|
---|
Category:Deficiency Correspondence (per 10CFR50.55e and Part 21) Deficiency Report (per 10CFR50.55e and Part 21)
[Table view] Category:Letter
MONTHYEARIR 05000315/20240032024-10-31031 October 2024 Integrated Inspection Report 05000315/2024003 05000316/2024003 07200072/2024001 and Exercise of Enforcement Discretion IR 05000338/20240032024-10-28028 October 2024 – Integrated Inspection Report 05000338-2024003 and 05000339-2024003 ML24302A2402024-10-28028 October 2024 CFR 21 Report 1-BY-BC-1-LV Battery Charger ML24302A2342024-10-23023 October 2024 Request for Project Number Related to Dominion Energy Services New Nuclear Program at North Anna Power Station AEP-NRC-2024-77, U2C28 Steam Generator Tube Inspection Report2024-10-21021 October 2024 U2C28 Steam Generator Tube Inspection Report AEP-NRC-2024-80, Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Cask2024-10-15015 October 2024 Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Cask ML24283A0392024-10-0909 October 2024 Annual Submittal of Technical Specification Bases Changes Pursuant to Technical Specification 5.5.13.D ML24281A1372024-10-0707 October 2024 ISFSI - Submittal of Cask Registration for Spent Fuel Storage AEP-NRC-2024-79, Unit 2, Independent Spent Fuel Storage Installation - Registration of Dry Spent Storage Cask2024-09-26026 September 2024 Unit 2, Independent Spent Fuel Storage Installation - Registration of Dry Spent Storage Cask 05000338/LER-2024-001-01, Automatic Reactor Trip Due to Prni High Negative Rate2024-09-24024 September 2024 Automatic Reactor Trip Due to Prni High Negative Rate IR 05000338/20244202024-09-23023 September 2024 Security Baseline Inspection Report 05000338/2024420 and 05000339/2024420, Cover Letter AEP-NRC-2024-78, Reply to a Notice of Violation: EA-24-0472024-09-23023 September 2024 Reply to a Notice of Violation: EA-24-047 ML24243A0872024-09-20020 September 2024 Response to EPA Comments Regarding the Final Site Specific Supplement to the Generic Eist for License Renewal North Anna Power Station, Units 1 and 2 IR 05000338/20244022024-09-17017 September 2024 Security Baseline Inspection Report 05000338/2024402 and 05000339/2024402 05000316/LER-2024-002-01, Manual Reactor Trip Following Rapid Downpower for Steam Leak2024-09-12012 September 2024 Manual Reactor Trip Following Rapid Downpower for Steam Leak IR 05000315/20244022024-09-10010 September 2024 Security Baseline Inspection Report 05000315/2024402 and 05000316/2024402, Independent Spent Fuel Storage Installation Security Inspection Report 07200072/2024401 AEP-NRC-2024-69, Core Operating Limits Report2024-09-0909 September 2024 Core Operating Limits Report IR 05000315/20243012024-09-0505 September 2024 NRC Initial License Examination Report 05000315/2024301 and 05000316/2024301 ML24225A0022024-09-0303 September 2024 Issuance of Amendment Nos. 363 and 344 Revising Technical Specifications Section 3.8.1, AC Sources-Operating, for a One-Time Extension of a Completion Time IR 05000315/20240112024-08-30030 August 2024 NRC Inspection Report 05000315/2024011 and 05000316/2024011 and Notice of Violation AEP-NRC-2024-51, Annual Report of Loss-Of-Coolant Accident Evaluation Model Changes2024-08-28028 August 2024 Annual Report of Loss-Of-Coolant Accident Evaluation Model Changes AEP-NRC-2024-76, Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating2024-08-28028 August 2024 Unit 2 - Supplement to License Amendment Request for One-Time Extension of Completion Time for Inoperable AC Source - Operating ML24215A2622024-08-28028 August 2024 Transmittal Letter for Subsequent Renewed License IR 05000338/20240052024-08-27027 August 2024 Updated Inspection Plan for North Anna Power Station, Units 1 and 2 (Report 05000338/2024005 and 05000339/2024005) 05000316/LER-2024-003, Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage2024-08-22022 August 2024 Plant Shutdown Required by Technical Specifications Due to Reactor Coolant System Identified Leakage IR 05000315/20240052024-08-21021 August 2024 Updated Inspection Plan for Donald C. Cook Nuclear Plant, Units 1 and 2 (Report 05000315/2024005 and 05000316/2024005) 05000339/LER-2024-001-01, Loss of Generator Field for 2J Eog During 2-PT-82.282024-08-20020 August 2024 Loss of Generator Field for 2J Eog During 2-PT-82.28 ML24234A0742024-08-15015 August 2024 Notification of Deviation from Pressurized Water Reactor Owners Group (PWROG) Letter OG-23-63, NEI 03-08 Needed Guidance: PWR Thermal Shield Flexure Inspection Requirements AEP-NRC-2024-61, Unit 2 - Response to Request for Additional Information for Neutron Flux Instrumentation License Amendment Request2024-08-15015 August 2024 Unit 2 - Response to Request for Additional Information for Neutron Flux Instrumentation License Amendment Request ML24221A2702024-08-0808 August 2024 Unit 2 Independent Spent Fuel Storage Installation - Registration of Dry Spent Fuel Storage Cask ML24163A3002024-08-0808 August 2024 Request for Relief Request N1-I5-NDE-007 Inservice Inspection Alternative ML24206A0052024-08-0808 August 2024 SLR Final EIS Letter to Achp ML24206A0062024-08-0808 August 2024 Notice of Availability of the Final Environmental Impact Statement for the North Anna Nuclear Power Station Unit Numbers 1 and 2 Subsequent License Renewal (Docket Numbers: 50-338 and 50-339) ML24208A0142024-08-0808 August 2024 Tribal Section 106 Letters-North Anna-Absentee-Shawnee Tribe of Indians of Oklahoma ML24221A1812024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Catawba Indian Nation ML24221A1822024-08-0808 August 2024 Tribal Section 106 Letters - North Anna - Chickahominy Indian Tribe ML24221A1832024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Chickahominy Indian Tribe-Eastern Division ML24221A1842024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Delaware Nation, Oklahoma ML24221A1852024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Delaware Tribe of Indians ML24221A1872024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Eastern Shawnee Tribe of Oklahoma ML24221A1882024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Monacan Indian Nation ML24221A1862024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Eastern Band of Cherokee Indians ML24221A1912024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Rappahannock Tribe, Inc ML24221A1892024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Nansemond Indian Nation ML24221A1902024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Pamunkey Indian Tribe ML24221A1922024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Tuscarora Nation of New York ML24221A1942024-08-0808 August 2024 Tribal Section 106 Letters-North Anna-United Keetoowah Band of Cherokee Indians in Oklahoma ML24221A1932024-08-0808 August 2024 Tribal Section 106 Letters-North Anna - Upper Mattaponi Tribe AEP-NRC-2024-62, Unit 2, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Cask2024-08-0707 August 2024 Unit 2, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Cask ML24241A0692024-08-0606 August 2024 ISFSI, Submittal of Cask Registration for Spent Fuel Storage 2024-09-09
[Table view] |
Text
r '-. -
FLOWSERVE '_.
NUCLEAR PRODUCTS OPERATIONS 10 September 2021 Vernon Nuclear Pump Operations, Verno_n, CA 90058
INTERIM REPORT-FORMAL EVALUATION OF DEVIATIONS REPORTED
To: Document Control Desk, Nuclear Regulatory Commission From: Thomas Yim, Nuclear Products Operations Team Leader, Flowserve Vernon NPO
Reference:
RLCA09317; O-Ring -AEP-DC Cook Flowserve Pump Division, Vernon, CA, 90058
Subject:
Request for extension to complete Formal Evaluation processes in accordance with 1 0CFR21.21
Date of Discovery by Customer: 04 May 2021 Date of Notification to Flowserve: 04 May 2021 Initial Evaluation by Flowserve Material Review Board: 10 September 2021 Results of Initial Evaluation: Inconclusive with further investigation and information required; Internal
Reference:
Docket Number - 99901369; Flowserve Pump Division, Vernon CA, 90058
- During installation at customer site, a Flowserve Field Service representative observed poor fit up of the O-ring in question. Investigation revealed an incorrect O-ring size was specified on Flowserve Kalamazoo Drawing.
- Flowserve provided the correct O-ring as a warranty replacement and the Flowserve Kalamazoo drawing was revised.
- Flowserve conducted a delivery history of the subject O-Ring and determined that Dominion - North Anna was the only other site that had received this O-Ring. (North Anna had been notified that there was an evaluation pending and reported that their O-Rings were not being used in a Safety-Related system).
- A meeting was held by the Flowserve Material Review Board to conduct an initial evaluation of the reported incorrect O-ring and to identify the inputs required to conduct a formal evaluation for the condition's impact to safety.
- The inputs include those system-related attributes as provided by the owner, AEP - DC Cook.
- While Flowserve's internal and DC Cook's on-site external corrective actions have been completed, an internal audit of corrective actions revealed that a formal evaluation by Flowserve Engineering and DC Cook System Engineers for the condition's impact to safety had not been formally conducted and recorded.
- This is in violation of the Flowserve Quality Program which is focused on conducting evaluation activities in accordance with the discovery requirements of 1 0CFR21.21. Accordingly, there has been an internal Corrective Action initiated to capture this violation.
- Efforts are currently taking place between Flowserve and DC Cook to formally convene an MRB to disposition the errant O-Ring as a Deviation or Defect.
This request is to advise of the current status regarding the delivery and installation of an errant O-Ring and to request approval for an extension through the end of September 2021 to gather critical system-related information and to conduct the delinquent Formal Evaluation.
Cc: Scott Ford, Director, Global Quality, Flowserve Corp.
Tanya Dembekjian, Plant Manager, FLS Vernon James Wilson, Facility Quality Manager, FLS Charlotte Dave Gobbi, Flowserve Quality Consultant <-/"~
,~°o~~perations Team Leader Nuclear Products Operations Flowserve Corporation Email: tyim@flowserve.com Phone: (323) 217-7989