ML20009F730: Difference between revisions

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Latest revision as of 07:35, 28 February 2020

Forwards LERs 81-019/01T-0,81-023/01T-0 & 81-025/01T-0
Date released: 01/23/2020 Download: ML20009F730


LER 81-025/01T-0:on 810710,analyses of Main Feedwater Indicated That Three RCPs Require Min of 500 Gpm of Auxiliary Feedwater Flow to Meet FSAR Spec.Caused by Updating of FSAR Analysis
ML20009F755
Person / Time
Site: Surry Dominion icon.png
Issue date: 07/21/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML20009F755 (3)
LER 81-023/01T-0:on 810708,delta T Protection Channel T-1-422A Was Found to Indicate Zero.Caused by Incorrect Wiring of Tc & Th RTD Following Design Change.Rtd Wired Correctly
ML20009F751
Person / Time
Site: Surry Dominion icon.png
Issue date: 07/21/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML20009F751 (3)
LER 81-019/01T-0:on 810707,urgent Failure Alarm for Control Rods Occurred,Indicating Rods Were Inoperrable.Caused by Blown Fuse in Power Cabinet.Fuse Replaced
ML20009F744
Person / Time
Site: Surry Dominion icon.png
Issue date: 07/21/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML20009F744 (2)
Forwards LERs 81-019/01T-0,81-023/01T-0 & 81-025/01T-0
ML20009F729
Person / Time
Site: Surry Dominion icon.png
Issue date: 07/21/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: OREILLY J P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML20009F729 (1)