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{{#Wiki_filter:United States Nuclear Regulatory Commission Official Hearing Exhibit In the Matter of
{{#Wiki_filter:United States Nuclear Regulatory Commission Official Hearing Exhibit Entergy Nuclear Operations, Inc.
: Entergy Nuclear Operations, Inc. (Indian Point Nuclear Generating Units 2 and 3)
In the Matter of:
ASLBP #:07-858-03-LR-BD01 Docket #:05000247 l 05000286 Exhibit #:
(Indian Point Nuclear Generating Units 2 and 3) lW\    c.\,Vf\REGCI<.q;. ASLBP #: 07-858-03-LR-BD01                                                                                                   RIV000029 Docket #: 05000247 l 05000286                                                                               Submitted: December 22, 2011 Exhibit #: RIV000029-00-BD01                   Identified: 10/15/2012
Identified:
                            < Admitted: 10/15/2012
Admitted: Withdrawn:
  **o                      0
Rejected: Stricken: Other: RIV000029-00-BD01 10/15/2012 10/15/2012 RIV000029 Submitted: December 22, 2011 c.\,Vf\REGCI<.q;.
                            <                                               Withdrawn:
l W\
  *                   'Y f?j
* 0 * < * < o 'Y f?j ... ",'7 . **** ... Entergy CONDITION REPORT I CR-IP3-2006-02270 Originator:
    ~...",'7 .         ~J'    Rejected:                                        Stricken:
Lizzo,Nicholas lriginator Group: Operations Watch Mgmt Supervisor Name: Cramer,Thomas A Discovered Date: 07/23/200604:49 Condition  
            **** ...             Other:
Entergy                             CONDITION REPORT                             ICR-IP3-2006-02270 Originator: Lizzo,Nicholas                                               Originator Phone: 8277 lriginator Group: Operations Watch Mgmt                                     Operability Required: N ReportabiHty Required: N Supervisor Name: Cramer,Thomas A Discovered Date: 07/23/200604:49                                                   Initiated Date: 07123/200604:58 Condition


==
== Description:==
Description:==


Originator Phone: 8277 Operability Required:
The line downstream of the 1104 valves ("A" reheaters) to 36 FWH shell side is leaking approximately 112 gpm. WRT IP3-06-\8192. Rapid Response activated.
N ReportabiHty Required:
N Initiated Date: 07123/200604:58 The line downstream of the 1104 valves ("A" reheaters) to 36 FWH shell side is leaking approximately 112 gpm. WRT IP3-06-\8192.
Rapid Response activated.
Immediate Action
Immediate Action


== Description:==
== Description:==


SM notified -rapid response activated Suggested Action
SM notified - rapid response activated Suggested Action
 
== Description:==
 
Repair.
EQUIPMENT:
Tag Name                                  Tag Suffix Name Component Code Process System Code 1104                                                                        HD REFERENCE ITEMS:
Type Code                            Description
                                            #LEVEL OF DEFENSE                    Observation KEYWORDS                              leak TEAM3C                                II WON                                  IP3-06-\8\92 TRENDING (For Reference Purposes Only):
Trend Type                                    Trend Code REPORT WEIGHT                                  4 EM                                            MAMM KEYWORDS                                      KW-LEAKS-WATER EFlI IPEC00025699
 
Entergy                I            CORRECTIVE ACTION                                  1CR-IP3-2006-02270 CANumber:
Group                                                Name Assigned By: CRG/CARB/OSRC                                              Harrison,Christine B Assigned To: P&C Eng Codes Mgmt                                        Azevedo,Nelson F Subassigned To: P&C Eng Codes Staff                                          Hartjen,Harry G Originated By: Harrison,Christine B                                        7/2512006 11:27:08 Performed 'By: Azevedo,Nelson F                                            8/15/2006 14:22:53 Sub performed By: Hartjen,Harry G                                              8110/200609:27:02 Approved By:
Closed By: Azevedo,Nelson F                                          8115/200614:22:53 Current Due Date: 08/16/2006                                Initial Due Date: 08/16/2006 CA Type: DISP - CA Plant Constraint: #NONE CA


== Description:==
== Description:==


Repair. EQUIPMENT:
Please review and assign further corrective actions as required.
Tag Name 1104 REFERENCE ITEMS: Type Code #LEVEL OF DEFENSE KEYWORDS TEAM3C WON Tag Suffix Name Component Code Process System Code HD Description Observation leak II IP3-06-\8\92 TRENDING (For Reference Purposes Only): Trend Type REPORT WEIGHT EM KEYWORDS IPEC00025699 Trend Code 4 MAMM KW-LEAKS-WATER EFlI Entergy I CORRECTIVE ACTION CANumber:
 
Group Assigned By: CRG/CARB/OSRC Assigned To: P&C Eng Codes Mgmt Subassigned To: P&C Eng Codes Staff Originated By: Harrison,Christine B Performed
===Response===
'By: Azevedo,Nelson F Sub performed By: Hartjen,Harry G Approved By: Closed By: Azevedo , Nelson F Current Due Date: 08/16/2006 CA Type: DISP -CA Plant Constraint
UTthickness m~asurements were taken around the leaking area on this pipe (UT Report 06UTl71). The thinned area was found to be localized on one side *o fthe pipe which is downsstream of a tee. A pipe clamp (Team Inc.) was installed over the leak and thinned area under work order IP3-06-18192. Leak repair was successful and the leak has stopped. CA 00002 has been issued to review the FAC program and determine if additional inspections .are warrented as a result of this leak.
: #NONE CA Description
  '""Ibresponse :
: Harrison,Christine B Azevedo,Nelson F Hartjen,Harry G 7/2512006 11:27:08 8/15/2006 14: 22: 53 8110/200609
Issued CA#2 Closure Comments:
: 27:02 8115/200614:22:53 Initial Due Date: 08/16/2006 Please review and assign further corrective actions as required.
IPEC00025700
Response:
 
1 CR-IP3-2006-02270 Name UTth i ckness were taken around the leaking area on this pipe (UT Report 06UTl71).
Entergy                 I           CORRECTIVE ACTION                                      ICR-IP3-2006-02270 CANumber:                 2 Group                          *1                      Name Assigned By: P&C Eng Codes Staff                                         Hartjen,Harry G Assigned To: P&C Eng Codes Staff                                         Hartjen,Harry G Subassigned T(} :
The thinned area was found to be localized on one side*ofthe pipe which is downsstream of a tee. A pipe clamp (Team Inc.) was installed over the leak and thinned area under work order IP3-06-18192. Leak repair was successful and the leak has stopped. CA 00002 has been issued to review the F AC program and determine if additional inspections  
Originated By: Hartjen,Harry G                                               8/10/200609:24:00 Performed By: Hartjen,Harry G                                               10/30/2006 II :28:34 Sub performed By:
.are warrented as a result of this leak. '""Ibresponse  
Approved By:
: Issued CA#2 Closure Comments:
CI(}sed By: Hartjen,Harry G                                             10/3012006 11 :28:34 Current Due Date: 10/3112006                                Initial Due Date: 10/3112006 CA Type: ACTION Plant Constraint: #NONE CA
IPEC00025700 Entergy I CANumber:
2 Assigned By: P&C Eng Codes Staff Assigned To: P&C Eng Codes Staff Subassigned T(} : Originated By: Hartjen,Harry G Performed By: Hartjen,Harry G Sub performed By: Approved By: CI(}sed By: Hartjen,Harry G Current Due Date: 10/3112006 CA Type: ACTION Plant Constraint:  
#NONE CA


== Description:==
== Description:==


CORRECTIVE ACTION Group *1 Hartjen,Harry G Hartjen,Harry G 8/10/200609:24
Review both Unit 2 and Unit 3 FAC Programs and determine if similar locations to this leak have been inspected for wall thinning. Also determine if and when additional inspections are required to determine if wall thinning is occuring at these similar locations. If additional inspections are required, incorporate inspections into work week schedule, or FAC Program outage scopes.
: 00 10/30/2006 II :28:34 10/3012006 11 :28:34 Initial Due Date: 10/3112006 I CR-IP3-2006-02270 Name Review both Unit 2 and Unit 3 F AC Programs and determine if similar locations to this leak have been inspected for wall thinning.
 
Also determine if and when additional inspections are required to determine if wall thinning is occuring at these similar locations.
===Response===
If additional inspections are required, incorporate inspections into work week schedule, or F AC Program outage scopes. Response:
A review of both Unit 2 and Unit 3 FAC programs was performed to determine if similar locations to the current Reheater Drain line leak have been inspected for wall thinning and determine if and when additional inspections are required to determine if wall thinning is occurring at these similar locations.
A review of both Unit 2 and Unit 3 F AC programs was performed to determine if similar locations to the current Reheater Drain line leak have been inspected for wall thinning and determine if and when additional inspections are required to determine if wall thinning is occurring at these similar locations.
Review of the Unit 2 FAC inspection history found that all similar locations have been recently inspected or replaced. No additional inspections are recommended for Unit 2 at this time.
Review of the Unit 2 F AC inspection history found that all similar locations have been recently inspected or replaced.
Review of the Unit 3 FAC inspection history found that some similar locations do not have recent inspections and should be inspected. A total of9 additional inspections were identified.
No additional inspections are recommended for Unit 2 at this time. Review of the Unit 3 FAC inspection history found that some similar locations do not have recent inspections and should be inspected. A total of9 additional inspections were identified. Details of this review, along with the recommended additional inspections are attached. No on-line exams are recommended due to the high temperature (385 degrees F) of these components, and the congestion of piping in these areas. Therefore the 9 additional inspections are to be performed during the JR14 refuel outage. CA 3 is issued to generate work orders and 3Rl4 scope add forms for these inspections.
Details of this review, along with the recommended additional inspections are attached.
Subresponse  
No on-line exams are recommended due to the high temperature (385 degrees F) of these components, and the congestion of piping in these areas. Therefore the 9 additional inspections are to be performed during the JR14 refuel outage.
: Closure Comments:
CA 3 is issued to generate work orders and 3Rl4 scope add forms for these inspections.
Subresponse :
Closure Comments:
Attachments:
Attachments:
Resp Description Review of F AC Inspections due to leak in U3 RHD IPEC00025701}}
Resp Description Review of FAC Inspections due to leak in U3 RHD IPEC00025701}}

Latest revision as of 20:19, 11 November 2019

Official Exhibit - RIV000029-00-BD01 - Entergy Condition Report CR-IP3-2006-02270, IPEC00025699 (Entergy CR-IP3-2006-02270)
ML12335A416
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 12/22/2011
From:
Entergy Nuclear Operations
To:
Atomic Safety and Licensing Board Panel
SECY RAS
References
RAS 21601, 50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01
Download: ML12335A416 (3)


Text

United States Nuclear Regulatory Commission Official Hearing Exhibit Entergy Nuclear Operations, Inc.

In the Matter of:

(Indian Point Nuclear Generating Units 2 and 3) lW\ c.\,Vf\REGCI<.q;. ASLBP #: 07-858-03-LR-BD01 RIV000029 Docket #: 05000247 l 05000286 Submitted: December 22, 2011 Exhibit #: RIV000029-00-BD01 Identified: 10/15/2012

< Admitted: 10/15/2012

    • o 0

< Withdrawn:

  • 'Y f?j

~...",'7 . ~J' Rejected: Stricken:

        • ... Other:

Entergy CONDITION REPORT ICR-IP3-2006-02270 Originator: Lizzo,Nicholas Originator Phone: 8277 lriginator Group: Operations Watch Mgmt Operability Required: N ReportabiHty Required: N Supervisor Name: Cramer,Thomas A Discovered Date: 07/23/200604:49 Initiated Date: 07123/200604:58 Condition

Description:

The line downstream of the 1104 valves ("A" reheaters) to 36 FWH shell side is leaking approximately 112 gpm. WRT IP3-06-\8192. Rapid Response activated.

Immediate Action

Description:

SM notified - rapid response activated Suggested Action

Description:

Repair.

EQUIPMENT:

Tag Name Tag Suffix Name Component Code Process System Code 1104 HD REFERENCE ITEMS:

Type Code Description

  1. LEVEL OF DEFENSE Observation KEYWORDS leak TEAM3C II WON IP3-06-\8\92 TRENDING (For Reference Purposes Only):

Trend Type Trend Code REPORT WEIGHT 4 EM MAMM KEYWORDS KW-LEAKS-WATER EFlI IPEC00025699

Entergy I CORRECTIVE ACTION 1CR-IP3-2006-02270 CANumber:

Group Name Assigned By: CRG/CARB/OSRC Harrison,Christine B Assigned To: P&C Eng Codes Mgmt Azevedo,Nelson F Subassigned To: P&C Eng Codes Staff Hartjen,Harry G Originated By: Harrison,Christine B 7/2512006 11:27:08 Performed 'By: Azevedo,Nelson F 8/15/2006 14:22:53 Sub performed By: Hartjen,Harry G 8110/200609:27:02 Approved By:

Closed By: Azevedo,Nelson F 8115/200614:22:53 Current Due Date: 08/16/2006 Initial Due Date: 08/16/2006 CA Type: DISP - CA Plant Constraint: #NONE CA

Description:

Please review and assign further corrective actions as required.

Response

UTthickness m~asurements were taken around the leaking area on this pipe (UT Report 06UTl71). The thinned area was found to be localized on one side *o fthe pipe which is downsstream of a tee. A pipe clamp (Team Inc.) was installed over the leak and thinned area under work order IP3-06-18192. Leak repair was successful and the leak has stopped. CA 00002 has been issued to review the FAC program and determine if additional inspections .are warrented as a result of this leak.

'""Ibresponse :

Issued CA#2 Closure Comments:

IPEC00025700

Entergy I CORRECTIVE ACTION ICR-IP3-2006-02270 CANumber: 2 Group *1 Name Assigned By: P&C Eng Codes Staff Hartjen,Harry G Assigned To: P&C Eng Codes Staff Hartjen,Harry G Subassigned T(} :

Originated By: Hartjen,Harry G 8/10/200609:24:00 Performed By: Hartjen,Harry G 10/30/2006 II :28:34 Sub performed By:

Approved By:

CI(}sed By: Hartjen,Harry G 10/3012006 11 :28:34 Current Due Date: 10/3112006 Initial Due Date: 10/3112006 CA Type: ACTION Plant Constraint: #NONE CA

Description:

Review both Unit 2 and Unit 3 FAC Programs and determine if similar locations to this leak have been inspected for wall thinning. Also determine if and when additional inspections are required to determine if wall thinning is occuring at these similar locations. If additional inspections are required, incorporate inspections into work week schedule, or FAC Program outage scopes.

Response

A review of both Unit 2 and Unit 3 FAC programs was performed to determine if similar locations to the current Reheater Drain line leak have been inspected for wall thinning and determine if and when additional inspections are required to determine if wall thinning is occurring at these similar locations.

Review of the Unit 2 FAC inspection history found that all similar locations have been recently inspected or replaced. No additional inspections are recommended for Unit 2 at this time.

Review of the Unit 3 FAC inspection history found that some similar locations do not have recent inspections and should be inspected. A total of9 additional inspections were identified.

Details of this review, along with the recommended additional inspections are attached.

No on-line exams are recommended due to the high temperature (385 degrees F) of these components, and the congestion of piping in these areas. Therefore the 9 additional inspections are to be performed during the JR14 refuel outage.

CA 3 is issued to generate work orders and 3Rl4 scope add forms for these inspections.

Subresponse :

Closure Comments:

Attachments:

Resp Description Review of FAC Inspections due to leak in U3 RHD IPEC00025701