Similar Documents at Byron |
---|
Category:NRC Preliminary Notification of Event/Occurrence
MONTHYEARPNO-III-15-004, Byron Unit 1 Automatic Shutdown After Falling Ice Caused Main Power Transformer Short Circuit2015-03-10010 March 2015 PNO-III-15-004 - Byron Unit 1 Automatic Shutdown After Falling Ice Caused Main Power Transformer Short Circuit PNO-III-12-003, Byron Station Unit 1 Unplanned Shutdown for Greater than 72 Hours2012-03-14014 March 2012 PNO-III-12-003 - Byron Station Unit 1 Unplanned Shutdown for Greater than 72 Hours PNO-III-12-002, A, (Update) Byron Unit 1 Loss of Offsite Power and Declaration of a Notice of Unusual Event2012-03-0202 March 2012 PNO-III-12-002A, (Update) Byron Unit 1 Loss of Offsite Power and Declaration of a Notice of Unusual Event ML12060A3862012-02-29029 February 2012 PNO-III-12-002 - Byron Unit 1 Loss of Offsite Power and Declaration of a Notice of Unusual Event PNO-III-12-001, Byron Unit 2 Restarts After a Loss of Offsite Power and Declaring a Notice of Unusual Event2012-02-0707 February 2012 PNO-III-12-001, Byron Unit 2 Restarts After a Loss of Offsite Power and Declaring a Notice of Unusual Event PNO-III-10-015, Byron, Initiation of Reactive Inspection in Response to a Failure of the Mechanism That Cools Water Surrounding a Canister Containing Spent Fuel2010-08-31031 August 2010 PNO-III-10-015: Byron, Initiation of Reactive Inspection in Response to a Failure of the Mechanism That Cools Water Surrounding a Canister Containing Spent Fuel PNO-III-08-002, A - Byron, Unit 2, Update Notice of Unusual Event Due to Loss of Offsite Power to Vital Busses2008-03-28028 March 2008 PNO-III-08-002A - Byron, Unit 2, Update Notice of Unusual Event Due to Loss of Offsite Power to Vital Busses ML0808602592008-03-26026 March 2008 PNO-III-08-002: Byron Unit 2 Notice of Unusual Event Due to Loss of Offsite Power to Vital Busses PNO-III-07-014, Byron Unit 1, Nitrogen Leak During Maintenance2007-11-27027 November 2007 PNO-III-07-014: Byron Unit 1, Nitrogen Leak During Maintenance PNO-III-07-012, A - NRC Inspection Team - Update to Dual Unit Shutdown2007-10-31031 October 2007 PNO-III-07-012A - NRC Inspection Team - Update to Dual Unit Shutdown ML0729601092007-10-23023 October 2007 PNO-III-07-012 - Both Units at Byron Shut Down Due to a Lead in Pipe PNO-III-06-004, B: Byron, Resumption of Effluent Discharges2006-04-20020 April 2006 PNO-III-06-004B: Byron, Resumption of Effluent Discharges ML0609006692006-03-31031 March 2006 PNO-III-06-004A Tritium Leakage (Update) PNO-III-06-006, Byron: Unusual Event Declared Due to a Fire within the Plant Protected Area2006-02-24024 February 2006 PNO-III-06-006, Byron: Unusual Event Declared Due to a Fire within the Plant Protected Area ML0604602112006-02-15015 February 2006 PNO-III-06-004, Tritium Leakage ML0535503512005-12-21021 December 2005 PNO-RIII-05-017- Byron Potential Gunshot Injury to a Site Employee 2015-03-10
[Table view] |
PRELIMINARY NOTIFICATION- REGION III October 31, 2007 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-III-07-012A This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.
Facility Licensee Emergency Classification Byron Station Unit 1 and 2 Notification of Unusual Event Exelon Generation Company, LLC Alert Byron, Illinois Site Area Emergency Docket: 50-454/50-455 General Emergency License: NPF-37/NPF-66 x Not Applicable
SUBJECT:
UPDATE TO DUAL UNIT SHUTDOWN DESCRIPTION:
This preliminary notification supplements information in PNO-III-07-012, which documented the shutdown of the Byron Station Unit 1 and Unit 2 reactors on October 19, 2007, due to a leak in an essential service water pipe.
During the shutdown, the utility investigated the cause of the leak and made necessary repairs in the essential service water system to support start-up. Additional repairs are in progress.
Byron Unit 1 and Unit 2 restarted on October 30, 2007. Full power is expected to be achieved on or about November 2, 2007.
The NRC had dispatched a Special Inspection team to the plant to review the root causes of the problem, extent of condition, and corrective actions. The team continues the review of the issues associated with the essential service water system. Prior to the reactor restart, the team verified the adequacy of the licensees repairs to the essential service water system that had necessitated the shutdown.
This information is current as of 7:30 a.m. on October 31, 2007.
The information in this preliminary notification has been reviewed with licensee management.
Richard Skokowski Bruce Bartlett 630-829-9620 815-234-5451