ML22118B146
| ML22118B146 | |
| Person / Time | |
|---|---|
| Site: | Vallecitos Nuclear Center |
| Issue date: | 04/28/2022 |
| From: | Martinez C GE Hitachi Nuclear Energy |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| M220070 | |
| Download: ML22118B146 (10) | |
Text
M220070 April 28, 2022 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555-001
Subject:
GEH Annual Nuclear Test Reactor (NTR) Operating Report for the Year 2021 (Rev 1)
Reference:
NRC License R-33, Docket 50-73 (NTR)
Enclosed is Rev 1 of the Annual Operating Report No. 62 for the GE Hitachi Nuclear Test Reactor (NTR) located at the Vallecitos Nuclear Center in Sunol, California. This revision corrects a typographical error in the time and date for Scram Report 21-02.
If there are any questions regarding this report or additional information required, please contact me at the number above.
Sincerely, Carlos Martinez Site Manager Vallecitos Nuclear Center
Enclosure:
- 1) NTR Annual Operating Report Number 62 (Rev 1) for the year 2021 cc: D. Hardesty, NRC NRR CM 22-002 GEHitachiNuclearEnergy
CarlosMartinez
SiteManager,VallecitosNuclearCenter
6705VallecitosRoad
Sunol,CA94586
USA
T9254959173
Carlos1.Martinez@ge.com
Digitally signed by Carlos Martinez Reason: Approved Date: 2022-04-28 14:31-07:00
GEHitachi
NuclearEnergy
VallecitosNuclearCenter
6705VallecitosRd
Sunol,CA94586
USA
NUCLEARTESTREACTOR
ANNUALREPORTNO.62Rev.1
FORTHEYEAR2021
LICENSER33
DOCKET5073
APRIL28,2022
Page 1 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
GEHitachiNuclearTestReactor
AnnualReportNo.62Rev.1
Thisreportsummarizestheoperations,changes,tests,experiments,andmajormaintenanceat
theGEHitachi(GEH)NuclearTestReactor(NTR),whichwereauthorizedpursuanttoLicenseR 33,Docket5073,and10CFR50,Section50.59,fortheperiodofJanuary1,2021through
December31,2021.
I.General
SpecificinformationabouttheoperationoftheNTRduringthereportingperiodispresentedas
follows:
- 1. In2021therewere201reactorstartupswiththereactoroperatingatorabovecritical
for618.62hours.Totalpowergenerationequaled603.85EFPH;equivalentto2.516
MWdays.Themajorityofthistimewasspentintheperformanceofapproved
experiments,eitherneutronradiographyorsmallsampleirradiations.
- 2. ThehighestradiationexposuretoanyworkeratNTRwas0.718Rem.
- 3. Therewerefiveunscheduledshutdownsofthereactorin2021andfiveunscheduled
shutdownspriortocriticality.SeesectionVfordetails.
- 4. One2020technicalspecificationviolationwascitedinNRCInspectionReport2021201
whentheoperatorrequalificationprogramactivitieswerenotcompletedbythe
requiredduedate.SeesectionVfordetails
II.Organization
Thedetailsofchangesinthestatusofpersonnelandoperatorlicenses,whichoccurredduring
thereportingperiod,aredescribedasfollows:
Page 2 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
A.
Personnel
TheLevel1&2,Level3,andVNCsiteRegulatoryCompliancemanagerswere
unchangedin2021.
B.
OperatorLicenses
TherewerenochangestothestatusofoperatorlicensesundertheVallecitosNuclear
TestReactor,FacilityLicenseNo.R33in2021.
III.FacilityChanges,Tests,Experiments,andProcedureChangesApprovedbytheFacility
Manager
Inaccordancewithwrittenprocedures,facilitymanagerapprovalisrequiredforchangestothe
facility,procedures,tests,andexperiments.Specificinformationaboutthereportingperiodis
presentedasfollows:
A.
FacilityChanges
Thereweretwofacilitychangesimplementedin2021requiringFacilityManagerand
RegulatoryComplianceapproval.
- 1. Primarycoolantsystemconductivityprobeandreadoutwerereplacedasdescribedin
ChangeAuthorization(CA)317.Theoriginalprobecouldnotsafelyberemovedfrom
thesystemforcalibrationagainstaknownstandardasdocumentedinConditionReport
(CR)37268.Thenewsystemallowseasyremovalandplannedmaintenanceprocedure
StandardOperatingProcedure(SOP)12.46describesthecalibrationprocess.
- 2. PrimarycoolantpumpfailedandwasreplacedunderEngineeringRelease(ER)2119.
Thepumpinletvalve(TV103),samplesinkreturnvalve(V121),andthesectionof
aluminumpipebetweenthepumpandTV103werealsoreplaced.NTRCA322
documentsthisvalveandpipingchangeandtheassociated50.59evaluation.
B.
Tests
Pursuantto10CFR50.59(a),nospecialtestswereperformedduring2021.
C.
Experiments
Pursuantto10CFR50.59(a),twopreviouslyapprovedexperimenttypeswereperformedin
2021.
Page 3 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
- 1. Experimenttypesdescribedasneutronradiographyandslidesampleirradiations,were
properlyauthorizedutilizingexperimentauthorizationformsthroughout2021.
D.
ProcedureChanges
Pursuantto10CFR50.59,theadministrativerevisionofallNTRStandardOperatingProcedures
thatwasbegunin2020anddocumentedinNTRCA318,wascompletedin2021.Additionally,
elevenproceduralchangeswereinitiatedduring2021toincorporateeditorialortypographical
corrections,technicaldata,andchangestorequirements,ortoprovidefortheadditionor
clarificationofinformationandreliabilityofperformance.ChangesweremadewithFacility
ManagerandRegulatoryCompliancereviewwhenrequired.Asummaryofthechangesis
presentedinthetablebelow.
Revision
Procedure
SummaryofChanges
1 SOP 2.7, Process Instrumentation Added description of recently installed conductivity probe and meter.
1 SOP 4.2, Safety Rod Repairs Added new section on adjusting the flexible coupling.
2 SOP 6.4, Daily Surveillance Check Sheet Added a check that the On-Duty Emergency Director is on site prior to operating NTR.
1 SOP 6.5, Monthly Surveillance Check Sheet Changes reflect simplified conductivity meter checks.
1 SOP 8.2, Non-Reactor Emergencies Updated references to SEP site emergency procedures to recently approved SEC procedures.
1 SOP 8.4, Off-Normal Alarm Response Rewritten to clarify the definition of a seismic occurrence, reference the VNC earthquake procedure, and simplify emergency response for different modes of reactor operation.
1 SOP 8.5, Seismic Activity Clarification of 1) actions to seismic events when the reactor is operating, and 2) definition of Modified Mercalli IV. Intent of procedure is not affected by this change.
1 SOP 9.14, Reactor Operator Requalification Program Added clarifications on 1) time interval between annual operating tests, 2) preserving exam integrity when multiple operators are taking the same test, and
- 3) using a calendar-based reminder system to track annual requalification requirements.
Page 4 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
1 SOP 10.6, Cable-Held Retractable Irradiation System Authorized SROs to sign the VNC 706 form when transferring irradiated samples on-site.
1 SOP 12.3, Safety Rod Drives Added annual visual checks of the anvil roll pin and flexible coupling.
1 SOP 12.31, Stack Gas Monitor Changed the stack gaseous activity alarm point to match the values in SOP 5.2 and SOP 8.4 Alarm #22.
IV.MajorPreventativeorCorrectiveMaintenance
Duringthisreportingperiod,allroutinepreventivemaintenanceandsurveillancecheckswere
completedasscheduledwiththeexceptionofthethirdquarter,semiannual,EmergencyDiesel
GeneratorLoadTest,PM00301SBN.Thesitegeneratorisbeingrepairedandarentalunithas
beenacquiredtofulfillthisemergencyfunction.
Thefollowingliststhenoteworthycorrectivemaintenanceactivitiesperformedin2021.
- 1. 1/8/21Replacedthestartupsourcedrivebelt
Duringmaintenance,thestartupsourcecouldnotbewithdrawnfromthereactorwithinthe
requiredtimeframe.ThedrivebeltwasreplacedandallretestsperSOP12.4completed
satisfactorily.
- 2. 2/8/21ReplacedSR#4magnetS3withmagnetS13
AbrokenleadwirewasdiscoveredonmagnetS3duringtheinvestigationintoScram2102.
Themagnetwasreplaced.SeesectionVItemA.2belowfordetails.
- 3. 3/2/21Regluedstop(rubber)ontotheanvilofSafetyRod(SR)#4
Duringmaintenance,SR#4failedtomeettherequiredinflightscramtime.Thestop
(rubber)ontheanvilwasfoundtobedetached.ThepartwasreattachedperER2110and
retestedsatisfactorily.
- 4. 4/27/21thru6/15/21Onmultipleoccasions,SR#4exhibitedanabnormallyhigh
resistancetooutwardmovement
Adeliberateandcontrolledapproachwasusedtoaddressthisrecurringbutnonrepeatable
issueresultinginthefollowingactions:1)replacedtheanvilrollpinandoring,2)replaced
thedashpotbearing,3)replacedinnerbearingsurface(bushing),and4)disassembledand
Page 5 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
cleanedtheentiresafetyrodassembly.IssuedocumentedandaddressedbyCR36854and
ERs2113,2115,and2117.
- 5. Spurioushighstackparticulatealarms1/11/21thruearlyJune2021
Receivedfrequenthighstackparticulateactivityalarmsthatweredeterminedtobe
spuriousbetweenJanuaryandJune2021.EffortsdocumentedinCR36408totroubleshoot
andcorrectthiscondition.
V.UnscheduledShutdowns
Duringthereportingperiod,therewerefiveunscheduledreactorshutdownsafterreaching
criticalityandfiveunscheduledshutdownspriortoreachingcriticality.
A. UnscheduledShutdowns
- 1. ScramReport2101
Anunscheduledshutdownoccurredat11:45AMon2/3/2021withthereactoroperatingat
100%power.AReactorSafetySystemscramwasautomaticallyinserted.Therewereno
indicationsofthecauseofthescram.Avisualinspectionandoperationaltestsofallfour
safetyrodswerecompletedwithnoabnormalitiesobserved.ActionsdocumentedunderCR
36141.
- 2. ScramReport2102
Anunscheduledshutdownoccurredat11:08AMon2/5/2021withthereactoroperatingat
100%power.AReactorSafetySystemscramwasautomaticallyinsertedandtherewereno
indicationsofthecauseofthescram.ER2106wasgeneratedtoguidetroubleshootingon
all4safetyrods.Subsequently,issuesfoundandcorrectedincluded1)abareleadwireon
SR#2magnet,2)abrokenleadwireuponinspectingSR#4magnetrequiringreplacement,
and3)matingsurfacesbetweenthemagnetsandanvilsforsafetyrods2,3and4were
adjustedforamoreoptimalalignment.ThescramreportandCR36196documented
correctiveactions.
- 3. ScramReport2103
Anunscheduledshutdownoccurredat10:24AMon5/21/2021duringareactorstartup.A
ReactorSafetySystemscramwasautomaticallyinsertedastheoperatorstartedtomove
controlrodsoutwardafterestablishingcriticalrodheightwhilein1outof2safetysystem
coincidencelogic.Whileswitchingrangesononeofthetwoonlinepowerpicoammeter
Page 6 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
instruments,anoisespikeoccurredresultingintheautomaticscram.Thescramreport
andCR37060documentedcorrectiveactions.
- 4. ScramReport2104
Anunscheduledshutdownoccurredat9:16AMon7/23/2021justafterreaching100%
power.Theoperatorbecamedistractedwhilerestoringtheplanttonormalsafetysystem
coincidencelogicafterperformingatestunderER2109duringthestartup.AReactor
SafetySystemscramwasautomaticallyinsertedbasedonthehighpowersignalfromone
powerpicoammeterinstrument.ThescramreportandCR37413documentedcorrective
actions.
- 5. ScramReport2105
Theoperatorperformedanunscheduledshutdownat10:09AMon10/15/2021.Shortly
afterreaching100%power,theoperatorobservedunexpected,fluctuatinginstrument
indicationsforreactorcoolantflow,reactorpower,andstackgaseousandparticulate
activities.Aprecautionarymanualshutdownwasperformed.ThescramreportandCR
38121documentedcorrectiveactions.
- 6. PriortoCriticality
On5occasionsduring2021,issueswithsafetyrodsoccurreduponinitialmovement
precludingareactorstartup.Threehadtodowithresistancetomovementofsafetyrod#4
(seeSectionIVItem4above)andtheothertwoinvolved1)theflexiblecoupling
disengagingonSR#4,and2)asafetyrodmagnetwirenutcominglooseonSR#2.All
occurrenceswereinvestigated,repairedandtheaffectedcomponentsretested
satisfactorily.TheFacilityManagerauthorizedreactorrestarts.
B. 2020TechnicalSpecificationViolationCited
NRCInspectionReport2021201citedaseverityLevelIVviolationpursuantto10CFR
55.59(a)(2)foralapsein2020oflicensedoperatorqualificationsresultingfromfailuretopass
anannualoperatingtestwithinthetimeconstraintsoftheapprovedrequalificationprogramas
per10CFR55.59(c).ThiswasreportedasEventNotification55113onFebruary24,2021and
furtherdescribedinthewrittenfollowupreportcontainedinGEHletterM210030dated
March10,2021.ThiseventisalsodescribedinNTRAnnualReportNo.61fortheYear2020.
Page 7 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
VI.RadiationLevelsandSampleResultsatOnSiteandOffSiteMonitoringStations
Thedatabelowarefromsampleanddosimeterresultsaccumulatedduringthe2021reporting
period.ExceptfortheNTRstackdata,thedatabelowcoverstheentireVNCsiteandinclude
theeffectsofoperationsotherthantheNTR.
A.
NTRStack
Totalairbornereleases(stackemissions)for2021areasfollows:
AlphaParticulate:1.11E08Ci(predominantlyradonthoriumdaughterproducts)
BetaGammaParticulate:4.93E07Ci
Iodine131:1.15E05Ci
NobleGases:1.30E+02Ci
NoblegasactivitiesrecordedfromtheNTRstackintegratebothbackgroundreadingsandthe
actualreleases.Backgroundreadingsmayaccountforasmuchas50%oftheindicatedrelease.
B.
GammaRadiation
Theyearlydoseresultsfortheyear2021asdeterminedfromevaluationofsiteperimeter
environmentalmonitoringdosimetersshowednodeparturefromnormalstablebackgrounds.
C.
Vegetation
Noalpha,beta,orgammaactivityattributabletoactivitiesattheNTRfacilitywasfoundonorin
vegetationinthevicinityofthesite.
D.
Water
Therewasnoreleaseofradioactivityinwaterortogroundwatergreaterthanthelimits
specifiedin10CFR20,AppendixB,Table2,andColumn2.
E.
OffSite
Theresultsofsamplescollectedfromoffsitelocationsindicatenormalbackgroundforthe
regionalarea.
Page 8 of 8 NTRAnnualReportNo.62Rev.1
April28,2022
VII.RadiationExposure
In2021,thehighestannualexposuretoanyfulltimeradiationworkerwhileworkingatNTRwas
0.718Remandthelowestexposureforthiscategoryofworkerwas0.019Rem.Theaverage
radiationexposureforthetenworkersinvolvedwas0.401Remperperson.
The2021totalradiationexposureforallworkerswhileperformingworkatNTRwas4.010Rem.
VIII.Conclusion
GEHitachiconcludesthattheNTRisstaffedandorganizedforefficientoperations.Extensive
useofourCorrectiveActionProgramwillcontinuecontributingtomakingusamoresafeand
compliantoperation.
GEHitachiNuclearEnergyAmericasLLC
VallecitosOperations
ThomasJ.McConnell,Manager
NuclearTestReactor
Thomas McConnell Digitally signed by Thomas McConnell DN: cn=Thomas McConnell, o=GE Hitachi, ou=NTR, email=thomas.mcconnell@ge.com, c=US Date: 2022.04.28 10:31:10 -07'00'