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{{#Wiki_filter:_____.-                                   .         . . . _ - . -   . - - -   _
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-
    ,'
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        y      ,'c         g                 NUCLEAR REGULATORY COMMISSION
- - - -
i-     E               :                                       REGloN IV                                                  4
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                                                                                                                            1
*
        *,                                            611 RYAN PLAZA DRIVE. SUITE 400
j
                                                        ARUNGToN TEXAS 76011 8064
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          %
UNITED STATES
            ***** '                                       February 5, 1998
y
                EA 97-589
,'c
              . Charles M. Dugger, Vice President
g
                Operations - Waterford 3
NUCLEAR REGULATORY COMMISSION
                Entergy Operations, Inc.'
,'
                P.O. Box B
REGloN IV
              ~ Killona, Louisiana 70066
i-
                SUBJECT:         NOTICE OF V80LATION (NRC INSPECTION REPORT 50 382/97-26)
E
                Dear Mr Dugger:
:
                This refers to the predecisional enforcement comvence conducted January 23,1998, in the
4
                NRC's Arlington, Texas office.' The conference was conducted to discuss several apparent
1
                violations related to a November 1997 incident involving a mispositioned valve controller in the
*
                auxiliary component cooling water system at the Waterford Steam Electric Station,
611 RYAN PLAZA DRIVE. SUITE 400
                Unit 3 (Waterford 3). The apparent violations were identified during an NRC inspection that
,
                concluded on December 15,1997, when the inspection findings were conveyed to Entergy
%
                . Operations, Inc. (Entergy) by telephone, ard were documented in the subject inspection report ;
ARUNGToN TEXAS 76011 8064
                on January 5,1998.
***** '
                Based on the information developed during the inspection, and our consideration of the -
February 5, 1998
                information that you provided during the conference, the NRC has determined that violations of           ,
EA 97-589
                  NRC requirements occurred. These violations are cited in the enclosed Notice of                             ;
. Charles M. Dugger, Vice President
                Violation (Notice) and the circumstances surrounding them were described in detail in the
Operations - Waterford 3
                  subject inspection report in brief, the violations are related to a failure to retum the controller for
Entergy Operations, Inc.'
                  Valve ACC-126A to automatic operation following its use on November 9,1997,- an error which
P.O. Box B
' .
~ Killona, Louisiana 70066
                  went unrecognized for 15 hours despite several control board walkdowns by operators and a                   1
SUBJECT:
                  shift tumover. The failure to retum this valve to automatic rendered Train A of the auxiliary
NOTICE OF V80LATION (NRC INSPECTION REPORT 50 382/97-26)
                  component cooling water system inoperable. Operators compounded this error by removing
Dear Mr Dugger:
                  Train B of the auxiliary component cooling water system from service for routine maintenance on
This refers to the predecisional enforcement comvence conducted January 23,1998, in the
                  November 10,1997, without first physically verifying the operability of Train A. Both trains of this
NRC's Arlington, Texas office.' The conference was conducted to discuss several apparent
                  system remained inoperable for approximately 7.5 hours. The problem was ultimately corrected
violations related to a November 1997 incident involving a mispositioned valve controller in the
                  on November 10,1997, when a relief opt rator walked down the control boards and discovered
auxiliary component cooling water system at the Waterford Steam Electric Station,
                  the mispositioned valve. Train A was imn ediately restored to service.
Unit 3 (Waterford 3). The apparent violations were identified during an NRC inspection that
                  The violations include the procedural error that resulted in the mispositioned valve controller, the
concluded on December 15,1997, when the inspection findings were conveyed to Entergy
                  failure to verify the operability of Train A before taking Train B out of service, and the failure to .
. Operations, Inc. (Entergy) by telephone, ard were documented in the subject inspection report ;
                  discover the mispositioned controller during control board walkdowns and shift turnover. We
on January 5,1998.
                  recognize that the Waterford-3 auxiliary component cooling water system, which supports the
Based on the information developed during the inspection, and our consideration of the -
                  component cooling water system, may not have been necessary to support the safety function
information that you provided during the conference, the NRC has determined that violations of
                  of the ultimate heat sink, given the meteorological conditions that existed at the time of this
,
                  incident, and the likelihood that operators could have restored Train A operability after receiving
NRC requirements occurred. These violations are cited in the enclosed Notice of
                                                                                                      !
;
            9902090163 990205
Violation (Notice) and the circumstances surrounding them were described in detail in the
            PDR
subject inspection report in brief, the violations are related to a failure to retum the controller for
            G
Valve ACC-126A to automatic operation following its use on November 9,1997,- an error which
                        ADOCK 05000382
'
                                        PDR
.
                                                                      * * * * *             Ah.        I
went unrecognized for 15 hours despite several control board walkdowns by operators and a
                                                                                                            5
1
shift tumover. The failure to retum this valve to automatic rendered Train A of the auxiliary
component cooling water system inoperable. Operators compounded this error by removing
Train B of the auxiliary component cooling water system from service for routine maintenance on
November 10,1997, without first physically verifying the operability of Train A. Both trains of this
system remained inoperable for approximately 7.5 hours. The problem was ultimately corrected
on November 10,1997, when a relief opt rator walked down the control boards and discovered
the mispositioned valve. Train A was imn ediately restored to service.
The violations include the procedural error that resulted in the mispositioned valve controller, the
failure to verify the operability of Train A before taking Train B out of service, and the failure to .
discover the mispositioned controller during control board walkdowns and shift turnover. We
recognize that the Waterford-3 auxiliary component cooling water system, which supports the
component cooling water system, may not have been necessary to support the safety function
of the ultimate heat sink, given the meteorological conditions that existed at the time of this
incident, and the likelihood that operators could have restored Train A operability after receiving
h.
!
9902090163 990205
5
PDR
ADOCK 05000382
* * * * *
A
I
G
PDR


                                                                                                                                    . - _ - _ _ _
... . . . _.
                                                          .
.
  ... . . . _.   .
.
r               -
. - _ - _ _ _
  .
r
                    Entergy Operations, Inc.                               2-
-
                    a h!gh temperature alarm on the component cooling water system. The NRC also recognizes
.
                - that no audible or visible alarms were triggered as a result of the controller being in the wrong
Entergy Operations, Inc.
                    position. Nonetheless, these violations are safety significant because a safety system which is
2-
                    designed to remove heat under certain accident conditions, and which was required to be
a h!gh temperature alarm on the component cooling water system. The NRC also recognizes
                    operable at the time, was rendered incapable of operating automatically as designed, in =
- that no audible or visible alarms were triggered as a result of the controller being in the wrong
                    addition, as discussed at some !sngth during the conference, corrective actions for prevbus, .
position. Nonetheless, these violations are safety significant because a safety system which is
                    similar events involving mispositioned switches and valves (NRC inspection report 50-382/96 ;
designed to remove heat under certain accident conditions, and which was required to be
                    13) were not effectively implemented in this case, as evidenced by the many missed
operable at the time, was rendered incapable of operating automatically as designed, in =
                    opportunities to have discovered this error eariier,
addition, as discussed at some !sngth during the conference, corrective actions for prevbus, .
                    Accordingly, these violations are classified in the aggregate as a Severity Level lil problem in
similar events involving mispositioned switches and valves (NRC inspection report 50-382/96 ;
                    accordance with the "Genorcl Statement of Policy and Procedure for NRC Enforcement Actions"
13) were not effectively implemented in this case, as evidenced by the many missed
                    (Enforcement Policy) NUREG-1600.' In accordance with the Enforcement Policy, a civil penaIty
opportunities to have discovered this error eariier,
                    with a base value of $55,000 is considered for a Seventy Level lli problem. Because your . _
Accordingly, these violations are classified in the aggregate as a Severity Level lil problem in
                    facility has been the subject of escalated enforcement actions within the last two years l the
accordance with the "Genorcl Statement of Policy and Procedure for NRC Enforcement Actions"
                    NRC considered whether credit was warranted for identification and Corrective Action in
(Enforcement Policy) NUREG-1600.' In accordance with the Enforcement Policy, a civil penaIty
                    accordance with the civil penalty assessment process in Section VI B.2 of the Enforcement
with a base value of $55,000 is considered for a Seventy Level lli problem. Because your . _
                    Policy. Given that the mispositioned valve controller was discovered by a Waterford-3 operator
facility has been the subject of escalated enforcement actions within the last two years l the
                    and not revealed by an event, and that the failures to identify the error earlier also were
NRC considered whether credit was warranted for identification and Corrective Action in
                    discovered by Entergy, the NRC concludes that credit for identification is warranted; We also
accordance with the civil penalty assessment process in Section VI B.2 of the Enforcement
                    conclude that credit for corrective actions is warranted, Your corrective actions included:
Policy. Given that the mispositioned valve controller was discovered by a Waterford-3 operator
                                                                                                                                                  I
and not revealed by an event, and that the failures to identify the error earlier also were
                  - immediate action to restore system operability and walk down all control boards; debrief of all
discovered by Entergy, the NRC concludes that credit for identification is warranted; We also
                    operators on duty when ACC-126A was mispositioned; meetings with all shift personnel to .
conclude that credit for corrective actions is warranted, Your corrective actions included:
                    reinforce expectations for walkdowns and shift tumover; procedural revision to eliminate two                                 y
I
                      actions in one step in OP-002-001; implementation of control board assessments by shift
- immediate action to restore system operability and walk down all control boards; debrief of all
                    technical advisor during shift tumover; enhancement of shift tumover control board walkdown
operators on duty when ACC-126A was mispositioned; meetings with all shift personnel to .
                    _ procedure; and plans for a corrective action effectiveness review within six months.
reinforce expectations for walkdowns and shift tumover; procedural revision to eliminate two
                      Therefore, to encourage identification and comprehensive correction of violations before events
y
                    - occur, I have been authorized, after consultation with the Director, Office of Enforcement, not to
actions in one step in OP-002-001; implementation of control board assessments by shift
                      assess a civil penalty in this case. However, significant violations of this nature in the future
technical advisor during shift tumover; enhancement of shift tumover control board walkdown
                      could result in a civil penalty.
_ procedure; and plans for a corrective action effectiveness review within six months.
                      You are required to respond to this letter and should follow the instructions specified in the
Therefore, to encourage identification and comprehensive correction of violations before events
                      enclosed Notice when preparing your response The NRC will use your response, in part, to
- occur, I have been authorized, after consultation with the Director, Office of Enforcement, not to
                      determine whether further enforcement action is necessary to ensure compliance with regulatory
assess a civil penalty in this case. However, significant violations of this nature in the future
                    -requirements.
could result in a civil penalty.
                          'For example, a $50.000 cml peratty was ,ssued March 28,1996 (EA 96-025), a $50,000 civil penalty was issued
You are required to respond to this letter and should follow the instructions specified in the
                      December 26.1996 (EA 96-255); and a $55.000 cwil penalty was issued May 9,1997 (EA 97-099).
enclosed Notice when preparing your response The NRC will use your response, in part, to
            . .
determine whether further enforcement action is necessary to ensure compliance with regulatory
-requirements.
'For example, a $50.000 cml peratty was ,ssued March 28,1996 (EA 96-025), a $50,000 civil penalty was issued
December 26.1996 (EA 96-255); and a $55.000 cwil penalty was issued May 9,1997 (EA 97-099).
. .


                                                                                        __ _ . _ _ _
.
.  . ,
. ,
        .
__
        .
_ . _ _ _
                Entergy Operations, Inc.                               3-
.
                In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter, its
.
              enclosure, and your response will be placed in the NRC Public Document Room (PDR).
Entergy Operations, Inc.
                                                                    Sincerely,
3-
                                                                              '
In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter, its
                                                                    Ellis W.
enclosure, and your response will be placed in the NRC Public Document Room (PDR).
                                                                    Regional Admi trator
Sincerely,
                Docket No.: 50-382
'
                License No.: NPF 38
Ellis W.
                Enclosure: Notice of Violation
Regional Admi
                cc w/ Enclosure:
trator
                  Executive Vice President and
Docket No.: 50-382
                            Chief Operating Officer
License No.: NPF 38
                  Entergy Operations, Inc.
Enclosure: Notice of Violation
                  P.O. Box 31995
cc w/ Enclosure:
                  Jackson, Mississippi 39286-1995
Executive Vice President and
                Vice President, Operations Support
Chief Operating Officer
                  Entergy Operations, Inc.
Entergy Operations, Inc.
                  P.O. Box 31995
P.O. Box 31995
                  Jackson, Mississippi 39286-1995
Jackson, Mississippi 39286-1995
                  Wise, Carter, Child & Caraway
Vice President, Operations Support
                  P.O. Box 651
Entergy Operations, Inc.
                  Jackson, Mississippi 39205
P.O. Box 31995
  .
Jackson, Mississippi 39286-1995
                    General Manager, Plant Operations
Wise, Carter, Child & Caraway
                  Waterford 3 SES
P.O. Box 651
                    Entergy Operations, Inc.
Jackson, Mississippi 39205
                    P.O. Box B
.
                    Killona, Louisiana 70066
General Manager, Plant Operations
                      Manager - Licensing Manager
Waterford 3 SES
                    Waterford 3 SES
Entergy Operations, Inc.
                      Entergy Operations, Inc.
P.O. Box B
                      P.O. Bo.y B
Killona, Louisiana 70066
                        Killona, Louisiana 70066
Manager - Licensing Manager
          _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - . _ - _ _ _ _ _ _ _
Waterford 3 SES
Entergy Operations, Inc.
P.O. Bo.y B
Killona, Louisiana 70066
_ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - . _ - _ _ _ _ _ _ _


                                                      - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _
- _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _
  .
.
  .
.
            Entergy Operations, Inc.                                                           -4-
Entergy Operations, Inc.
            Chairman
-4-
            Louisiana Public Service Commission
Chairman
            One American Place, Suite 1830
Louisiana Public Service Commission
            Baton Rouge, Louisiana 70825-1697
One American Place, Suite 1830
            Director, Nuclear Safety &
Baton Rouge, Louisiana 70825-1697
            Regulatory Affairs
Director, Nuclear Safety &
            Waterford 3 SES
Regulatory Affairs
            Entergy Operations, Inc.
Waterford 3 SES
            P.O. Box B
Entergy Operations, Inc.
            Killona, Louisiana 70066
P.O. Box B
            William H. Spell, Administrator
Killona, Louisiana 70066
            Louisiana Radiation Protection Division
William H. Spell, Administrator
            P,0. Box 82135
Louisiana Radiation Protection Division
            Baton Rouge, Louisiana 70884-2135                                                                           '
P,0. Box 82135
            Parish President
Baton Rouge, Louisiana 70884-2135
            St. Charles Parish
'
            P.O. Box 302
Parish President
            Hahnville, Louisiana 70057
St. Charles Parish
P.O. Box 302
Hahnville, Louisiana 70057
1
1
            Mr. William A. Cross
Mr. William A. Cross
            Bethesda Licensing Office
Bethesda Licensing Office
            3 Metro Center
3 Metro Center
            Suite 610
Suite 610
            Bethesda, Maryland 20814
Bethesda, Maryland 20814
            Winston & Strawn
Winston & Strawn
            1400 L Street, N.W.
1400 L Street, N.W.
            Washington, D.C. 20005-3502
Washington, D.C. 20005-3502
-
. -
-
-
    . - -
.
          .            _ _ _ _ _ _ _ . - _ _ . - - -
_ _ _ _ _ _ _ . - _ _ . - - -


                                                                                        __ _-_-__ -
__ _-_-__ -
  4
4
.
.
    Entergy Operations, Inc.                                       -5-
Entergy Operations, Inc.
    bec w/ Enclosure:
-5-
    PDR                                                         IE 14
bec w/ Enclosure:
    LPDR                                                         NUDOCS
PDR
    SECY                                                         EC's: RI, Ril, Rlli
IE 14
    CA.                                                         PA (0-2G4)
LPDR
    EDO (0-17G21)                                               . OlG (T-SD28)
NUDOCS
    DEDO (0-17G21)                                               LIEBERMAN, OE (0-7H5)
SECY
    OE.EAFile (0-7H5)                                           01 (0-3E4)
EC's: RI, Ril, Rlli
    CHANDLER, OGC (0-15E 18)                                     GOLDBERG, OGC (0-15B18)
CA.
    COLLINS, NRR (0-12G18)                                       ZIMMERMAN, NRR/ADP (0-12G18)
PA (0-2G4)
    WIGGINTON, NRR                                               OC/DAF (T-9E10)
EDO (0-17G21)
    OC/LFDCB (T-9E10)                                           AEOD (T-4D18)
. OlG (T-SD28)
    RA Reading File                                               GSanborn-EAFile                                     7
DEDO (0-17G21)
                                                                                                                      s
LIEBERMAN, OE (0-7H5)
    RIV Files                                                     MIS Coordinator
OE.EAFile (0-7H5)
    PAO-Henderson
01 (0-3E4)
    RSLO-Hackney
CHANDLER, OGC (0-15E 18)
    HARRELL
GOLDBERG, OGC (0-15B18)
    E-Mall DISTRIBUTION:
COLLINS, NRR (0-12G18)
    OEMAIL                                                               JDyer (JED2)
ZIMMERMAN, NRR/ADP (0-12G18)
    TPGwynn (TPG)                                                       WBrown (WLB)
WIGGINTON, NRR
    GSanborn (GFS)                                                       GMVasquez (GMV)
OC/DAF (T-9E10)
    BHenderson (BWH)                                                     CHackney (CAH)
OC/LFDCB (T-9E10)
    Art Howell(ATH)                                                     DChamberlain (DDC)
AEOD (T-4D18)
    KPerkins (KEP)                                                       Harrell(PHH)
7
    KBrockman (KEB)                                                     Pellet (JLP)
RA Reading File
    DOCUMENT                     ME: G:\EA\ CASES \WAT3ACCW\EA97589.DFT
GSanborn-EAFile
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Latest revision as of 04:00, 8 December 2024

Discusses Predecisional EC Conducted 980123 Re Insp Rept 50-382/97-26 on 971215 & Forwards NOV Re Failure to Return Controller for Valve ACC-126A to Automatic Operation Following Use on 971109
ML20199L262
Person / Time
Site: Waterford Entergy icon.png
Issue date: 02/05/1998
From: Merschoff E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Dugger C
ENTERGY OPERATIONS, INC.
Shared Package
ML20199L269 List:
References
50-382-97-26, EA-97-589, NUDOCS 9802090163
Download: ML20199L262 (5)


See also: IR 05000382/1997026

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGloN IV

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611 RYAN PLAZA DRIVE. SUITE 400

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ARUNGToN TEXAS 76011 8064

          • '

February 5, 1998

EA 97-589

. Charles M. Dugger, Vice President

Operations - Waterford 3

Entergy Operations, Inc.'

P.O. Box B

~ Killona, Louisiana 70066

SUBJECT:

NOTICE OF V80LATION (NRC INSPECTION REPORT 50 382/97-26)

Dear Mr Dugger:

This refers to the predecisional enforcement comvence conducted January 23,1998, in the

NRC's Arlington, Texas office.' The conference was conducted to discuss several apparent

violations related to a November 1997 incident involving a mispositioned valve controller in the

auxiliary component cooling water system at the Waterford Steam Electric Station,

Unit 3 (Waterford 3). The apparent violations were identified during an NRC inspection that

concluded on December 15,1997, when the inspection findings were conveyed to Entergy

. Operations, Inc. (Entergy) by telephone, ard were documented in the subject inspection report ;

on January 5,1998.

Based on the information developed during the inspection, and our consideration of the -

information that you provided during the conference, the NRC has determined that violations of

,

NRC requirements occurred. These violations are cited in the enclosed Notice of

Violation (Notice) and the circumstances surrounding them were described in detail in the

subject inspection report in brief, the violations are related to a failure to retum the controller for

Valve ACC-126A to automatic operation following its use on November 9,1997,- an error which

'

.

went unrecognized for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> despite several control board walkdowns by operators and a

1

shift tumover. The failure to retum this valve to automatic rendered Train A of the auxiliary

component cooling water system inoperable. Operators compounded this error by removing

Train B of the auxiliary component cooling water system from service for routine maintenance on

November 10,1997, without first physically verifying the operability of Train A. Both trains of this

system remained inoperable for approximately 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The problem was ultimately corrected

on November 10,1997, when a relief opt rator walked down the control boards and discovered

the mispositioned valve. Train A was imn ediately restored to service.

The violations include the procedural error that resulted in the mispositioned valve controller, the

failure to verify the operability of Train A before taking Train B out of service, and the failure to .

discover the mispositioned controller during control board walkdowns and shift turnover. We

recognize that the Waterford-3 auxiliary component cooling water system, which supports the

component cooling water system, may not have been necessary to support the safety function

of the ultimate heat sink, given the meteorological conditions that existed at the time of this

incident, and the likelihood that operators could have restored Train A operability after receiving

h.

!

9902090163 990205

5

PDR

ADOCK 05000382

  • * * * *

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PDR

... . . . _.

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-

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Entergy Operations, Inc.

2-

a h!gh temperature alarm on the component cooling water system. The NRC also recognizes

- that no audible or visible alarms were triggered as a result of the controller being in the wrong

position. Nonetheless, these violations are safety significant because a safety system which is

designed to remove heat under certain accident conditions, and which was required to be

operable at the time, was rendered incapable of operating automatically as designed, in =

addition, as discussed at some !sngth during the conference, corrective actions for prevbus, .

similar events involving mispositioned switches and valves (NRC inspection report 50-382/96 ;

13) were not effectively implemented in this case, as evidenced by the many missed

opportunities to have discovered this error eariier,

Accordingly, these violations are classified in the aggregate as a Severity Level lil problem in

accordance with the "Genorcl Statement of Policy and Procedure for NRC Enforcement Actions"

(Enforcement Policy) NUREG-1600.' In accordance with the Enforcement Policy, a civil penaIty

with a base value of $55,000 is considered for a Seventy Level lli problem. Because your . _

facility has been the subject of escalated enforcement actions within the last two years l the

NRC considered whether credit was warranted for identification and Corrective Action in

accordance with the civil penalty assessment process in Section VI B.2 of the Enforcement

Policy. Given that the mispositioned valve controller was discovered by a Waterford-3 operator

and not revealed by an event, and that the failures to identify the error earlier also were

discovered by Entergy, the NRC concludes that credit for identification is warranted; We also

conclude that credit for corrective actions is warranted, Your corrective actions included:

I

- immediate action to restore system operability and walk down all control boards; debrief of all

operators on duty when ACC-126A was mispositioned; meetings with all shift personnel to .

reinforce expectations for walkdowns and shift tumover; procedural revision to eliminate two

y

actions in one step in OP-002-001; implementation of control board assessments by shift

technical advisor during shift tumover; enhancement of shift tumover control board walkdown

_ procedure; and plans for a corrective action effectiveness review within six months.

Therefore, to encourage identification and comprehensive correction of violations before events

- occur, I have been authorized, after consultation with the Director, Office of Enforcement, not to

assess a civil penalty in this case. However, significant violations of this nature in the future

could result in a civil penalty.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response The NRC will use your response, in part, to

determine whether further enforcement action is necessary to ensure compliance with regulatory

-requirements.

'For example, a $50.000 cml peratty was ,ssued March 28,1996 (EA 96-025), a $50,000 civil penalty was issued

December 26.1996 (EA 96-255); and a $55.000 cwil penalty was issued May 9,1997 (EA 97-099).

. .

.

. ,

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.

.

Entergy Operations, Inc.

3-

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter, its

enclosure, and your response will be placed in the NRC Public Document Room (PDR).

Sincerely,

'

Ellis W.

Regional Admi

trator

Docket No.: 50-382

License No.: NPF 38

Enclosure: Notice of Violation

cc w/ Enclosure:

Executive Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, Mississippi 39286-1995

Vice President, Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, Mississippi 39286-1995

Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, Mississippi 39205

.

General Manager, Plant Operations

Waterford 3 SES

Entergy Operations, Inc.

P.O. Box B

Killona, Louisiana 70066

Manager - Licensing Manager

Waterford 3 SES

Entergy Operations, Inc.

P.O. Bo.y B

Killona, Louisiana 70066

_ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ - . _ - _ _ _ _ _ _ _

- _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _

.

.

Entergy Operations, Inc.

-4-

Chairman

Louisiana Public Service Commission

One American Place, Suite 1830

Baton Rouge, Louisiana 70825-1697

Director, Nuclear Safety &

Regulatory Affairs

Waterford 3 SES

Entergy Operations, Inc.

P.O. Box B

Killona, Louisiana 70066

William H. Spell, Administrator

Louisiana Radiation Protection Division

P,0. Box 82135

Baton Rouge, Louisiana 70884-2135

'

Parish President

St. Charles Parish

P.O. Box 302

Hahnville, Louisiana 70057

1

Mr. William A. Cross

Bethesda Licensing Office

3 Metro Center

Suite 610

Bethesda, Maryland 20814

Winston & Strawn

1400 L Street, N.W.

Washington, D.C. 20005-3502

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4

.

Entergy Operations, Inc.

-5-

bec w/ Enclosure:

PDR

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LPDR

NUDOCS

SECY

EC's: RI, Ril, Rlli

CA.

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01 (0-3E4)

CHANDLER, OGC (0-15E 18)

GOLDBERG, OGC (0-15B18)

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ZIMMERMAN, NRR/ADP (0-12G18)

WIGGINTON, NRR

OC/DAF (T-9E10)

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7

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SAN $1DF3h N

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