PLA-2765, Monthly Operating Repts for Nov 1986

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Monthly Operating Repts for Nov 1986
ML20211Q516
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 11/30/1986
From: Keiser H, Sadvary D
PENNSYLVANIA POWER & LIGHT CO.
To: Beebe M
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
PLA-2765, NUDOCS 8703030114
Download: ML20211Q516 (9)


Text

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AVERAGE DAILY UNIT POWER LEVEL D \ }

E U --"" - DOCKET NO.

50-387 La " ;

IT PPal DATE 12/05/86 k I$ COMPLETED BY Duane Sadvary TELEPHONE 717-542-3856 November 1986 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 559 1000-17 2 609 gg 1041 3 615 1044 9

4 852 1043 0

1045 1044 5

949 1045 6 g 7 984 p 1041 g 993 1042 24 9

1036 1044 10 1045 26 1042 II 1046 27 1043 12 1045 1044 28 13 1046 1045 29 906 14 30 15 625 3 16 714 INSTRUCTIONS On this format list the average daily unit power level in MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

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  • 50-388

+ UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. dscs-Unit 2 9 Y, Q UNIT NAME % DATE 12/05/66 8C COh@LETED BY Duane Sadvary REPORT MONTH November 1986 TELEPHONE 717-542-3855 . . "i - Licensee N. Ibte 1 -c > .c -> cc Event ,E ._ c Cause & Corrective Action to $5 5 j i% g Report 2 rN G Prevent Recurrence i 6. 10 861121 S O B 5 N/A SG CO!D Reduced power to approximately 60% 1 to facilitate the repair of condenser tube leaks. Two tubes plugged on I the 'A' low pressure waterbox. 9 861030 F 18.7 B 4 N/A IG 75 On October 30, 1986, Unit Two was manually scrammed to facilitate a containment entry in order to repair the indexing mechanism to the 'E' Traversing Incore Probe Machine. The indexer was repaired and Unit Two was synchronized to the grid on November 1, 1986 at approximately 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br />. t t i I 2 3 4 F: Forced Reason: Method: S- Scheduled Exhibit G - Instructions A-Equiprnent Failure (Explain) I-Manual for Preparatism of Data B-Maintenance of Test 2-Manual Scram. Entry Sheets for tiensee C-Refceling 3-Automatic Scram. Event Report (LER) File (NUREG- , D-Regulatory Restriction 4-Continuation 0161)

E-Operator Training & lxense Examination from p
evious month F-Adtninistrative 5 Goperational Error iEsplain) 5-Reduction Exlaibit I - Same Source 19/77) Ilother (Explam) 9-0ther I

o t UNIT 2 t SUSQUEIIANNA STEAM ELECTRIC STATION Docket Number 50-388 Date 12/05/86 Completed by Duane Sadvary Telephone (717) 542-3856 Challenges to Main Steam Safety Relief Valves None Otanges to the Offsite Dose Calculation Manual None Major Changes to Radioactive Waste Treatment Systems None b. @ Pennsylvania Power & Light Company Two North Ninth Street

  • Allentown, PA 18101
  • 215 I 770 5151 Harold W. Kelser Vice President-Nuclear Operations 215/770-7502 DEC ' 51986 Director. Data Automation &

Management Information Division Attention: Mr. M. R. Beebe Management Information Branch Office of Resource Management U.S. Nuclear Regulatory Commission Washington, D.C. 20555 SUSQUEHANNA STEAM ELECTRIC STATION MONTilLY OPERATING REPORTS Docket Nos. 50-387/NPF-14 , PLA-2765 FILE R41-2A 50-388/NPF-22 Dear Mr. Beebe The November 1986 monthly operating reports for Susquehanna SES Units 1 and 2 are attached. Very truly yours. / LLom II. W. Keiser Vice President-Nuclear Operations Attachment cc Dr. Thomas E. Murley Regionni Administrator-Region i U.S. Nuclear Regulatory Commission 631 Park Avenue King of Prursia. PA 19406 Director Office of Inrpection and Enforcement U.S. Nucicar Regulatory Commission Washington. D.C. 20555 Attn Document Control Desk (12 copien) Mr. !.. R. Plinco - NRC Mr. M. C. Thadant - NRC l< t