ML20244C993
| ML20244C993 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 03/31/1989 |
| From: | Bradham O, Haltiwanger J SOUTH CAROLINA ELECTRIC & GAS CO. |
| To: | Barry L NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 8904210091 | |
| Download: ML20244C993 (5) | |
Text
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Document Control. Desk March Monthly Operating Report-Page 1 ATTACHMENT I.
. AVERAGE DAILY UNIT POWER LEVEL.
DOCKET NO.: 50/395 UNIT:
V..C. SUMMER I' DATE: 04/03/89 COMPLETED BY:~ J. W. HALTIWANGER.
TELEPHONE:
(803)~345-4297 MARCH 1989 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1.
392 17.
-14 2.
376 18.
-13 3.
347 19.
-13 4.
361 20.
-14 5.
361 21.
-14' 6.
361 22.
-13 7.
362 23.
-15 8.
359 24.
-13 9.
360 25.
-14 10.
139 26.
-17 11.
-29 27.
-32 12.
-14 28.
-34 13.
-13 29.
-33 14.
-14 30.
-31 15.
-14 31.
86 1
16.
-15 nemmmed f@
R
Document Control Desk March Monthly Operating Report Page 2 ATTACHMENT II OPERATING DATA REPORT DOCKET N0.:
50/395' UNIT:
V. C. SUMMER I DATE: 04/03/89 COMPLETED BY:
J. W. HALTIWANGER TELEPHONE:
(803) 345_4297 OPERATTNG STATUS
- 1. Reporting. Period:
March 1989 Gross Hours in Reporting Period:
744' i
- 2. Currently Authorized Power Level (MWt):
2775 Max. Depend. Capacity (MWe-Net):
-885 Design Electrical Rating (MWe-Net):
900
- 3. Power Level to Which Restricted (If Any)(MWe-Net):
N/A
- 4. Reasons for Restrictions: N/A THIS MONTH YR TO DATE CUMULATIVE
- 5. Number of Hours Reactor Critical 277.2 1588.2 34324.8
- 6. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
- 7. Hours Generator on Line 241 '
1547.3 33630.0-
- 8. Unit Reserve Shutdown Hours C.y 0.0 0.0
- 9. Gross-Thermal Energy Generated (MMH) 318786 3280820 88129424 3
- 10. Gross Electrical Energy (MWH) 93430 1071020 29217849
- 11. Net Electrical Energy Generated (MWH)
,4923 999758 27686916
- 12. Reactor Service Factor 37.3 73.5 74.6
- 13. Reactor Availability Factor 37.3 73.5 74.6
- 14. Unit Service Factor 32.4 71.6 73.1
- 15. Unit Availability Factor 32.4 71.6 73.1
- 16. Unit Capacity Factor (Using MDC) 11.4 52.3 68.0
- 17. Unit Capacity Factor (Design MWe) 11.2 51.4 66.9
- 18. Unit Forced Outage Rate 67.6 28.4 7.6
- 19. Shutdowns Scheduled Over Next 6 Months (Type, Date & Duration of Each):
None
- 20. If Shut Down at End of Report Period, Estimated Date of Startup:
N/A
- 21. Units in Test Status (Prior to Commercial Operation): N/A f
L
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l Document Control Desk l
March Monthly Operating Report Page 3 i
ATTACHMENT III UNIT SHUTDOWNS AND POWER REDUCTIONS 1
DOCKET N0.:
50/395 UNIT:
V. C. SUMMER I DATE:
04/03/89 COMPLETED BY:
J. W. HALTIWANGER TELEPHONE:
(803) 345-4297 MARCH 1989 Method of TYPE Shutting j
F or S Duration Down the Corrective Actions /
No.
Date Reason Forced or (Hours)
Reactor or Comments Scheduled Reducing Power 3
890310 F
486.1 H
2 Clean up of secondary system.
4 890330 F
16.5 H
5 Adjusted moisture separator / reheater level switch.
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Document Control Desk
~ March Monthly Operating Report
-Page 4 h
ATTACHMENT IV NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE
'l DOCKET NO.:
50/395 1
UNIT:
V. C. SUMMER I
{
DATE:
04/03/89
{
COMPLETED BY:
J. W. HALTIWANGER
{
TELEPHONE:
(803) 345-4297 MARCH 1989 At the beginning of March 1989, the plant was operating at approximately 47 percent power to allow cleanup of steam generator water chemistry which was out of specification as a result of a resin intrusion event. This power level was maintained until March 10.
On March 10, at 1005 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.824025e-4 months <br />, a controlled manual shutdown was initiated. The generator was taken off line at 1225 hours0.0142 days <br />0.34 hours <br />0.00203 weeks <br />4.661125e-4 months <br /> and the plant entered Mode 3 at 1205.
The shutdown was initiated primarily to allow cleanup of steam generator water chemistry which could not be accomplished at power. The steam generators were sludge lanced and the remainder of the secondary system was flushed and cleaned.
On March 29, at 2255 hours0.0261 days <br />0.626 hours <br />0.00373 weeks <br />8.580275e-4 months <br />, the reactor was taken critical. The generator was placed on line at 1732 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.59026e-4 months <br /> on March 30. At 1819 hours0.0211 days <br />0.505 hours <br />0.00301 weeks <br />6.921295e-4 months <br />, the turbine tripped on indicated high moisture separator / reheater level. The generator was again placed on line at 1047 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.983835e-4 months <br /> on March 31.
At the end of March, the plant was at approximately 30 percent power, holding for steam generator chemistry cleanup.
- ,2 So th Cerotin2 Ehetric & Gas Company Crille. c dhIm enkin v le SC 29065 Nuclear Operations SCE&G L
April 7, 1989 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Attention: Mr.-Learned W. Barry
SUBJECT:
Virgil C. Summer Nuclear Station Docket No. 50/395 Operating License No. NPF-12 March tionthly Operating Report Gentlemen:
Please find enclosed the March 1989 Monthly Operating Remrt for the Virgil C.
Summer Nuclear Station Unit No. 1.
This sube.aittal is maoe in accordance with the requirements of Technical Specifications, Section 6.9.1.10.
If there are any questions, please call me at your convenience.
Very truly yours,
- 0. S. Bradham AMM/JWH/0SB:lcd Attachments c:
D. A. Nauman/0. W. Dixon, Jr./T. C. Nichols, Jr.
E. C. Roberts W. A. Williams, Jr.
INP0 Records Center S. D. Ebneter ANI Library J. J. Hayes, Jr.
L. N. Carter General Managers R. E. Rainear C. A. Price /R. M. Campbell, Jr.
J. W. Flitter R. B. Clary Marsh & McLennan K. E. Nodland NPCF J. C. Snelson NSRC G. O. Percival RTS (RG890002)
R. L. Prevatte File (818.03-1)
J. B. Knctts, Jr.
I \\
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