i Primary coolant system depressurization is very rapid for large breaks and the time delay caused by initiating accumu. itor flow at 352 psia jg 9
previously accepted large break analyses are still valid.                                                       y 3
instead of 420 psia is insignificant.
b The Yankee-Rowe accumulator contains 700 ft of water and has a constant nitrogen dome as a driving force.                     The method proposed by the license'e to reduce the flow is to reduce the accumulator pressure.                                       An accumula-       d tor flow test was performed with a 30 ft. head of water above the core                                             D in the reactor vessel.       The accumulator nitrogen overpressure was 382 psig.                                     }
As such, it will not result in g
                                                                                                                                          ,g Flow was measured by monitoring accumulator level changes and by                                                   'I measuring the flow to each loop and the average flow was determined to d
w.
R n
appreciably different reflood and heatup transients.
be 5,375 gpm.                                                                                                   k' x-g e-                             ,=#w.       e.mg .     . syne.ernme% evye ,     e= syme ===ee-+ ===ne. w , y             so.
The staff believes k
previously accepted large break analyses are still valid.
y b
3 The Yankee-Rowe accumulator contains 700 ft of water and has a constant nitrogen dome as a driving force.
The method proposed by the license'e to reduce the flow is to reduce the accumulator pressure.
An accumula-dD tor flow test was performed with a 30 ft. head of water above the core in the reactor vessel.
The accumulator nitrogen overpressure was 382 psig.
}
,g Flow was measured by monitoring accumulator level changes and by
'I d
measuring the flow to each loop and the average flow was determined to R
n be 5,375 gpm.
k' x-g e-
,=#w.
e.mg.
. syne.ernme% evye,
e= syme===ee-+===ne. w, y so.


w -. .. . -- . ~                 . - -          .      .+                 .-
w -.... --. ~
.+
3
3
{t
{t
            ^-
^ -
N '1 y   [
. N '1 y [
A simplified 6 Volurae RELAP 4-EM model was constructed equivalent to                       kk
A simplified 6 Volurae RELAP 4-EM model was constructed equivalent to k k
(     -
(
the nodal representation used for the ECCS analysis for the Core XII                               J LOCA submittal. A parametric study of !drge break EC.C5 flow versus accumulator pressure was perfonned over a range of accumulator                               l pressures.
the nodal representation used for the ECCS analysis for the Core XII J
It was determined that an accumulator pressure of 352 psia will produce an ECCS flow rate in agreement with the Yankte-Rowe Core XII LOCA                               f submittal. It was also shown that an uncertainty range of + 10 psi on this pressure would maintain acceptable BOCREC, reflood rates, and
LOCA submittal. A parametric study of !drge break EC.C5 flow versus accumulator pressure was perfonned over a range of accumulator l
pressures.
It was determined that an accumulator pressure of 352 psia will produce an ECCS flow rate in agreement with the Yankte-Rowe Core XII LOCA f
submittal.
It was also shown that an uncertainty range of + 10 psi on this pressure would maintain acceptable BOCREC, reflood rates, and
['
['
4 accumulator empty times.         These parameters versus accumulator pressure               '. e ifb are shown below:                                                                           N Reflood Rates (1b/secl                                     h gK A:cumulator                           Before           After             Effective             1 Pressure           B0CREC         Accumulator     Accumulator         Accumulator       k,.
4 accumulator empty times.
(psia)             (sec)         Empty           Empty         Empty Time (sec)     d
These parameters versus accumulator pressure
                                                                                                            ;g YR Core XII         102.49           534.0             221               114.79         F LOCA Submittal                                                                             Ek M
'.e ifb are shown below:
342           103.80           541.5             221               118.67 hy 352           102.83           550.2             221               115.87 h_
N Reflood Rates (1b/secl h
362           102.50           558.7             221               113.88 h
gK A:cumulator Before After Effective 1
: 2)     Small Breaks                                                                                 8
Pressure B0CREC Accumulator Accumulator Accumulator k,.
                                                                                                            .e.g
(psia)
                                                                                                              .n Small break analyses were performed by the licensee using the WFLASH code h
(sec)
dy and submitted to the NRC on July 31, 1974.           These analyses, considered           g, n.
Empty Empty Empty Time (sec) d
2, 3, and 4-inch diameter breaks.           Results of these analyses indicated           9         '
;g YR Core XII 102.49 534.0 221 114.79 F
                                                                                                            't; that the core never became uncovered for the 2" break.             A peak clad             W 3        '
LOCA Submittal Ek M
p        l 1
342 103.80 541.5 221 118.67 h
i V"                   .      .
y h_
s
352 102.83 550.2 221 115.87 h
362 102.50 558.7 221 113.88 8
2)
Small Breaks
.e.g
.n Small break analyses were performed by the licensee using the WFLASH code h
dy and submitted to the NRC on July 31, 1974.
These analyses, considered g,
n.
2, 3, and 4-inch diameter breaks.
Results of these analyses indicated 9
't; that the core never became uncovered for the 2" break.
A peak clad W
3p i
V" s


                                                                                                              '~
'~
Q
Q
                                                                  ~
~
s               ~
s
~
n v),
n v),
r                        .-
7p.-
7p.-
k
r k
        '   ~
~ '
                                                                    '                                      h?
h
                                                                                                              ;;,   K temperature (PCT) of approximately 750*F was calculated for the 3-inch break and occurred at 160 seconds after break initiation. The 4-inch                     fk
?
                                                                                                          .A break was detemined to be limiting with a PCT of 1300*F occurring                   .-
;;, K temperature (PCT) of approximately 750*F was calculated for the 3-inch fk break and occurred at 160 seconds after break initiation. The 4-inch
l            r 235 seconds after break initiation.                                                 i' i
.A break was detemined to be limiting with a PCT of 1300*F occurring l
The potential effcet of the proposed change in accumulator pressure on                   (j the ECCS performance to mitigate the consequences of a small break was                             ;
r 235 seconds after break initiation.
evaluated. The Core =XII LOCA analysis submitted to the NRC on                     ,
i' i
                    ' October 10, 1975, predicted that for the 3-inch break the PCT occurred                             -
The potential effcet of the proposed change in accumulator pressure on (j
prior to the time that the reactor coolant pressure decreased to a                               $
the ECCS performance to mitigate the consequences of a small break was evaluated.
value, that permitted flow from the accumulator to the reactor coolant                           ;r kif system; that is, ior the 3-inch diameter break the accident was mitigated                 %:
The Core =XII LOCA analysis submitted to the NRC on
without the accumulator. Therefore, the staff concluded that the
' October 10, 1975, predicted that for the 3-inch break the PCT occurred prior to the time that the reactor coolant pressure decreased to a value, that permitted flow from the accumulator to the reactor coolant
                    . change in accum.u l ator pressure would have no effect on ECCS performance               W m mq for breaks of 3-inches or less.                                                         gi U 5 The 4-inch break was reanalyzed using the ENC WREM based evaluation                       p.t model. The results of this re-analysis were included in the licensee's k
;r kif system; that is, ior the 3-inch diameter break the accident was mitigated without the accumulator. Therefore, the staff concluded that the
b[.
. change in accum.u ator pressure would have no effect on ECCS performance W
October 10, 1975, application for a license amendment for authorizing operation of Yankee-Rowe with Core XII. The calculated PCT during the period of core uncovery was determined to be 1400'F and to occur                       >h at 230 seconds. However, a PCT of about 1850*F was calculated to occur                   lh3 at about 9 seconds, before the core was uncovered, due to a momentary
l m
                                                                                                                  @M flow stagnatior.                                                                           ;;g a
mq for breaks of 3-inches or less.
y
gi U
                                                                                                                  ?fs.
p.t 5
The 4-inch break was reanalyzed using the ENC WREM based evaluation kb[.
model.
The results of this re-analysis were included in the licensee's October 10, 1975, application for a license amendment for authorizing operation of Yankee-Rowe with Core XII. The calculated PCT during the period of core uncovery was determined to be 1400'F and to occur
>h lh at 230 seconds.
However, a PCT of about 1850*F was calculated to occur 3
@M at about 9 seconds, before the core was uncovered, due to a momentary
;;g flow stagnatior.
ay
?fs.
T
T
                                                                                                                  , .wp
,.wp
                                                                                                                  \G m,
\\G m,
I[
I[
y-                                         -
y-a=r ce m
a=r ce m   -
?:k.
    ?:k.                                               ?,l ?
?,l ?
s                                    "1   't         t Y              a,   ,      .,  am. - , . a+-
Y "1
't t
a, am.
a+-
s


  .      .                  _ . _ _        _ _ . _ _ . _  .~           _ _ _ _ _ _ _ _ _        ~__
.~
  '                                  .                    w
~__
            '.                      h                                                                                                                               ,
w h e It was determined that the accumulator would begin delivery to the main coolant system at 230 seconds (380 psia). With a reduced accumu-
e It was determined that the accumulator would begin delivery to the
,1 lator pressure of 352 psia, injection will be delayed to s 252 seconds I
                                                                                                        ,1 main coolant system at 230 seconds (380 psia). With a reduced accumu-lator pressure of 352 psia, injection will be delayed to s 252 seconds I   -
(312 psia).
(312 psia).     Assuming the adiabatic heatup, which started at 215 seconds,   t         .
Assuming the adiabatic heatup, which started at 215 seconds, t
continues to 252 se>:onds, the second peak would be e'xpected to increase from 1400*F to about 1680*F. This value is well below the 2200 F limit
continues to 252 se>:onds, the second peak would be e'xpected to increase from 1400*F to about 1680*F. This value is well below the 2200 F limit of 10 CFR Part 50.46 and is significantly less than the initial peak PCT If
                                                                                                        .g of 10 CFR Part 50.46 and is significantly less than the initial peak PCT
.g of 18500F. As such, the change in the accumulator pressure does not g
          -                                                                                              If g
b significantly increase the overall PCT fQr the 4l breck.,
of 18500F. As such, the change in the accumulator pressure does not b
significantly increase the overall PCT fQr the 4l breck.,
k' W
k' W
W, The licensee has not submitted analyses for small breaks larger than 4-inches in diameter and contends that the larger small breaks (i.e.,               $
W, The licensee has not submitted analyses for small breaks larger than 4-inches in diameter and contends that the larger small breaks (i.e.,
N ff(
$ff(
5-inch or larger) are not limiti.ng and will result in icwer PCTs. This           Nf contention is based on the argument that larger breaks result in faster         [k- w yt; system depressurization and more rapid injection of ECC Coolant which               %
5-inch or larger) are not limiti.ng and will result in icwer PCTs. This NN contention is based on the argument that larger breaks result in faster
in turn results in the core being uncovered for a shorter period of                 @
[k-f w
time.
system depressurization and more rapid injection of ECC Coolant which yt; in turn results in the core being uncovered for a shorter period of time.
g During its review, the staff determined that the Yankee Rowe coolant injection rate is much greater than the H.B. Robinson plant (for which         Q8l w
g During its review, the staff determined that the Yankee Rowe coolant injection rate is much greater than the H.B. Robinson plant (for which Q8l w
a complete small break spectrum exists).       H.B. Robinson, which had           $1 i f
a complete small break spectrum exists).
previously been reviewed by the staff, had a maximum small break PCT             g$
H.B. Robinson, which had
occuring for an 8-inch diameter break, but exhibited the same trend as           P*)
$1 i fg$
expected for Yankee-Rowe, that is, a decrease in PCT for break sizes             Q
previously been reviewed by the staff, had a maximum small break PCT P*)
                                                                                                        ,Q greater than the small break limiting break size before an increase               tf R,
occuring for an 8-inch diameter break, but exhibited the same trend as expected for Yankee-Rowe, that is, a decrease in PCT for break sizes Q
again occurs in the large break region. Because of a substantially                 g.
,Q greater than the small break limiting break size before an increase tf R,
w faster depressurization rate and a much higher coolant injection rate,         ,;,
again occurs in the large break region.
Yankee-Rowe would be expected to have the maximum PCT for small breaks
Because of a substantially g.
w faster depressurization rate and a much higher coolant injection rate, Yankee-Rowe would be expected to have the maximum PCT for small breaks


w                         ,      . a..         ..-    ..-.=....-.:-. .= w                                                                       -        - .      -.
w a..
                                                                                                                                                                ,p' q
..-.=....-.:-..= w
,p' q
(
(
M 4,
M 4,
                                                                                                                                                                        )
)a occuring at a substantia 11y'sma11er size break than for H.B.
a occuring at a substantia 11y'sma11er size break than for H.B.                                                                                     g A
g A
4 Robinson.
4 Robinson.
* h A comparison was made between the WREM analysis submitted on                                                                                       p October 10, 1975; the July 31, 1974 WFLASH analysis; and a small                                                                                   h break analysis conducted with the SLAP code and submitted in 1971. The                                                                             E-l staff considers the SLAP code to be less refined than more recent codes,                                                                           %
h A comparison was made between the WREM analysis submitted on p
h, but considers that for small break pressure decay, the behavior should                                                                             g, g
October 10, 1975; the July 31, 1974 WFLASH analysis; and a small h
give reasonable answers.             From reviewing these results, it was found                                                                   g that for the pressure transient in the pressure range of ECC injection,                                                                           W}
break analysis conducted with the SLAP code and submitted in 1971. The E-l$
k excellent agreement was obtained between SLAP and WFLASH calculations for                                                                         $
staff considers the SLAP code to be less refined than more recent codes, h,
JK the 3-inch diameter break which was the only case for which analyses                                                                             %'
but considers that for small break pressure decay, the behavior should g,g give reasonable answers.
y for both codes was performed for Yankee Rowe.                                           A 5-inch diameter break                                   F op.   ,
From reviewing these results, it was found g
                  ' analyzed with SLAP indicates that the core never uncovers.                                                                       Therefore,        f the SLAP results indicate that the 5" break is not limiting.                                                                                     k h:
W}
w , .
that for the pressure transient in the pressure range of ECC injection, k
The staff believes that the SLAP pressure decays approximate the                                                                                 YOf results that would be calculated by current blowdown analyses with                                                                               4, p
excellent agreement was obtained between SLAP and WFLASH calculations for JK the 3-inch diameter break which was the only case for which analyses y
Since the ECC injection                                            4 both WFLASH and RELAP 4-EM (ENC Version).                                                                                                       @
for both codes was performed for Yankee Rowe.
rates and initiation pressures are the same for all analyses, it is                                                                                 '
A 5-inch diameter break F
reasonable to expect that prediction of liquid level in the core would                                                                           hW   ,
op.
y be comparable.         Although it is recognized that the SLAP Code models the                                                                 b.
Therefore, f
e P'
' analyzed with SLAP indicates that the core never uncovers.
entire primary system as only one or two volumes, the total volumes are                                                                           f f(
the SLAP results indicate that the 5" break is not limiting.
kh:.
w,
The staff believes that the SLAP pressure decays approximate the YOf results that would be calculated by current blowdown analyses with 4,
p4 both WFLASH and RELAP 4-EM (ENC Version).
Since the ECC injection rates and initiation pressures are the same for all analyses, it is reasonable to expect that prediction of liquid level in the core would hW y
be comparable.
Although it is recognized that the SLAP Code models the b.eP' entire primary system as only one or two volumes, the total volumes are ff(
the same regardless of the analytical model used.
the same regardless of the analytical model used.
                                                                                                                                                                        @)
@ )
As noted.above, the 4-inch dianeter break size has an initial PCT of rA' I
As noted.above, the 4-inch dianeter break size has an initial PCT of rA I
1850 and a second peak of 14000F (which can be extrapolated to approximately B
1850 and a second peak of 14000F (which can be extrapolated to approximately B
16800F with the lower accumulator                                                                                                                     i
16800F with the lower accumulator i
                                        . , . ,      . . _  ~ ~ . . . . . , _ . _ . . . . _ . _ _ - _ _ . . . . . . _ ~ - . . . . . , . - - . . . , _ _
~ ~....., _. _.... _. _ _ - _ _...... _ ~ -.....,. - -..., _ _


&                ~ _ _ -            - - . -
~ _ _ -
t 0                       f   sc U     Therefore, in the pressure). The limiting large break PCT is 1896 F.
t 0
event that bre'aks slightly above or below 4 inches turned out to be the limiting small break, reasonable assurar.ce exists that the PCT criterion
f sc U
pressure). The limiting large break PCT is 1896 F.
Therefore, in the event that bre'aks slightly above or below 4 inches turned out to be the limiting small break, reasonable assurar.ce exists that the PCT criterion
[.
[.
of 10 CFR 50.46 is not exceeded. The staff also concludes that there                         ,
of 10 CFR 50.46 is not exceeded. The staff also concludes that there is reasonable assurance that the calculated PCT does n.ot significantly I
is reasonable assurance that the calculated PCT does n.ot significantly                   I ey increase over the entire break spectrum as a result of the accumulator               k pressure decrease.
ey increase over the entire break spectrum as a result of the accumulator k
The staff therefore concludes that the 5-inch diameter break is likely                   y to be less limiting than the 4-inch diameter break.
pressure decrease.
The lic'ensee has stated that he will confirm that the most limiting small break has been identified without relying on comparison with the SLAP calculations. The additional analyses to be performed by the licensee                 h_
The staff therefore concludes that the 5-inch diameter break is likely y
will, as a minimam, evaluate a 4-inch, a 5-inch, and a 10-inch diameter               );kk e
to be less limiting than the 4-inch diameter break.
break and will utilize the revised accumulator pressure.                             Ak k$
The lic' nsee has stated that he will confirm that the most limiting small e
Findinas                                                                                   &
break has been identified without relying on comparison with the SLAP h_
m.
calculations. The additional analyses to be performed by the licensee will, as a minimam, evaluate a 4-inch, a 5-inch, and a 10-inch diameter
The staff concludes that adjusting accumulator pressure to match previous                   h yg ECCS calculation values         is acceptable for large break sizes and that no             $
);kk e
4 further analysis is required for these breaks.           Also, regarding large breaks,   &
break and will utilize the revised accumulator pressure.
the staff further believes that the licensee has properly determined the WP-7/A accumulator set pressure and that the predicted differences in blowdown                   @
Ak
py times and reflood rates shown in the table contained therein are acceptably               l[
$k Findinas m.
                                                                                                        %E close to those determined from the Yankee-Rowe Core XII ECCS submittal.                     M W.
The staff concludes that adjusting accumulator pressure to match previous h
i.,,9 The staff also concludes that the analyses performed by the licensee are                   Q4 adequate to provide reasonable assurance that the requirements of 10 CFR A
yg ECCS calculation values is acceptable for large break sizes and that no
                                                                                                          ?
$4 further analysis is required for these breaks.
Part 50.46 are satisfied for small breaks.           However, for the small breaks, the staff agrees with the licensee that it is desirable to perform additional l!
Also, regarding large breaks, the staff further believes that the licensee has properly determined the WP-7/A accumulator set pressure and that the predicted differences in blowdown py times and reflood rates shown in the table contained therein are acceptably l[
%E close to those determined from the Yankee-Rowe Core XII ECCS submittal.
M W.
i.,,9 The staff also concludes that the analyses performed by the licensee are Q
4 adequate to provide reasonable assurance that the requirements of 10 CFR
?
A Part 50.46 are satisfied for small breaks.
However, for the small breaks, the staff agrees with the licensee that it is desirable to perform additional l!


,      m                     -.....u_.u...____,
m
                                                        -__ _ . _ _ -                  2.__. _ . &      _ _ . . .
-.....u_.u...____,
o                                       .
2.__.
                                                                                                    .C                       <
o
      .                                                                                                                                      m
.C m
                                                                                              -8                                               is E
-8 is E
Q analyses to further verify that the small break spectrum has been completely                                               I
Q analyses to further verify that the small break spectrum has been completely I
                                                                                                                                              ~
~
analyzed for the revised accumulator press're and to better quantify the                                                 h PCT predicted to occur following various size pipe break,s.                         ,
analyzed for the revised accumulator press're and to better quantify the h
PCT predicted to occur following various size pipe break,s.
g
g
                                                                                                                                              $g. .
$g.
k The staff has also determined that the amendment does not authorize a change                                               #;
k The staff has also determined that the amendment does not authorize a change
in effluent types or total amounts, nor an increase in power level, and will                                           :
#;h in effluent types or total amounts, nor an increase in power level, and will 4 (R not result in any significant environmental impact.
h 4   (R not result in any significant environmental impact.                             Having made this                       ysp
Having made this ysp a
                                                                                                                                            <  a determination, we have further concluded that the amendment involves an                                                 ,
determination, we have further concluded that the amendment involves an b
b action which is insignificant from the standpoint of environmental impact                                               g(T :
action which is insignificant from the standpoint of environmental impact g(T :
and pursuant to 10 CFR 5 51.5(d)(4) that an environmental statement, negative                                         !p.
!p.
:g s~
and pursuant to 10 CFR 5 51.5(d)(4) that an environmental statement, negative
declaration, or environmental impact appraisal need not be prepared in w
:g ~
connection with the issuance of this amendment.                                                                       g h
s declaration, or environmental impact appraisal need not be prepared in w
Conclusion                                                                                                             @
connection with the issuance of this amendment.
We have concluded, based on the considerations discussed above, that:                                                 Mw          .
g h
(1) because the change does not involve a significant increase in the probability or consequences of accidents previously considered and does not                                         '
Conclusion We have concluded, based on the considerations discussed above, that:
2je involve a significant decrease in a safety margin, the change does not                                           l.jf involve a significant hazards consideration, (2) there is reasonable assur-
M w
                                                                                                                                          @b ance that the health and safety of the public will not be endangered by                                           '
(1) because the change does not involve a significant increase in the probability or consequences of accidents previously considered and does not 2je involve a significant decrease in a safety margin, the change does not l.jf
l operation in the proposed manner, and (3) such activities will be conducted                                                 ;.,
@b involve a significant hazards consideration, (2) there is reasonable assur-ance that the health and safety of the public will not be endangered by
1 in compliance with the Commission's regulations and the issuance of this                                                   )
' l operation in the proposed manner, and (3) such activities will be conducted 1
amendment will not be inimical to the common defense and security or to                                                   y,!'
)
in compliance with the Commission's regulations and the issuance of this amendment will not be inimical to the common defense and security or to y,!'
the health and safety of the public.
the health and safety of the public.
k g
k g
Date: May 19, 1976
Date: May 19, 1976
                                                                                                                                      %v
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;,ta!
                                                "M*k8*+"r.%== ><4em u s,sseyq 9_g , .,
"M*k8*+"r.%==
                                                                                    ,      ,}}
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Latest revision as of 11:42, 11 December 2024

Safety Evaluation Supporting Amend 25 to License DPR-3
ML20148G048
Person / Time
Site: Yankee Rowe
Issue date: 05/19/1976
From:
Office of Nuclear Reactor Regulation
To:
Shared Package
ML20148G041 List:
References
NUDOCS 8011070145
Download: ML20148G048 (8)


Text

.,

ff,

,m UNITED STATES 3

O"

't

,V NUCLEAR REGULATORY COMMISSION J

tV'(s.. 1

.E WASHINGTON, D. C. 20555 i

f g's j

l g, %......f l

SAFETYENALUATIONBYTHEOFFICEOFNUCLEARREACTORREGULATION i

SUPPORTING AMENDMENT NO. 25 TO FACILITY OPERATING LICENSE N0. DPR-3 YANKEE ATOMIC ELECTRIC COMPANY YANKEE NUCLEAR POWER STATION (YANKEE-R6WE)

DOCKET NO. 50-29 Introduction By application dated May 11, 1976, and supplements dated May 11, 17 and 19, 1976, Yankee Atomic Electric Company [the licensee) proposed a change to the Technical Specifications appended to License No. DPR-3. for the Yankee-Rowe reactor.

The proposal involves a change to the set pressure for the Low Pressure Safety Injection Accumulator, specified in s

4.

Section D.2.c(4), from 410 psig to 337 psig +_10 psig.

L$

t'

'y Discussion During a previous refueling outage, the licensee measured the accumulator t"n a

> ?

flow rate to confirm minimum ECCS flow.

Recently, in the course of a con-h[

tinuinc review of ECCS design and performance, the licensee discovered that

@N the actual accumulator flow rate was higher than was used in RELAP 4-EM code ps dI#

calculations for ECCS performance for Yankee-Rowe.

The apparent cause of the WPE lower calculated accumulator flow was a non-conservative input to the LOCA L'

blowdown calculation.

..M Staff Evaluation N

y, In a meeting en May 13, 1976, the licensee presented to the staff their eval-k uation of the effect of the difference between actual measured and calculated M

f:

accumulator flow.

They also presented their proposal for correcting this j.y difference.

g0 11070 l9c u

m w

k

~

b n

o e

~2-

. g.

v.

W The licensee proposed a readjustment of the accumulator pressure downward h

n such that accumulator flow would agree with the value in the current licensee's analyses.

The NRC staff agrees that accumulator pressure should h

be readjusted downward to be consistent with the licensee's analysis.

The

t

'~

staff believes this action is appropriate because of the design of ECCS y$

cooling system of the Yankee-Rowe plant (particularly the accumulator injec-tion system) and because the staff believes that to determine if higher f-accumulator flow rates are conservative would require extensive analysis.

Ep p

Such a revision of the accumulator pressure will affect the ECCS perfor-j p.

mance evaluation for both the large and small breaks.

They are discussed h$

4l$

in the fo1 5 wing sections.

b@

1)

Large Breaks

[f 0"i Primary coolant system depressurization is very rapid for large breaks and the time delay caused by initiating accumu. itor flow at 352 psia jg 9

instead of 420 psia is insignificant.

As such, it will not result in g

w.

appreciably different reflood and heatup transients.

The staff believes k

previously accepted large break analyses are still valid.

y b

3 The Yankee-Rowe accumulator contains 700 ft of water and has a constant nitrogen dome as a driving force.

The method proposed by the license'e to reduce the flow is to reduce the accumulator pressure.

An accumula-dD tor flow test was performed with a 30 ft. head of water above the core in the reactor vessel.

The accumulator nitrogen overpressure was 382 psig.

}

,g Flow was measured by monitoring accumulator level changes and by

'I d

measuring the flow to each loop and the average flow was determined to R

n be 5,375 gpm.

k' x-g e-

,=#w.

e.mg.

. syne.ernme% evye,

e= syme===ee-+===ne. w, y so.

w -.... --. ~

.+

3

{t

^ -

. N '1 y [

A simplified 6 Volurae RELAP 4-EM model was constructed equivalent to k k

(

the nodal representation used for the ECCS analysis for the Core XII J

LOCA submittal. A parametric study of !drge break EC.C5 flow versus accumulator pressure was perfonned over a range of accumulator l

pressures.

It was determined that an accumulator pressure of 352 psia will produce an ECCS flow rate in agreement with the Yankte-Rowe Core XII LOCA f

submittal.

It was also shown that an uncertainty range of + 10 psi on this pressure would maintain acceptable BOCREC, reflood rates, and

['

4 accumulator empty times.

These parameters versus accumulator pressure

'.e ifb are shown below:

N Reflood Rates (1b/secl h

gK A:cumulator Before After Effective 1

Pressure B0CREC Accumulator Accumulator Accumulator k,.

(psia)

(sec)

Empty Empty Empty Time (sec) d

g YR Core XII 102.49 534.0 221 114.79 F

LOCA Submittal Ek M

342 103.80 541.5 221 118.67 h

y h_

352 102.83 550.2 221 115.87 h

362 102.50 558.7 221 113.88 8

2)

Small Breaks

.e.g

.n Small break analyses were performed by the licensee using the WFLASH code h

dy and submitted to the NRC on July 31, 1974.

These analyses, considered g,

n.

2, 3, and 4-inch diameter breaks.

Results of these analyses indicated 9

't; that the core never became uncovered for the 2" break.

A peak clad W

3p i

V" s

'~

Q

~

s

~

n v),

7p.-

r k

~ '

h

?

, K temperature (PCT) of approximately 750*F was calculated for the 3-inch fk break and occurred at 160 seconds after break initiation. The 4-inch

.A break was detemined to be limiting with a PCT of 1300*F occurring l

r 235 seconds after break initiation.

i' i

The potential effcet of the proposed change in accumulator pressure on (j

the ECCS performance to mitigate the consequences of a small break was evaluated.

The Core =XII LOCA analysis submitted to the NRC on

' October 10, 1975, predicted that for the 3-inch break the PCT occurred prior to the time that the reactor coolant pressure decreased to a value, that permitted flow from the accumulator to the reactor coolant

r kif system; that is, ior the 3-inch diameter break the accident was mitigated without the accumulator. Therefore, the staff concluded that the

. change in accum.u ator pressure would have no effect on ECCS performance W

l m

mq for breaks of 3-inches or less.

gi U

p.t 5

The 4-inch break was reanalyzed using the ENC WREM based evaluation kb[.

model.

The results of this re-analysis were included in the licensee's October 10, 1975, application for a license amendment for authorizing operation of Yankee-Rowe with Core XII. The calculated PCT during the period of core uncovery was determined to be 1400'F and to occur

>h lh at 230 seconds.

However, a PCT of about 1850*F was calculated to occur 3

@M at about 9 seconds, before the core was uncovered, due to a momentary

g flow stagnatior.

ay

?fs.

T

,.wp

\\G m,

I[

y-a=r ce m

?:k.

?,l ?

Y "1

't t

a, am.

a+-

s

.~

~__

w h e It was determined that the accumulator would begin delivery to the main coolant system at 230 seconds (380 psia). With a reduced accumu-

,1 lator pressure of 352 psia, injection will be delayed to s 252 seconds I

(312 psia).

Assuming the adiabatic heatup, which started at 215 seconds, t

continues to 252 se>:onds, the second peak would be e'xpected to increase from 1400*F to about 1680*F. This value is well below the 2200 F limit of 10 CFR Part 50.46 and is significantly less than the initial peak PCT If

.g of 18500F. As such, the change in the accumulator pressure does not g

b significantly increase the overall PCT fQr the 4l breck.,

k' W

W, The licensee has not submitted analyses for small breaks larger than 4-inches in diameter and contends that the larger small breaks (i.e.,

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5-inch or larger) are not limiti.ng and will result in icwer PCTs. This NN contention is based on the argument that larger breaks result in faster

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system depressurization and more rapid injection of ECC Coolant which yt; in turn results in the core being uncovered for a shorter period of time.

g During its review, the staff determined that the Yankee Rowe coolant injection rate is much greater than the H.B. Robinson plant (for which Q8l w

a complete small break spectrum exists).

H.B. Robinson, which had

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previously been reviewed by the staff, had a maximum small break PCT P*)

occuring for an 8-inch diameter break, but exhibited the same trend as expected for Yankee-Rowe, that is, a decrease in PCT for break sizes Q

,Q greater than the small break limiting break size before an increase tf R,

again occurs in the large break region.

Because of a substantially g.

w faster depressurization rate and a much higher coolant injection rate, Yankee-Rowe would be expected to have the maximum PCT for small breaks

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)a occuring at a substantia 11y'sma11er size break than for H.B.

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4 Robinson.

h A comparison was made between the WREM analysis submitted on p

October 10, 1975; the July 31, 1974 WFLASH analysis; and a small h

break analysis conducted with the SLAP code and submitted in 1971. The E-l$

staff considers the SLAP code to be less refined than more recent codes, h,

but considers that for small break pressure decay, the behavior should g,g give reasonable answers.

From reviewing these results, it was found g

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that for the pressure transient in the pressure range of ECC injection, k

excellent agreement was obtained between SLAP and WFLASH calculations for JK the 3-inch diameter break which was the only case for which analyses y

for both codes was performed for Yankee Rowe.

A 5-inch diameter break F

op.

Therefore, f

' analyzed with SLAP indicates that the core never uncovers.

the SLAP results indicate that the 5" break is not limiting.

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The staff believes that the SLAP pressure decays approximate the YOf results that would be calculated by current blowdown analyses with 4,

p4 both WFLASH and RELAP 4-EM (ENC Version).

Since the ECC injection rates and initiation pressures are the same for all analyses, it is reasonable to expect that prediction of liquid level in the core would hW y

be comparable.

Although it is recognized that the SLAP Code models the b.eP' entire primary system as only one or two volumes, the total volumes are ff(

the same regardless of the analytical model used.

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As noted.above, the 4-inch dianeter break size has an initial PCT of rA I

1850 and a second peak of 14000F (which can be extrapolated to approximately B

16800F with the lower accumulator i

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pressure). The limiting large break PCT is 1896 F.

Therefore, in the event that bre'aks slightly above or below 4 inches turned out to be the limiting small break, reasonable assurar.ce exists that the PCT criterion

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of 10 CFR 50.46 is not exceeded. The staff also concludes that there is reasonable assurance that the calculated PCT does n.ot significantly I

ey increase over the entire break spectrum as a result of the accumulator k

pressure decrease.

The staff therefore concludes that the 5-inch diameter break is likely y

to be less limiting than the 4-inch diameter break.

The lic' nsee has stated that he will confirm that the most limiting small e

break has been identified without relying on comparison with the SLAP h_

calculations. The additional analyses to be performed by the licensee will, as a minimam, evaluate a 4-inch, a 5-inch, and a 10-inch diameter

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break and will utilize the revised accumulator pressure.

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$k Findinas m.

The staff concludes that adjusting accumulator pressure to match previous h

yg ECCS calculation values is acceptable for large break sizes and that no

$4 further analysis is required for these breaks.

Also, regarding large breaks, the staff further believes that the licensee has properly determined the WP-7/A accumulator set pressure and that the predicted differences in blowdown py times and reflood rates shown in the table contained therein are acceptably l[

%E close to those determined from the Yankee-Rowe Core XII ECCS submittal.

M W.

i.,,9 The staff also concludes that the analyses performed by the licensee are Q

4 adequate to provide reasonable assurance that the requirements of 10 CFR

?

A Part 50.46 are satisfied for small breaks.

However, for the small breaks, the staff agrees with the licensee that it is desirable to perform additional l!

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Q analyses to further verify that the small break spectrum has been completely I

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analyzed for the revised accumulator press're and to better quantify the h

PCT predicted to occur following various size pipe break,s.

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k The staff has also determined that the amendment does not authorize a change

  1. h in effluent types or total amounts, nor an increase in power level, and will 4 (R not result in any significant environmental impact.

Having made this ysp a

determination, we have further concluded that the amendment involves an b

action which is insignificant from the standpoint of environmental impact g(T :

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and pursuant to 10 CFR 5 51.5(d)(4) that an environmental statement, negative

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s declaration, or environmental impact appraisal need not be prepared in w

connection with the issuance of this amendment.

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Conclusion We have concluded, based on the considerations discussed above, that:

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(1) because the change does not involve a significant increase in the probability or consequences of accidents previously considered and does not 2je involve a significant decrease in a safety margin, the change does not l.jf

@b involve a significant hazards consideration, (2) there is reasonable assur-ance that the health and safety of the public will not be endangered by

' l operation in the proposed manner, and (3) such activities will be conducted 1

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in compliance with the Commission's regulations and the issuance of this amendment will not be inimical to the common defense and security or to y,!'

the health and safety of the public.

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Date: May 19, 1976

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