ML25196A293

From kanterella
Jump to navigation Jump to search
12-13-77 Report on Donald C. Cook Nuclear Plant Unit No. 2
ML25196A293
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/13/1977
From: Bender M
Advisory Committee on Reactor Safeguards
To: Hendrie J
NRC/Chairman
References
Download: ML25196A293 (1)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ADVISORY COMMITTEE ON REACTOR SAFEGUARDS WASHINGTON, D. C. 20555 Honorable Joseph M. Hendrie Chairman December 13, 1977

u. s. Nuclear Regulatory Corrmission Washington, DC 20555 SUBJEcr:

REPORI' ON DONALD C. CXX)K NUCLEAR PLANT UNIT NO. 2

Dear Dr. Hendrie:

During its 212th meeting, December 8-10, 1977, the Advisory Conmittee on Reactor Safeguards completed its review of the application of the Indiana and Michigan Electric Company and the Indiana and Michigan Power Conpany (the Applicants) for a permit to operate the Donald C. Cook Nuclear Plant Unit No. 2. The application was reviewed at a Subcomnittee meeting in St. Joseph, Michigan on December 3, 1977, and a tour of the facility was made by Subcomnittee members on December 2, 1977. During its review, the Committee had the benefit of discussions with representatives and con-sultants of the Nuclear Regulatory Conmission (NRC) Staff, Westinghouse Electric Corporation, American Electric Power Service Corporation, and the Applicants. The Comnittee also had the benefit of the doctnnents listed.

The Donald C. Cook Nuclear Plant is a two-unit station located on the eastern shore of Lake Michigan about 11 miles south-southwest of Benton Harbor, Michigan. The two units are virtually identical except that D. C. Cook Unit 1 utilizes 15 x 15 fuel assemblies and is licensed to operate at 3250 MWt while it is proposed that D. C. Cook Unit 2 will utilize 17 x 17 fuel assemblies and operate at 3391 MWt.

Each unit includes a Westinghouse Electric Corporation pressurized water reactor and ice condenser containment structure. The Comnittee reported on the application for an operating license on D. C. Cook Unit 1 in its letters of October 17, 1973, March 11, 1976, and January 14, 1977 and for a con-struction permit on both units in its letter of December 13, 1968.

A surveillance program has been developed by the NRC Staff to follow the behavior of the 17 x 17 fuel assemblies and data are being obtained from several plants now in operation using 17 x 17 fuel assemblies.

Experience to date has been good. The Comnittee was informed that the first full core inspection of the 17 x 17 fuel assemblies is scheduled for mid-1978 for the Trojan Nuclear Power Plant. The Comnittee wishes to be kept informed of the results of the various 17 x 17 fuel assembly inspections and test programs planned for the future.

302

Honorable Joseph December 13, 1977 The Applicants have requested two significant changes in the reactor core thermal hydraulic performance analysis for o. c. Cook Unit 2 which have not been requested for previously reviewed plants. These changes include the WRB-1 critical heat flux correlation and the Westinghouse Electric Corporation improved thermal design procedures. The NRC Staff has not yet conpleted its review. The Conmittee wishes to be kept in-formed and suggests that it should review these matters on a generic basis prior to any use of the new procedures.

The NRC Staff has identified a number of safety items which will require resolution before full power operation of o. c. Cook Unit 2. These mat-ters should be resolved in a manner satisfactory to the NRC Staff.

The Applicants have made a number of design changes too. C. Cook Unit 2 as a result of operating experience gained in o. C. Cook Unit 1. This experience, especially operation of the o. C. Cook Unit 1 ice condenser containment system over the last three-year period, has been helpful in the ice inventory maintenance of the D. C. Cook Unit 2 ice condenser.

The Applicants and the NRC Staff should continue to monitor the ice con-denser containments in both units to further enhance the safe operation of plants using this new concept.

The ACRS recomnends that a report be made to the-Comnittee after one year of operation at power which treats the following subjects:

a)

A substantial data base obtained with D. C. Cook Unit 2 to verify the validity of out-of-core and incore measure-ments with the axial power distribution monitoring system (APDMS).

b)

An evaluation of the emergency core cooling systems and shutdown heat removal systems to determine the possibility of improvements in reliability for o. C. Cook Unit 2.

With regard to the generic problems listed in the COI11nittee's report, "Status of Generic Items Relating to Light-Water Reactors - Report No. 6, 0 dated November 15, 1977, items considered relevant to Donald c.-Cook Nuclear Plant are: II-2, 3, 4, SB, 6, 7, 107 IIA-1, 2, 3, 47 IIB-27 IIC-1, 3A, 3B, 4, 5, 67 IID-2. These problems should be dealt with by the NRC Staff and Applicants as solutions are found.

303

Honorable Joseph December 13, 1977 The Advisory Comnittee on Reactor Safeguards believes that, if due con-sideration is given to the items mentioned above, and subject to satis-factory conpletion of construction and preoperational testing, there is reasonable assurance that the Donald C~ Cook Nuclear Plant Unit No. 2 can be operated at power levels up to 3391 MWt without undue risk to the health and safety of the public.

Sincerely yours, 11!.Jl~

Chairman

References:

1. u. s. Nuclear Regulatory Conmission:

nReport to the Advisory Ccmnittee on Reactor Safeguards,n in the matter of Indiana and Michigan Electric Company and Indiana and Michigan Power Conpany (I&MP Co.) application for an operating license for the Donald c. Cook Nuclear Plant Unit No. 2, Docket No. 50-316, dated November, 1977.

2. Indiana and Michigan Power Company:

noonald C. Cook Nuclear Plant Final Safety Analysis Report" with Amendments 1-79.

3. Letters from M. H. Judkis, Manager of American Electric Power Project for Westinghouse Electric Corporation, to Edson Case, Acting Director of the Office of Nuclear Reactor Regulation {c:mm.), concerning reso-lution of outstanding issues, dated November 21, 1977 and November 18, 1977.
4. Letters from J. Tillinghast, Vice President of Indiana and Michigan Power Conpany (V.P. of I&MP Co.), to Edson Case, Acting Director, ONRR, concerning the OVerpressurization Mitigating System, dated November 18, 1977 and August 4, 1977.
5. Letter from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning qualification of containment electrical penetrations for accident environments, dated November 17, 1977.
6. Letter from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning qualification tests of ice condenser corrponents, dated October 27, 1977.
7. Letters from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning an analysis of a fuel handling accident inside containment, dated September 30, 1977 and June 17, 1977.
8. Letters from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning proposed technical specifications, dated September 22, 1977 and June 17, 1977.

304

Honorable Joseph December 13, 1977

9. Letter from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning the Quality Assurance Program for Operations, dated September 9, 1977.
10. Letter from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning design of the emergency power systems, dated July 22, 1977.
11. Letter from J. Tillinghast, V.P. of I&MP Co., to Edson Case, Acting Director, ONRR, concerning the design and procedures for operation of the local shutdown panels, dated June 1, 1977.
12. Letter from G. P. Malone, V.P. of I&MP Co., to B. Rusche, Director, ONRR, concerning fire hazards analysis, dated March 31, 1977.

305