RBG-46089, February 2003 Monthly Operating Report for River Bend
| ML030770572 | |
| Person / Time | |
|---|---|
| Site: | River Bend |
| Issue date: | 03/13/2003 |
| From: | King R Entergy Operations |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| RBF1-03-0038, RBG-46089 | |
| Download: ML030770572 (4) | |
Text
Entergy Operations, Inc.
River Bend Station 5485 U S Highway 61 P 0 Box 220 St Francisville, LA 70775 EntergyTel 225 336 6225 Fax 225 635 5068 Rick J. King Director Nuclear Safety Assurance March 13, 2003 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
Subject:
Monthly Operating Report River Bend Station Docket No. 50-458 License No. NPF-47 File No.:
G9.5, G4.25 RBG-46089 RBF1-03-0038 Ladies and Gentlemen:
In accordance with River Bend Station Technical Specification 5.6.4, enclosed is the Monthly Operating Report for February 2003.
er ely, RJK/dhw enclosure 0ýý
Monthly Operating Report March 13, 2003 RBG-46089 RBF1-03-0038 Page 2 of 2 cc:
U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011 NRC Senior Resident Inspector R-SB-14 INPO Records Center 700 Galleria Parkway Atlanta, GA 30339-3064 Mr. Jim Calloway Public Utility Commission of Texas 1701 N. Congress Ave.
Austin, TX 78711-3326 Dottie Sherman American Nuclear Insurers 29 South Main Street West Hartford, CT 06107
DOCKET NO. 501458 RIVER BEND STATION DATE March 13, 2003 COMPLETED BY Danny H. Williamson TITLE Sr. Licensing Specialist TELEPHONE 225-381-4279 PAGE 1
OF 2
OPERATING STATUS
- 1. REPORTING PERIOD:
February 2003
- 2. MAXIMUM DEPENDABLE CAPACITY (MWe-Net):
966
- 3. DESIGN ELECTRICAL RATING (MWe-Net):
966 MONTH YEAR TO CUMULATIVE DATE
- 4. NUMBER OF HOURS REACTOR WAS CRITICAL 643.2 1387.2 121,395.3
- 5. HOURS GENERATOR ON LINE 626.8 1370.8 117,716.2
- 6. UNIT RESERVE SHUTDOWN HOURS 0
0 0
- 7. NET ELECTRICAL ENERGY GENERATED (MWH) 543,862 1,283,383 105,348,759
PAGE 2
OF 2
UNIT SHUTDOWNS SHUTDOWN CAUSE /
NUMBER DATE TYPE DURATION METHOD REASON CORRECTIVE ACTIONS 03-01 030222 F
45 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 2
A A manual reactor scram was initiated due to a fluid leak in the main turbine electro-hydraulic control system. Details will be available in Licensee Event Report 50-458/03-001-00, due for issue by April 23, 2003.
LEGEND:
SHUTDOWN METHOD:
1 - Manual 2 - Manual trip / scram 3 - Automatic trip I scram 4 - Continuation 5 - Other (explain)
REASON:
A - Equipment failure (explain)
B - Maintenance or Test C - Refueling D - Regulatory restriction E - Operator training ! License Exam F - Administrative G - Operational error (explain)
H - Other (explain)
NOTES:
- 1. There were no challenges to the reactor safety relief valves in February.
Danny H. Williamson TYPE:
F - Forced S - Scheduled