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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 ML20140H0441997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Davis-Besse Nuclear Power Station Unit 1 ML20141B9521997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Davis-Beese Nuclear Power Station Unit 1 ML20137T5271997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20136G7221997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Davis-Besse Nuclear Station Unit 1 ML20134L9831997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Dbnps,Unit 1. W/Undated Ltr ML20133G0161996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20149M4071996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Davis-Besse Nuclear Power Station Unit 1 ML20134P9821996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20128Q0611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Davis-Besse NPP, Unit 1 ML20117D5341996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20117D5411996-06-30030 June 1996 Revised MOR for June 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20116E0161996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Davis-Besse Nuclear Station Unit 1 ML20113B9111996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Davis-Beese Nuclear Power Station Unit 1 ML20117H7231996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Davis-Besse Unit 1 ML20112E6061996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for David-Besse Nuclear Power Station,Unit 1 ML20101G5251996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DBNPS Unit 1 ML20149K7711996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Davis-Besse Nuclear Power Station.W/Undated Ltr ML20096C7971995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20095H3761995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20094L1041995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20093J2341995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Davis-Besse Nuclear Power Station ML20098A2651995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
Text
- - _ - - _..._._ _ _
s
. 1 TOLEDO EDISON '
o
- i EDIGON PLAZA JOO MADISON AVENUE '
TOLEDO. OHIO 43652-0001
~I 1
- June 15, 1989
')
KB89-00331 L
Docket No. 50-346 License No.'NPF-3
'I Document Control Desk 1
U. S. Nuclear Regulatory Commission 7920 Norfolk Avenue i
Bethesda, MD.
20555 i
Gentlemen:
Monthly Operating Report, May, 1989 Davis-Besse Nuclear Power Station Unit 1
)
Enclosed are ten copies of the Monthly Operating Report for Davis-Besse j
Nuclear Power Station Unit No. 1 for the month of May, 1989.
]
If you have any questions, please contact Bilal Sarsour at (419).321-7384.
Very truly yours, f
gfcup Louis F. Storz
~
'I I
Plant Manager
- Davis-Besse Nuclear Power Station BMS/mj b Enclosures
.,l l
cc Mr. A. Bert Davis i
Regional Administrator, Region III l
Mr. 1aul Byron l
NRC Resident Inspector-
- i l
Mr. T. V. Watabach NRC Senior Project Manager a
utve 8906210190 090531
[I 1
PDR ADOCK 0500 6
R I
m_________
_-_-_m_m___u_.___.___.2__
AVERAGE DAILY UNIT POWER LEVEL.
DOCKET NO.-
50-346-UNIT Davis-Besse #1- >
DATE June 15.-1989.
COMPLETED BY Bila1'Sarsour I
TELEPHONE '(419) 321-7384 L l
l i
MONTH May, 1989 DAY AVERAGE DAILY POWER LEVEL DAY
. AVERAGE DAILY POWER LEVEL '
(MWe-Net)
(MWe-Net) i 884' g7 882 2
885 gg.
883 3
887 19 877 4
884
- 20 876-5 883 21 879 6
888 22 877 7
854 23 880 8
883 24 878
[
9 880 25 878 10 886 26' 773-31 884 27 128 12 881 28 432-13 883 29.
797 14 884 30 821 15 885 3:
112 16 884 INSTRUCTIONS On this format. list the average daily unit power level in MWe-Net for each day iri the reporting month. Cornpute the nearest whole ruegawatt.
W/77) 4
OPERATING DATA REPORT DOCKET NO. 50-346 DATE June 15. 1989 COMPLETED BY Bilal Sarsour TELEPIIONE (419) 321-7384 OPERATING STATUS
- 1. Unit Name:
. Davis-Besse Unit #1 Notes
- 2. Reporting Period:
May, 1989
- 3. Licensed Thermal Power (MWt):
2772
- 4. Nameplate Rating (Gross MWe):
925
- 5. Design Electrical Rating (Net MWe):
906
- 6. Maximum Dependable Capacity (Gross MWe):
918
- 7. Maximum Dependable Capacity (Net MWe):
874
- 8. If Changes Octur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level To Which Restricted,If Any (Net MWe):
- 10. Reasons For Restrictions,if Any:
This Month Yr.-to.Date Cumulative
- 11. Hours in Reporting Period 744 3,623 94,992
- 12. Number Of Hours Reactor Was Critical 728.8 3,410.1 49,017.6
- 13. Reactor Reserve Shutdown Hours 15.2 89.0 5,393.7
- 14. Hours Generator Op-Line 709.4 3,369.6 47.063.4
- 15. Unit Reserve Shutdown Houn 0.0 0.0 1,732.5
- 16. Gmss Thermal Energy Generated (MWH) 1,878,751 9,030,511 110,899,900
- 17. Gross Electrical Energy Generated (MWH) 626,036 3,020,747 36,661,931
- 18. Net Electrical Energy Generated (MWH) 593,428 2.861.839 34.326.891
- 19. Unit Service Factor 95.3 93.0 49.5
- 20. Unit Availability Factor 95.3 93.0 51.4
- 21. Unit Capacity Factor (Using MDC Net) 91.3 90.4 41.3
- 22. Unit Capacity Factor (Using DER Net) 88.0 87.2 39.9
- 23. Unit Forced Outage Rate 3.4 4.5 30.9
- 24. Shutdowns Scheduled Oser Next 6 Months (Type Date,and Duration of Each t:
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior 1o Commercial Operation):
Forecast Achieved INITIA L CRITICALITY INITIAL ELECTRICITY CONIM ERCIA L OPER ATION (4/77 )
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L Operational Summary i
May, 1989 Reactor power was maintained at approximately 100% full power until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on May 7, 1989, when a manual power reduction was initiated to approximately 82% to perform Control Rod Drive (CRD) exercise testing.
l After the completion of the CRD exercise testing, reactor power was slowly increased to approximately 100% at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> on May 7, 1989.
Reactor. power was maintained at approximately 100% full power until 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on May 21, 1989, when a manual power reduction to approximately 96% power was i
l initiated to perform CRD exercise testing.
After the completion of the CRD exercise testing, reactor power was slowly increased to approximately 100% at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on May 21, 1989.
Reactor power was maintained at approximately 100% full pver until 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> l
on May 26, 1989, when a planned power reduction was initiated.
Reactor power was reduced to approximately 6% and the turbine generator was taken off line at 1138 hours0.0132 days <br />0.316 hours <br />0.00188 weeks <br />4.33009e-4 months <br /> on May 27, 1989.
During the power reduction, the following are the more significant activities performed:
1)
Added oil to Reactor Coolant Pump 2-2 lover motor bearing.
2)
Eliminated vest D-ring steam leak (SP9B1) by backseating the valve.
3)
Repairs to the Main Feedvater Control Valves (SP6A and SP6B).
4)
Low Pressure Condenser water box was cleaned.
The turbine generator was synchronized on line at 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> on May 27, 1989, and reactor power was slowly increased to 100% full power which was achieved at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on May 29, 1989.
Reactor power was maintained at approximately 100% full power until 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> on May 30, 1989, when a reactor trip occurred.
The reactor tripped on an Anticipatory Reactor Trip Signal (ARTS) caused by a trip of the main turbine.
The turbine tripped on low condenser vacuum shortly after the de-energization of two circulating water pumps. The circulating water pumps were de-energized when their breakers tripped on high phase differential current caused by an electrical fault that occurred at a splice in cable feed for a 480V transformer. This transformer is also powered from the e-m 13.8K? bus that powers the tripped circulating water pumps.
After identifying and. correcting the cause of the trip, reactor was taken critical at 0611 hours0.00707 days <br />0.17 hours <br />0.00101 weeks <br />2.324855e-4 months <br /> on May 31, 1989, the turbine generator was synchronized on line at 1520 hours0.0176 days <br />0.422 hours <br />0.00251 weeks <br />5.7836e-4 months <br /> on May 31, 1989, and reactor power was slowly increased to 100% full power.
3
REFUELING INFORMATION Dater May 1989 1.
Name of facility: ' Davis-Besse Unit 1 2.
Scheduled date for next refueling outage? February 1990 3.
Scheduled date for restart from current refueling:
June 1990 I
4.
Will. refueling or resumption'of operation-thereafter require a 1
technical specification change or other license amendment? If answer is yes, what in general vill these be? If answer is no, has the reload fuel' design and core configuration been reviewed by your Plant' q
Safety Review Committee to determine whether any unreviewed safety.
l questions are associated with the core reload (Ref. 10 CFR Section
]
50.59)?
1 Ans: A license amendment' request is planned to remove cycle-specific values from Section 3 of the Technical Specifications..This submittal is planned for June 1989 and vill be based on Generic Letter 88-16.
1 Assuming approval of this submittal by November 1989, no Cycle 7 I
Technical Specification changes are expected for Section 3 of the Technical Specifications. Cycle-specific changes to Section 2 of
)
Technical Specifications will likely be made. This depends on the i
d date of approval of a document on criteria and methodology, which is presently under development by the B&W Owners Group.
5.
Scheduled date(s) for submitting proposed licensing action and
-supporting information:
For Section 2, January, 1990.-
6.
Important licensing considerations associated with refueling, e.g.,
new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new j
operating procedures.
a.
Sixty Batch Reload 3.38% enriched instead of 60 Batch Reload.
b.
New fuel design Mark B8A (Reconstitutable, removable upper end fitting, Zircaloy grid spacer, debris resistant lover'end' cap, lover prepressurization, and annealed guide tubes.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool, and (c) the new fuel storage areas.
l (a) 177 (b) 268 (c) 0 6.
The present licensed spenti uel pool storage capacity and the size of-any f
increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
l Present:
735 Increased size by: 0 (zero) l 9.
The projected date of the last refueling that can be~ discharged to the spent fuel pool assuming the present licensed capacity.
Date:
1995 - assuming ability to unload the entire core into the' spent fuel pool is maintained
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