ML21105A419

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Reply to Notice of Violation
ML21105A419
Person / Time
Site: River Bend Entergy icon.png
Issue date: 04/15/2021
From: Karenina Scott
Entergy Operations
To:
Document Control Desk, NRC Region 4
References
RBG-480
Download: ML21105A419 (4)


Text

m EntergyOperations, inc.

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RiverBendStation 5485U.S.Highway 61N LA70775 StFrancisville, Tel225-381-4374 Kentscott GeneralManager PlantOperations RBG-48084 15,2021 April ATTN:Document ControlDesk U.S. Regulatory Nuclear Commission DC20555-0001 Washington,

Subject:

Reply toa NoticeofViolation; 2021010-03 River BendStation -

Unit 1 NRCDocket Nos. 50-458 Renewed Facility Operating License No. NPF-47

Reference:

NRCLetter toEntergy, "River BendStation Biennial ProblemIdentification andResolution Inspection Report 05000458/2021010 andNotice ofViolation" dated March18,2021(ADAMS Accession Number ML21064A220)

On March18,2021,theNRCtransmitted a Notice ofViolation toEntergy Operations, ine (Entergy).

Thecited wasfor violation Technical Specification 5.4.1.a for failuretomaintain procedures required Guide byRegulatory Revision 1.33, 2,Appendix A.Specifically, theNRCissued a violation for failure tomaintain adequate proceduresfor feedwater system operationonApril29, 2020, andthe failed licensee torestore compliance withina reasonable amount oftime.

TheEnclosureprovidesEntergy'sresponse totheNotice ofViolation. This informationis provided inaccordance with10CFR2.201.

Thisletter contains nonewregulatory commitments.

Shouldyouhaveany please questions, contact Mr. TimSchenk, Regulatory Assurance Manager, at 225-381-4177. /

Respectfully, KS/blj

Enclosure:

Reply toNoticeofViolation; 2021010-03 cc: NRCRegional Administrator -

Region IV NRCSenior Resident Inspector -

River BendStation

Enclosure RBG-48084 toa Notice Reply ofViolation; 2021010-03

RBG-48084 Enclosure Page 1of2 Entergy Operations, Inc.

Reply toa Notice ofViolation; 2021010-03 Byletter dated March 18, 2021toEntergy Operations, Inc. (Entergy),

theNuclear Regulatory Commission (NRC) issued "River Bend Station -

Biennial Problem Identification and Resolution Inspection Report 05000458/2021010 andNotice ofViolation" (ADAMS Accession Number ML21064A220).

Entergy concurswith the violation ascitedinthe Notice (NOV) ofViolation regarding Technical Specification 5.4.1.a forfailure to maintain procedures required byRegulatory Guide 1.33, Revision 2,Appendix A.Specifically, the NRCissued aviolation forfailuretomaintain adequate procedures for feedwater system operation onApril 29,2020, andthe licensee failed torestore within compliance a reasonable amount of time.

Inaccordance with 10CFR2.201, this enclosure provides Entergy'sreply totheNotice of Violation.

M During anNRCinspection conducted from January 25through February 12,2021, a violationof NRCrequirements wasidentified. Inaccordance with the NRCEnforcement Policy, theviolation islisted below:

Technical Specification 5.4.1.a, requires, inpart, thatprocedures shall beestablished, implemented, andmaintained covering theapplicable procedures recommended in Appendix A ofRegulatory Guide 1.33, Revision 2.Section 4.oofAppendix A to Regulatory Guide 1.33, Revision 2,requires instructions fortheoperation of the feedwater system.

Contrarytotheabove, from June1,2019, toFebruary 10,2021,thelicensee failed to establish,implement, and maintain applicable procedures recommended inAppendix A ofRegulatory Guide Revision 1 .33, 2, Section 4.o fortheoperation ofthe feedwater system. Specifically, thelicensee established Procedures SOP-0009, "Reactor Feedwater System (SYS #107)," Revision 80 82,andOSP-0053, "Emergency and Transient Response Support Procedure," Revision 27and28,tomeet theRegulatory Guide 1.33 requirement, andthe licensee failed tomaintainthese procedures for feedwater operation toinclude necessary precautions toprevent operation ofthesystem inanimproper lineup.

This violation isassociated with a Green SDPfinding.

Reason.for..the Violatio.n OnApril 29,2020 theNRCissued "River BendStation -

IntegratedInspection Report 05000458/2020001." Theinspection report documented a non-citedviolation (NCV 2020001-

03) for failure to maintain adequate procedures forf eedwater system operation because ofthe inspectors review ofa reactor scram that occurred onMay31,2019. Additional details were

RBG-48084 Enclosure Page 2of2 provided intheinspectionreport thattheNRCconcerns werespecific toSOP-0009, "Reactor Feedwater System," andOSP-0053, "Emergency andTransient Response Support Procedure."

Although the violation was documented initially inthe Corrective Action Program (CR-RBS-2020-00965) the condition report wasclosed tothetwoactions taken under CR-RBS-2019-03891 that addressed the causal evaluation forthereactor scram. All corrective actions were closed to NRC issuing inspection priorthe report05000458/2020001.

Uponreceipt oftheinspection report, RegulatoryAssurance personnel didnotrecognize that a newcondition report needed to begenerated toensure theadditional details associated with the NCVwereadequately addressed asrequired byEntergy procedure EN-Ll-123, "NRCInspection Support." Asa result correctiveactions werenot developed inaccordance with EN-LI-102, "Corrective Action Program," toadequately address correcting theSOP-0009 andOSP-0053 procedures.

Theidentified condition wasentered into Entergy'scorrective action program (CR-RBS-2021-00644).

Thefollowing corrective actions were taken:

Action 1: Revised OSP-0053, Emergency andTransient Response Support Procedure, hard card toensure Operators understand therequirements that atleast one LowPressure Heater Stringisinservice whenrestarting feedwater pumps.

Action 2: Revised SOP-0009, Reactor Feedwater System, toadd a precaution and limitation statement tonot attempt tostart a Reactor FeedPump unless at least oneLowPressure Heaterstring isvalved into service on the condensate side.

Asa result ofthe corrective actions taken, Entergycompleted the required changes tothe affected procedures, addressing therefore, the issueof concern and resulted in restoringfull compliance.

M Noadditional corrective actions havebeenidentified.

Entergy restored fullcompliance onFebruary 10,2021