NRC-05-0019, February 2005 Monthly Operating Report for Fermi 2

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February 2005 Monthly Operating Report for Fermi 2
ML050770414
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 03/08/2005
From: Peterson N
Detroit Edison
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
GL-97-002, NRC-05-0019
Download: ML050770414 (3)


Text

Fermi 2 6400 North Dixie Hwy., Newport, MI 48166 Detroit Edison

<4OF9 Generic Letter 97-02 March 8, 2005 NRC-05-0019 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington D C 20555

Reference:

Fermi 2 NRC Docket No. 50-341 NRC Operating License No. NPF-43

Subject:

Monthly Operating Status Report for February 2005 Enclosed for your information and use is the Fermi 2 Monthly Operating Status Report for February 2005. This report includes the Operating Data Report and Summary of Unit Shutdowns identified in NRC Generic Letter 97-02 and Fermi 2 Technical Specification 5.6.4.

Should you have any questions or require additional information, please contact me at (734) 586-4258.

Sincerely, Nrma Peterson Manager - Nuclear Licensing Enclosure cc: R. J. Aben, Jr.

E. R. Duncan , I- tl'- 0 N. K. Ray M. V. Yudasz, Jr.

NRC Resident Office Regional Administrator, Region m A DTE Energy Company

OPERATING DATA REPORT DOCKET NO. 50-341 UNIT NAME Fermi 2 DATE March 8.-2005 COMPLETED BY Kevin Burke-TELEPHONE (734) 586-5148 REPORTING PERIOD: February 2005

1. Design Electrical Rating (MWe-Net) 1.150.00
2. Maximum Dependable Capacity (MWe-Net) 1,089.00 This Month Year-to-Date Cumulative
3. Number of Hours the Reactor Was Critical 571.97 1,140 116.941
4. Number of Hours Generator On-line 532.62 1.101 112.875
5. Reserve Shutdown Hours 0.00 0.00 0.00
6. Net Electrical Energy Generated (MWH) 582,965 1,221.768 114.298.446 UNIT SHUTDOWNS No. Date Type Duration Reason Method of Cause and Corrective Action F: Forced (Hours) (1) Shutting Comments S: Scheduled Down (2) 05-01 02/01/05 F 139.4 A 4 Plant shutdown caused by unidentified drywell leakage above Technical Specification limit. Inspection identified Drywell Cooler unit Number 4 failed end-bell gasket as the source of the leak.

SUMMARY

Following plant shutdown on January 24, 2005 due to a failed end-bell gasket on the Number 4 Drywell Cooler, plant startup commenced on February 2, 2005 after repairs were completed. During power ascension, a steam leak was identified from the Reactor Recirculation Pump "A" Discharge Valve packing and the plant was shutdown for repairs. On February 5, 2005 repairs to the Reactor Recirculation Pump "A" Discharge Valve packing was completed and plant was restarted. On February 6, 2005 the Main Turbine Generator was synchronized and the plant achieved full power on February 7, 2005. On February 12, 2005 at 0428 hours0.00495 days <br />0.119 hours <br />7.07672e-4 weeks <br />1.62854e-4 months <br />, power was reduced from 100 percent to 90 percent for a Control Rod Pattern Adjustment and the plant was returned to full power at 0512 hours0.00593 days <br />0.142 hours <br />8.465608e-4 weeks <br />1.94816e-4 months <br />. The plant operated at full power (excluding small power reductions for required surveillance testing) for the remainder of the month.

(1) Reason: (2) Method:

A Equipment Failure (Explain) I Manual

  • B Maintenance or Test 2 Manual Trip/Scram C Refueling 3 Automatic Trip/Scram D Regulatory Restriction 4 Continuation E Operator Training and License Examination 5 Other (Explain)

F Administration G Operational Error (Explain)

H Other (Explain)

Text

Fermi 2 6400 North Dixie Hwy., Newport, MI 48166 Detroit Edison

<4OF9 Generic Letter 97-02 March 8, 2005 NRC-05-0019 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington D C 20555

Reference:

Fermi 2 NRC Docket No. 50-341 NRC Operating License No. NPF-43

Subject:

Monthly Operating Status Report for February 2005 Enclosed for your information and use is the Fermi 2 Monthly Operating Status Report for February 2005. This report includes the Operating Data Report and Summary of Unit Shutdowns identified in NRC Generic Letter 97-02 and Fermi 2 Technical Specification 5.6.4.

Should you have any questions or require additional information, please contact me at (734) 586-4258.

Sincerely, Nrma Peterson Manager - Nuclear Licensing Enclosure cc: R. J. Aben, Jr.

E. R. Duncan , I- tl'- 0 N. K. Ray M. V. Yudasz, Jr.

NRC Resident Office Regional Administrator, Region m A DTE Energy Company

OPERATING DATA REPORT DOCKET NO. 50-341 UNIT NAME Fermi 2 DATE March 8.-2005 COMPLETED BY Kevin Burke-TELEPHONE (734) 586-5148 REPORTING PERIOD: February 2005

1. Design Electrical Rating (MWe-Net) 1.150.00
2. Maximum Dependable Capacity (MWe-Net) 1,089.00 This Month Year-to-Date Cumulative
3. Number of Hours the Reactor Was Critical 571.97 1,140 116.941
4. Number of Hours Generator On-line 532.62 1.101 112.875
5. Reserve Shutdown Hours 0.00 0.00 0.00
6. Net Electrical Energy Generated (MWH) 582,965 1,221.768 114.298.446 UNIT SHUTDOWNS No. Date Type Duration Reason Method of Cause and Corrective Action F: Forced (Hours) (1) Shutting Comments S: Scheduled Down (2) 05-01 02/01/05 F 139.4 A 4 Plant shutdown caused by unidentified drywell leakage above Technical Specification limit. Inspection identified Drywell Cooler unit Number 4 failed end-bell gasket as the source of the leak.

SUMMARY

Following plant shutdown on January 24, 2005 due to a failed end-bell gasket on the Number 4 Drywell Cooler, plant startup commenced on February 2, 2005 after repairs were completed. During power ascension, a steam leak was identified from the Reactor Recirculation Pump "A" Discharge Valve packing and the plant was shutdown for repairs. On February 5, 2005 repairs to the Reactor Recirculation Pump "A" Discharge Valve packing was completed and plant was restarted. On February 6, 2005 the Main Turbine Generator was synchronized and the plant achieved full power on February 7, 2005. On February 12, 2005 at 0428 hours0.00495 days <br />0.119 hours <br />7.07672e-4 weeks <br />1.62854e-4 months <br />, power was reduced from 100 percent to 90 percent for a Control Rod Pattern Adjustment and the plant was returned to full power at 0512 hours0.00593 days <br />0.142 hours <br />8.465608e-4 weeks <br />1.94816e-4 months <br />. The plant operated at full power (excluding small power reductions for required surveillance testing) for the remainder of the month.

(1) Reason: (2) Method:

A Equipment Failure (Explain) I Manual

  • B Maintenance or Test 2 Manual Trip/Scram C Refueling 3 Automatic Trip/Scram D Regulatory Restriction 4 Continuation E Operator Training and License Examination 5 Other (Explain)

F Administration G Operational Error (Explain)

H Other (Explain)