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05000255/FIN-2015004-012015Q4PalisadesInadequate Dye Penetrant Examination of Pipe Lug WeldsThe inspectors identified a finding of very-low safety significance (Green), and an associated NCV of Title 10, Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion IX, Control of Special Processes, for the licensees failure to perform a dye penetrant (PT) examination of the Safety Injection System (SIS) pipe lug welds in accordance with the American Society of Mechanical Engineers (ASME) Code Section XI requirements. The licensee entered this issue into the Corrective Action Program (CAP) as CR-PLP-2015-04191, repeated the PT examination of the affected SIS lug welds to meet the full extent of coverage required by the ASME Code, repeated examinations of other welds conducted by the PT examiner during the outage, and removed the PT examiner from further weld examination activities. This performance deficiency was determined to be more than minor because, if left uncorrected, the failure to perform a PT examination in accordance with the ASME Code requirements could result in acceptance and return to service of a component with an undetected crack that would increase the possibility of pipe leakage or failure. In addition, the failure to perform a PT examination in accordance with the ASME Code adversely affected the Mitigating System Cornerstone attribute of Equipment Performance, because it could result in failure to detect cracks in pipe welds, which would reduce the availability and reliability of the SIS mitigating system. The inspectors evaluated the finding in accordance with IMC 0609, Appendix A, The SDP for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, and answered yes to screening question number 1. Although this finding adversely affected the design or qualification of the SIS pipe lugs, the finding screened as very-low safety significance (Green), because it did not result in the loss of operability or functionality of the affected SIS pipe segment. This finding had a cross-cutting aspect in the Field Presence component of the Human Performance cross-cutting area. Specifically, licensee leaders were not observed in the work areas of the plant to coach and reinforce standards or expectations for the licensees vendor staff to ensure deviation from standards and expectations were promptly corrected (H.2).
05000255/FIN-2015004-022015Q4PalisadesFailure to Identify Components Required to be Covered by the Quality Assurance ProgramThe inspectors identified a finding of very-low safety significance, and an associated NCV of 10 CFR, Part 50, Appendix B, Criterion II, Quality Assurance Program, for the licensees failure to identify all component cooling water (CCW) structures, systems, and components (SSC), which were required to be covered by the Quality Assurance Program (i.e., be safety-related). As a result, the licensee incorrectly credited nonsafety-related CCW components to remain functional during and following a design basis event (DBE). The licensee entered this finding into their CAP and, after performing operability determinations, concluded the system would still be capable of performing its function. The performance deficiency was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of equipment performance, and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding screened as having very-low safety significance (Green) because, although it was a deficiency affecting the design or qualification of a mitigating SSC, the SSC maintained its operability. The inspectors did not identify a cross-cutting aspect associated with this finding because it was determined not to be representative of current performance.
05000255/FIN-2015004-032015Q4PalisadesFailure to Provide Bases to Determine Changes Did Not Involve Unreviewed Safety QuestionsThe inspectors identified a Severity Level (SL) IV, NCV of 10 CFR, Part 50, Section 59, Changes, Tests, and Experiments, for the licensees failure to maintain records of written safety evaluations, which provide the bases for concluding the nonsafety-related portions of the CCW system inside containment could be credited to perform their function during and following a DBE, and that the change would not result in an unreviewed safety question. The licensee entered this issue into their CAP and, after performing operability determinations, concluded the system would still be capable of performing its function. The violation was determined to be more than minor because the inspectors could not reasonably determine that the changes would not have ultimately required NRC prior approval. The violation was categorized as a SL IV in accordance with Section 6.1.d.2 of the NRC Enforcement Policy because the resulting changes were evaluated by the SDP as having very-low safety significance (i.e., green finding). The resulting changes, the violations underlying technical concerns, impacted the Mitigating Systems cornerstone, and were evaluated separately as the Green finding with the associated 10 CFR, Part 50, Appendix B, Criterion II, NCV discussed above. The inspectors did not identify a cross-cutting aspect because cross-cutting aspects are not assigned to traditional enforcement violations.
05000255/FIN-2015004-042015Q4PalisadesFailure to Perform a Required 50.59 Evaluation for Declassification of the CVCSThe inspectors identified a SL IV, NCV of 10 CFR, Part 50.59, Changes, Tests, and Experiments, and an associated finding of very-low safety significance (Green) for the licensees failure to maintain a record of the declassification of the Chemical Volume and Control System (CVCS) from safety-related to nonsafety-related, which includes a written evaluation that provides the bases for the determination that the change did not require a license amendment. The licensee entered this issue into their CAP, and after a review of the system, determined there was reasonable assurance that it could perform its function. The inspectors determined the underlying technical concern was a performance deficiency associated with the Mitigating Systems cornerstone that was more than minor because, if left uncorrected, would become a more significant safety concern. The underlying technical concern screened as a finding with very-low safety significance (Green) because, although it affected the design or qualification of the CVCS, it did not result in the loss of functionality of the CVCS. The violation was determined to be more than minor because the inspectors could not reasonably determine that the changes would not have ultimately required NRC prior approval. The violation was categorized as a SL IV in accordance with Section 6.1.d.2 of the NRC Enforcement Policy because the changes were evaluated by the SDP, described above, as having very-low safety significance (i.e., Green finding). The inspectors did not identify a cross-cutting aspect associated with the finding because the finding was not representative of current performance.
05000255/FIN-2015004-052015Q4PalisadesLicensee-Identified ViolationTitle 10 CFR 50.65(a)(1), requires, in part, that the holders of an operating license shall monitor the performance or condition of structures, systems, and components (SSCs), against licensee-established goals, in a manner sufficient to provide reasonable assurance that these SSCs, as defined in 10 CFR 50.65(b), are capable of fulfilling their intended functions. Title10 CFR 50.65(a)(2) states that monitoring as specified in 50.65(a)(1) is not required, where it has been demonstrated that the performance or condition of a SSC is being effectively controlled through the performance of appropriate preventive maintenance, such that the SSC remains capable of performing its intended function. Contrary to the above, as identified after the November 14, 2014, TDAFW pump trip, the licensee failed to demonstrate the performance or condition of the safety-related auxiliary feedwater system steam traps had been effectively controlled through the performance of appropriate preventive maintenance. Specifically, some of the safety-related steam traps, one relief valve, and one check valve associated with the steam supply piping of the turbine-driven AFW system were inappropriately classified in the maintenance rule program, resulting in inadequate and/or untimely maintenance being performed on these components, which probably contributed to the overspeed trip event. The licensee found 3 steam traps and one relief valve classified as non-critical components that were reclassified as high critical components and one steam trap and one check valve classified as run-to-failure components that were reclassified as high critical components. Some of these components also had no preventive maintenance (PM) strategies or ones that were not the correct frequency based on the component classification. The licensee identified this issue while conducting the equipment apparent cause evaluation for the overspeed trip event and documented actions to correct the issue in CR-PLP-2014-5477. The licensee performed inspections of all the steam traps required for the TDAFW pump operation and identified some issues with steam cutting, foreign material exclusion in the traps, and incomplete seat contact. These issues were corrected and PM changes have been made for all the system components mentioned above. The inspectors determined that the inconsistent equipment classifications and ineffective preventive maintenance strategy for the safety-related steam traps in the turbine-driven auxiliary feedwater system is considered a performance deficiency. The performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events. Specifically, the licensee identified that the degraded condition of the moisture removal system could have led to excess condensate being present in the steam supply line which had the potential to adversely affect the operation of the turbine for the TDAFW pump, contributing to the overspeed trip event. The inspectors screened the issue using IMC 0609, Appendix A, The SDP for Findings at Power, Exhibit 2, Mitigating Systems Screening Questions, and answered Yes to the question of does this finding represent a loss of system and/or function? This trip of the TDAFW pump on overspeed was evaluated as a failure that impacted the ability of the AFW system to provide the specific function, which could only be accomplished by this train, of decay heat removal via steaming of the A Steam Generator. The turbine-driven AFW pump was also determined to not be in a condition to meet performance requirements defined by the probabilistic risk assessment success criteria, which for AFW is a 24 hour mission time. Therefore, the issue was screened further in a detailed risk evaluation. A Region III Senior Reactor Analyst performed a detailed risk evaluation using the NRCs Standardized Plant Analysis Risk Model for Palisades, Revision 8.20. The SRA assumed the turbine driven AFW pump was unavailable to perform its function for a period of 3 days because the pump was successfully tested and returned to service on November 16, 2014. Given the short exposure period, the calculated delta core delta frequency was less than 1.0E-7/yr. As a result of the low calculated delta core delta frequency, no additional analysis of external event risk contribution or large early release risk contribution was necessary. The dominant core damage sequence was a station blackout followed by the failure of the turbine driven AFW pump and the failure to recover onsite or offsite power. Therefore, the finding screened as very low safety significance (Green).
05000324/FIN-2015007-012015Q2BrunswickFailure to Identify Conditions Adverse to QualityAn NRC-identified Green non-cited violation (NCV) of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action, was identified for licensee failure to identify conditions adverse to quality during the evaluation of an emergency diesel generator (EDG) output breaker failure on March 16, 2015. Specifically, the licensee missed that an internal change made to a relay was a condition adverse to quality. Further, the licensee failed to reclassify a corrective action document to higher significance when information arose indicating that the event in question was a loss of safety function. The licensee documented these issues in their corrective action program, completed the necessary reviews for a condition adverse to quality, and reclassified the original event to Significance Level 1. The inspectors determined that the finding was more than minor in accordance with Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated September 7, 2012, because, if left uncorrected, additional unqualified relays would likely have been installed in the plant. Using Manual Chapter 0609, Appendix A, Exhibit 1, effective July 1, 2012, the finding screened as Green for each unit by answering no to the questions related to an actual loss of function of a system, a single train, non-technical specification equipment designated as high safety-significant in accordance with the licensees maintenance rule program for >24 hrs. The finding had a cross-cutting aspect for Evaluation in the area of Problem Identification & Resolution because the most likely cause of the missed conditions adverse to quality was a lack of thorough investigation during the evaluations (for cause and reportability) of the relay issue.
05000324/FIN-2015007-022015Q2BrunswickInsufficient Material Evaluation of Commercially Dedicated Allen Bradley RelaysAn NRC-identified Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control was identified for the licensees inadequate commercial grade dedication technical evaluation that resulted in non-conforming relays being installed in the control circuits for emergency diesel generator output breakers. This led to specification of a relay that was unsuitable for the application being installed in the control circuit for two emergency diesel generator output breakers and failure of one of those breakers to close. The licensee documented this issue in their corrective action program and performed corrective actions to mitigate the effects of the undetected changes on the relay. The inspectors determined that the finding was more than minor in accordance with Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated September 7, 2012, because, if the process for detecting commercial grade item changes using material evaluations was left uncorrected, additional undetected design or process changes would likely occur. Using Manual Chapter 0609, Appendix A, issued June 19, 2012, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined the finding required a detailed risk evaluation because the effect on two emergency diesel generators was considered a loss of function. For Unit 1, the regional Senior Reactor Analyst used demand data to adjust the probability that an emergency diesel generator would fail to start and ran a condition assessment on SAPHIRE. Because of limited exposure time, the finding was determined to be Green for Unit 1. For Unit 2, the conditions for exposure occurred during an outage with the reactor cavity filled, and both EDGs would be available. The SRA determined the significance to be bounded by the at power risk analysis performed for Unit 1. Because of the low exposure time, and the high likelihood of operators recovering the failure to start of the EDGs, this issue was Green for Unit 2. The inspectors did not identify a crosscutting aspect associated with this finding because the original relay evaluation was done in 1999 and was not indicative of current licensee performance.