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 Issue dateTitle
RS-04-160, Request for Amendment to Technical Specifications to Eliminate Requirements to Provide Monthly Operating Reports and Annual Occupational Radiation Exposure Reports21 October 2004Request for Amendment to Technical Specifications to Eliminate Requirements to Provide Monthly Operating Reports and Annual Occupational Radiation Exposure Reports
Information Notice 1999-14, Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick5 May 1999Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick
A98020, Application for Amends to Licenses DPR-39 & DPR-48,to Eliminate License Conditions No Longer Applicable & Replace Existing Operational Custom TS with Permanently Defueled TS2 October 1998Application for Amends to Licenses DPR-39 & DPR-48,to Eliminate License Conditions No Longer Applicable & Replace Existing Operational Custom TS with Permanently Defueled TS
NRC Generic Letter 1998-0228 May 1998NRC Generic Letter 1998-002: Loss of Reactor Coolant Inventory and Associated Potential for Loss of Emergency Mitigation Functions While in a Shutdown Condition
Information Notice 1997-83, Recent Events Involving Reactor Coolant System Inventory Control During Shutdown5 December 1997Recent Events Involving Reactor Coolant System Inventory Control During Shutdown
ML20202H36428 November 1997Proposed Improved TSs Using Guidance Provided in NUREG-1431
ML20199D62510 November 1997Proposed Improved TS Bases Changes & Supporting Info & Final Proposed TS Bases for Section 3.3,including Revised Table of Contents & List of Effective Pages
A97052, Responds to NRC Re Violations Noted in Insp Repts 50-295/97-02,50-304/97-02,50-295/97-07 & 50-304/97-07, Respectively.Corrective Actions:Placed Both Units in Cold Shutdown & Removed Operators Involved in Event1 October 1997Responds to NRC Re Violations Noted in Insp Repts 50-295/97-02,50-304/97-02,50-295/97-07 & 50-304/97-07, Respectively.Corrective Actions:Placed Both Units in Cold Shutdown & Removed Operators Involved in Event
ML20217R2442 September 1997Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $330,000.Violation Noted:Primary Nso Did Not Establish Power at or Less than Point of Adding Heat IAW GOP-4,step 5.21.f
ML20149H99616 July 1997Predecisional Enforcement Conference Rept on 970703.Areas Discussed:Violations Noted in Insp Repts 50-295/97-02, 50-304/97-02,50-295/97-07 & 50-304/97-07 on 970206-0402 & 0312-0428 & Corrective Actions
ML20140G8294 June 1997Insp Repts 50-295/97-02 & 50-304/97-02 on 970206-0402. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
Information Notice 1996-65, Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown11 December 1996Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown
Information Notice 1996-56, Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power22 October 1996Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power
Information Notice 1996-42, Unexpected Opening of Multiple Safety Relief Valves5 August 1996Unexpected Opening of Multiple Safety Relief Valves
Information Notice 1996-37, Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown18 June 1996Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown
Information Notice 1996-05, Partial Bypass of Shutdown Cooling Flow from Reactor Vessel18 January 1996Partial Bypass of Shutdown Cooling Flow from Reactor Vessel
Information Notice 1994-52, Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 115 July 1994Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1
Information Notice 1994-36, Undetected Accumulation of Gas in Reactor Coolant System24 May 1994Undetected Accumulation of Gas in Reactor Coolant System
Information Notice 1993-89, Potential Problems with BWR Level Instrumentation Backfill Modifications26 November 1993Potential Problems with BWR Level Instrumentation Backfill Modifications
Information Notice 1993-62, Thermal Stratification of Water in BWR Reactor Vessels10 August 1993Thermal Stratification of Water in BWR Reactor Vessels
Information Notice 1993-27, Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization8 April 1993Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization
NRC Generic Letter 1992-0419 August 1992NRC Generic Letter 1992-004 - Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in BWRs Pursuant to 10 CFR 50.54(F)
Information Notice 1992-16, Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown25 February 1992Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown
Information Notice 1990-22, Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units23 March 1990Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units
ML20247E7428 September 1989Safety Evaluation Supporting Amends 118 & 107 to Licenses DPR-39 & DPR-48,respectively
IR 05000295/19880169 September 1988Insp Repts 50-295/88-16 & 50-304/88-16 on 880720-0823.No Violations Noted.Major Areas Inspected:Operational Safety Verification & Engineered Safety Feature Sys Walkdown, Surveillance Observation & Maint Observation
ML20235J27125 September 1987Forwards Info Assessing Safe Operation of PWRs When RCS Water Level Below Top of Reactor Vessel,Per Generic Ltr 87-12
ML20205F58919 March 1987Amends 102 & 92 to Licenses DPR-39 & DPR-48,respectively, Revising Tech Specs to Allow Disabling of Rod Control Sys During Periods That Reactor in Mode 3 W/Less than Four Reactor Coolant Pumps Operating
ML20197B12316 October 1986Proposed Tech Specs Re RCS Limiting Conditions for Operation & Surveillance Requirements,Authorizing Disabling of Rod Control Sys When Reactor in Mode 3 W/Less than Four Reactor Coolant Pumps Operating
PNO-III-85-102, on 851214,during Outage,Both Trains of RHR Sys Lost When Water in Reactor Vessel Drained Below Level of Suction Line.Caused by Erroneous Control Room Indication of RCS Configuration Used for Outage16 December 1985PNO-III-85-102:on 851214,during Outage,Both Trains of RHR Sys Lost When Water in Reactor Vessel Drained Below Level of Suction Line.Caused by Erroneous Control Room Indication of RCS Configuration Used for Outage
NRC Generic Letter 1985-0923 May 1985NRC Generic Letter 1985-009: Technical Specifications for Generic Letter 1983-028, Item 4.3
NRC Generic Letter 1985-0823 May 1985NRC Generic Letter 1985-008: 10 CFR 20.408 Termination Reports - Format
NRC Generic Letter 1985-072 May 1985NRC Generic Letter 1985-007: Implementation of Integrated Schedules for Plant Modifications
NRC Generic Letter 1985-0217 April 1985NRC Generic Letter 1985-002: Staff Recommended Actions Stemming from NRC Integrated Program for the Resolution of Unresolved Safety Issues Regarding Steam Generator Tube Integrity
NRC Generic Letter 1985-0531 January 1985NRC Generic Letter 1985-005: Inadvertent Boron Dilution Events
ML03115058529 January 1985Withdrawn NRC Generic Letter 1985-004: Operator Licensing Examinations