ML20249B191: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:(    _--
{{#Wiki_filter:_-
o          _-
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(
                                                ,,,,                        ,pMMVE)                 . March 18, 1976 PRELIMINARY NOTIFICATION OF EVE!           R   ;U UAL     CUR E         --PNO-76-45     W This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information
o
  ~                        presented in as initially received without verification or evaluation and is basically all that is knoun by OIE staff as of 4:00 p.m. on date of this notification. IT S!!OULD BE SPECIFICALLY HOTED THAT THIS NOTIFICATION MAY CONTAIN INFOPJIAT]ON THAT LATER MAY BE DATERMINED TO BE INACCURATE OR' INCO: SISTENT. AN OFFICE OF INSPECTION AND ENFORCEMENT NOTIFICATION OF AN IUCIDENT OR OCCURRENCE (BLUE SHEET) SUBSEQUENTLY WILL BE ISSUED IF WARRAUTED.
,pMMVE)
Facility:     Pacific Gas & Electric Company Humboldt Bay Unit No. 3
. March 18, 1976 PRELIMINARY NOTIFICATION OF EVE!
R
;U UAL CUR E
--PNO-76-45 W
This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance.
The information presented in as initially received without verification or evaluation
~
and is basically all that is knoun by OIE staff as of 4:00 p.m. on date of this notification.
IT S!!OULD BE SPECIFICALLY HOTED THAT THIS NOTIFICATION MAY CONTAIN INFOPJIAT]ON THAT LATER MAY BE DATERMINED TO BE INACCURATE OR' INCO: SISTENT. AN OFFICE OF INSPECTION AND ENFORCEMENT NOTIFICATION OF AN IUCIDENT OR OCCURRENCE (BLUE SHEET) SUBSEQUENTLY WILL BE ISSUED IF WARRAUTED.
Facility:
Pacific Gas & Electric Company Humboldt Bay Unit No. 3


==Subject:==
==Subject:==
Crack in 2-Inch Diameter Suction Piping of Reactor Cleanup System A circumferential crack, approximately one inch in length, was found in the heat affected zone of a socket veld in the 2 inch diameter stainless steel suction piping of the reactor cicanup system. The reactor was                         .
Crack in 2-Inch Diameter Suction Piping of Reactor Cleanup System A circumferential crack, approximately one inch in length, was found in the heat affected zone of a socket veld in the 2 inch diameter stainless steel suction piping of the reactor cicanup system. The reactor was shutdown at 0150 3/17/76 due to an abnormal increase in coolant leakage which had risen to 11.8 GPH. An inspection of piping inside the drywell during a subsequent hydrostatic test of the reactor coolant system disclosed the crack at approximately 7:00 pm on 3/17/76. A " soft patch" was applied to secure the leakage, which is unisolable from the reactor j
shutdown at 0150 3/17/76 due to an abnormal increase in coolant leakage which had risen to 11.8 GPH. An inspection of piping inside the drywell during a subsequent hydrostatic test of the reactor coolant system disclosed the crack at approximately 7:00 pm on 3/17/76. A " soft patch" was applied to secure the leakage, which is unisolable from the reactor j                   coolant system. An investigation of the problem and possible means of repair is underway by licensee personnel. The technical specification limit for primary coolant Icakage is 1 gpm (60 gallons per hour).
coolant system. An investigation of the problem and possible means of repair is underway by licensee personnel.
The technical specification limit for primary coolant Icakage is 1 gpm (60 gallons per hour).
A Region V inspector has been dispatched to the site.
A Region V inspector has been dispatched to the site.
It is expected that the Humboldt Plant will remain shutdown at least a week. The licensee and Region V are planning to issue press releases.                       #
It is expected that the Humboldt Plant will remain shutdown at least a week. The licensee and Region V are planning to issue press releases.
Hedia interest is expected in California because of awareness generated                       / j by the nuclear moratorium referendum.
Hedia interest is expected in California because of awareness generated
Region V (Walnut Creek,.CA) received notification of this occurrence by telephon'e from the Plant Superintendent at 9:00 a.m. on March 18, 1976.                                                                                           f
/
j by the nuclear moratorium referendum.
Region V (Walnut Creek,.CA) received notification of this occurrence by telephon'e from the Plant Superintendent at 9:00 a.m. on March 18, f
1976.


==Contact:==
==Contact:==
RFWarnick,     IE x27261       GWRoy,     IE x27261           DThompson, IE x27541
RFWarnick, IE x27261
    ?
: GWRoy, IE x27261 DThompson, IE x27541
?
Distribution:
Distribution:
Chairman Anders                 Commissioner Mason                 S. J. Chilk, SECY l
Chairman Anders Commissioner Mason S. J. Chilk, SECY Commissioner Gilinsky Commissioner Rowden G. F. Murphy, JCAE l
Commissioner Gilinsky           Commissioner Rowden               G. F. Murphy, JCAE i              -
Commissioner Kennedy C. C. Kammerer, CA i
Commissioner Kennedy             C. C. Kammerer, CA 1                  L. V. Gossick,                   J. C. Davis, OIE                   J. A. Harris, PA B. C. Rusche, NRR               J. La Fleur, ISP K. R. Chapman, NMSS T. J. McTiernc7, AIA H. K. Shapar, ELD l                   Transmitted:     P Bldg /4 /f/[d   H St M//f,,; MNBBh[r
L. V. Gossick, J. C. Davis, OIE J. A. Harris, PA 1
                                                                                              ;  Luge /h.((
B. C. Rusche, NRR J. La Fleur, ISP T. J. McTiernc7, AIA K. R. Chapman, NMSS H. K. Shapar, ELD l
i I
Transmitted:
!                    . j2     PRELIMINARY NOTIFICATION - NOT FOR PUBLIC DISCLOSURE l                 990&t20153 760318                                                                           _      17
P Bldg 4 /f/[d H St M//f,,; MNBBh[r
!                PDR   ISE PNO-76-045         PDR                                                     -}}
/
Luge /h.((
I i
j2 PRELIMINARY NOTIFICATION - NOT FOR PUBLIC DISCLOSURE l
17 990&t20153 760318 PDR ISE PNO-76-045 PDR
-}}

Latest revision as of 14:08, 30 November 2024

PNO-76-045:on 760317,reactor Was Shutdown Due to Abnormal Increase in Coolant Leakage Which Had Risen to 11.8 Gph.Insp of Piping Inside Drywell Disclosed Crack.Soft Patch Was Applied to Secure Leakage
ML20249B191
Person / Time
Site: Humboldt Bay
Issue date: 03/18/1976
From: Roy G, Thompson D, Warnick R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
To:
References
PNO-76-045, PNO-76-45, NUDOCS 9806220153
Download: ML20249B191 (1)


Text

_-

~veme

(

o

,pMMVE)

. March 18, 1976 PRELIMINARY NOTIFICATION OF EVE!

R

U UAL CUR E

--PNO-76-45 W

This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance.

The information presented in as initially received without verification or evaluation

~

and is basically all that is knoun by OIE staff as of 4:00 p.m. on date of this notification.

IT S!!OULD BE SPECIFICALLY HOTED THAT THIS NOTIFICATION MAY CONTAIN INFOPJIAT]ON THAT LATER MAY BE DATERMINED TO BE INACCURATE OR' INCO: SISTENT. AN OFFICE OF INSPECTION AND ENFORCEMENT NOTIFICATION OF AN IUCIDENT OR OCCURRENCE (BLUE SHEET) SUBSEQUENTLY WILL BE ISSUED IF WARRAUTED.

Facility:

Pacific Gas & Electric Company Humboldt Bay Unit No. 3

Subject:

Crack in 2-Inch Diameter Suction Piping of Reactor Cleanup System A circumferential crack, approximately one inch in length, was found in the heat affected zone of a socket veld in the 2 inch diameter stainless steel suction piping of the reactor cicanup system. The reactor was shutdown at 0150 3/17/76 due to an abnormal increase in coolant leakage which had risen to 11.8 GPH. An inspection of piping inside the drywell during a subsequent hydrostatic test of the reactor coolant system disclosed the crack at approximately 7:00 pm on 3/17/76. A " soft patch" was applied to secure the leakage, which is unisolable from the reactor j

coolant system. An investigation of the problem and possible means of repair is underway by licensee personnel.

The technical specification limit for primary coolant Icakage is 1 gpm (60 gallons per hour).

A Region V inspector has been dispatched to the site.

It is expected that the Humboldt Plant will remain shutdown at least a week. The licensee and Region V are planning to issue press releases.

Hedia interest is expected in California because of awareness generated

/

j by the nuclear moratorium referendum.

Region V (Walnut Creek,.CA) received notification of this occurrence by telephon'e from the Plant Superintendent at 9:00 a.m. on March 18, f

1976.

Contact:

RFWarnick, IE x27261

GWRoy, IE x27261 DThompson, IE x27541

?

Distribution:

Chairman Anders Commissioner Mason S. J. Chilk, SECY Commissioner Gilinsky Commissioner Rowden G. F. Murphy, JCAE l

Commissioner Kennedy C. C. Kammerer, CA i

L. V. Gossick, J. C. Davis, OIE J. A. Harris, PA 1

B. C. Rusche, NRR J. La Fleur, ISP T. J. McTiernc7, AIA K. R. Chapman, NMSS H. K. Shapar, ELD l

Transmitted:

P Bldg 4 /f/[d H St M//f,,; MNBBh[r

/

Luge /h.((

I i

j2 PRELIMINARY NOTIFICATION - NOT FOR PUBLIC DISCLOSURE l

17 990&t20153 760318 PDR ISE PNO-76-045 PDR

-