NL-04-1766, August 2004 Monthly Operating Reports for Hatch Nuclear Plant

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August 2004 Monthly Operating Reports for Hatch Nuclear Plant
ML042590233
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 09/13/2004
From: Sumner H
Southern Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NL-04-1766
Download: ML042590233 (7)


Text

H. L Sumner, Jr.

Vice President Hatch Project Southern Nuclear Operating Company, Inc.

Post Office Box 1295 Birmingham, Alabama 35201 Tel 205.992.7279 September 13, 2004 SOUTHERNEWa COMPANY Energy to Serve Your World' NL-04-1766 Docket Nos.:

50-321 50-366 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555-0001 Hatch Nuclear Plant Monthly Operating Reports Ladies and Gentlemen:

Enclosed are the August 2004 Monthly Operating Reports as required by section 5.6.4 of the Technical Specifications.

This letter contains no NRC commitments. If you have any questions, please advise.

Sincerely, H. L. Sumner, Jr.

HLS/il/daj

Enclosures:

El - HNP Unit 1 Monthly Operating Report E2 - HNP Unit 2 Monthly Operating Report cc:

Southern Nuclear Operating Company Mr. J. T. Gasser, Executive Vice President Mr. G. R. Frederick, General Manager - Plant Hatch RTYPE: CHAO2.004 U. S. Nuclear Regulatory Commission Dr. W. D. Travers, Regional Administrator Mr. C. Gratton, NRR Project Manager - Hatch Mr. D. S. Simpkins, Senior Resident Inspector - Hatch J-,- '

Enclosure I Plant Hatch Unit I Monthly Operating Report August 2004

OPERATING DATA REPORT DOCKET NO.

50-321 UNIT NAME Hatch I DATE September 10, 2004 COMPLETED BY R. M. Beard TELEPHONE (912) 366-2000 x5925 REPORTING PERIOD:

August 2004

1.

Design Electrical Rating 885.00

2.

Maximum Dependable Capacity (MWe-Net) 869.00 This Month Yr-to-Date Cumulative

3. Number of Hours the Reactor was Critical 744.00 5,190.13 204,062.94
4.

Number of Hours Generator On-line 744.00 5,117.43 198,028.15

5.

Reserve Shutdown Hours 0.00 0.00 0.00

6. Net Electrical Energy Generated (MWHrs) 645,145.00 4,294,596.00 145,972,765.0 UNIT SHUTDOWNS Type Method of F: Forced Duration Reason Shutting Cause & Corrective Action No.

Date S: Scheduled (Hours)

Down 2 Comments

SUMMARY

Unit 1 began the month operating at -94% of rated thermal power while performing CRD Exercises. The unit was returned to rated thermal power at 0415 on 8/1/04 following a preconditioning ramp. Shift reduced power to

<2777 CMWth at 1129 on 8/5/04 when it was determined that the feedwater flow correction factor from the ultrasonic flow meter, CROSSFLOW, was not being utilized by the process computer due to an operator failing to initiate the input to the heat balance following the Recirculation System runback on 7/7/04. The CROSSFLOW input to the process computer was re-initiated at 1549 on 8/5/04 and the unit returned to rated thermal power at 1730 on 815104.

Shift reduced power to <2777 CMWth (-99% of rated) at 0824 on 8/7/04 and removed the CROSSFLOW input from the heat balance due to an increasing number of nuisance alarms. Shift reduced load to -865 GMWe (-2625 CMWth) at 2300 on 8/7/04 to perform CRD Exercises. The unit was returned to 99% of rated thermal power, due to the CROSSFLOW input to the heat balance not being utilized, at 0315 on 818/04. Shift reduced load to -900 GMWe

(<2750 CMWth) at 1718 on 8/14/04 due to the Core Thermal Power (CTP) program on the process computer not updating. CTP was restored to service and the unit returned to -99% of rated thermal power at 1932 on 8114/04.

Shift reduced load to -860 GMWe (-2625 CMWth) at 2300 on 8/14/04 to perform CRD Exercises, a Rod Pattern Adjustment and Turbine Stop Valve Testing. The unit was returned to -99% of rated thermal power at 0400 on 8/15/04 following a preconditioning ramp. The CROSSFLOW input to the heat balance was re-initiated and the unit returned to rated thermal power at 1305 on 8/17/04. Shift began reducing load to -500 GMWe (-1600 CMWth) at 0800 on 8/21/04 to perform a Rod Sequence Exchange, CRD Scram Time Testing, Turbine Control Valve Testing, and CRD Exercises. Shift stopped reducing load when a discrepancy was discovered with the Control Rod Movement Sheet and the Rod Worth Minimizer. The unit was at -710 GMWe (-2175 CMWth). Shift resumed the load reduction at 1520 after the discrepancy was resolved. The unit was returned to 99% of rated thermal power at 2020 on 8/22/04 following a preconditioning ramp while awaiting a setpoint change to be implemented on CROSSFLOW before initiating the Input to the heat balance. Unit power level began decreasing at 0525 on 8123/04 due to a limiting rod pattern following the sequence exchange. Shift reduced load for a rod pattern adjustment at 2023 on 8/23/04 and returned the unit to rated thermal power at 2356 on 8/23/04 following a preconditioning ramp. Shift reduced load to

-860 GMWe (-2625 CMWth) for CRD Exercises at 2300 on 8128/04. The unit was returned to rated thermal power at 0402 on 8129/04. Unit I completed the month of August maintaining rated thermal power. There were no challenges to the safety relief valves.

Page 1 of 2

1 2

Reason:

A Equipment Failure (Explain)

B Maintenance or Test C

Refueling D

Regulatory Restriction E

Operator Training & License Examination F

Administration G

Operational Error (Explain)

H Other (Explain)

Method:

I Manual 2

Manual Trip/Scram 3

Automatic TriplScram 4

Continuation 5

Other (Explain)

Page 2 of 2 Plant Hatch Unit 2 Monthly Operating Report August 2004

OPERATING DATA REPORT DOCKET NO.

50-366 UNIT NAME Hatch 2 DATE September 10, 2004 COMPLETED BY R. M. Beard TELEPHONE (912) 366-2000 x5925 REPORTING PERIOD:

August 2004

1.

Design Electrical Rating 908.00

2.

Maximum Dependable Capacity (MWe-Net) 883.00 This Month Yr-to-Date Cumulative

3.

Number of Hours the Reactor was Critical 744.00 5,855.00 180,615.90

4.

Number of Hours Generator On-line 744.00 5,855.00 176 227.47

5.

Reserve Shutdown Hours 0.00 0.00 0.00

6.

Net Electrical Energy Generated (MWHrs) 647,848.00 5,144,651.00 132,725,063.0 UNIT SHUTDOWNS Type Method of F: Forced Duration Reasoni Shutting Cause & Corrective Action No.

Date S: Scheduled (Hours)

Down 2 Comments

SUMMARY

Unit 2 began the month maintaining maximum operating power (MOP) of -2765 CMWth. Unit 2 is limited to a maximum control voltage (EsubL) of 4.82 to the #4 Turbine Control Valve. Shift reduced load to -720 GMWe (-2230 CMWth) at 1300 on 811/04 to perform a Rod Pattern Adjustment and CRD Exercises. The unit was returned to MOP at 0450 on 8/2104 following a preconditioning ramp. Shift reduced load to -720 GMWe (-2220 CMWth) at 1659 on 818/04 to perform a Rod Pattem Adjustment and CRD Exercises. The unit was returned to MOP at 0450 on 8/9/04 following a preconditioning ramp. Shift reduced load to -910 GMWe (-2763 CMWth) at 0844 on 8/14/04 to support removing the security power inverter from service. The security power inverter impacts the power supply to the process computer. Shift further reduced load to -900 GMWe (<2773 CMWth) when power was restored and the process computer activated but the CROSSFLOW derate clock active. Shift did not initiate the CROSSFLOW input to the heat balance while the derate clock was active, The unit was returned to MOP at 2036 on 8/14/04 following a preconditioning ramp after the CROSSFLOW derate clock cleared and the input to the process computer heat balance was restored. Shift reduced load to -860 GMWe at 2258 on 8/15/04 to perfrom CRD Exercises, a Rod Pattern Adjustment and Turbine Stop Valve Testing. The unit was returned to MOP at 0502 on 8/16/04 following a preconditioning ramp. Shift reduced load to -830 GMWe (-2525 CMWth) at 2301 on 8/22/04 to perfrom a Rod Pattern Adjustment and CRD Exercise. The unit was returned to MOP at 0802 on 8/23/04 following a preconditioning ramp. Shift increased power to -2790 CMWth at 0914 on 8/25/04 after increasing vessel pressure by 10 Ibs, from 1035 PSIG to 1045 PSIG to reduce the value of the control signal to the #4 Turbine Control Valve and begin testing for the Appendix K Power Uprate. Shift decreased power back to MOP at 1657 on 8/25/04 after experiencing delays in the recirculation system response to minor speed adjustments. Shift reduced vessel pressure to 1035 PSIG at 1936 on 8/25/04 per management direction. Shift reduced load to -860 GMWe (-2625 CMWth) at 2300 on 8/29/04 to perform CRD Exercises and a Rod Pattern Adjustment. The unit was returned to MOP at 0538 on 8/30/04 following a preconditioning ramp. Unit 2 completed the month of August maintaining MOP. There were no challenges to the safety relief valves.

Page 1 of 2

I 2

Reason:

A Equipment Failure (Explain)

B Maintenance or Test C

Refueling D

Regulatory Restriction E

Operator Training & License Examination F

Administration G

Operational Error (Explain)

H Other (Explain)

Method:

I Manual 2

Manual Trip/Scram 3

Automatic Trip/Scram 4

Continuation 5

Other (Explain)

Page 2 of 2