ML20244B845
| ML20244B845 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 02/08/1982 |
| From: | Widner W GEORGIA POWER CO. |
| To: | Office of Nuclear Reactor Regulation |
| Shared Package | |
| ML20236H997 | List: |
| References | |
| TAC-54378, TAC-54379, NUDOCS 8202160488 | |
| Download: ML20244B845 (2) | |
Text
.r n
q; fb]
[j'h3.f h ?fhh*k,.',
.l jg;., _
~
.Il
^^
- JGeg a Powe, Cornpany -
d M ?..A*hpJ (333 Pra?none Avenue (
y.
aw 2
~
JWi wania' Georps 30308,.
'y; y i Tetepnone 404 526g025 ?
F yr l
n J
' ; Masng Adoress, L
N
,, &> J V hg~ ;po,u Otsc, gy s$as.
a b
-f b $
i Aranta Georga 30302 p1 y
- Georgia PowerL 4
E 2 Wi A. Widner February 8, ?l982 >
- * * *'" #*C" " " '"
d by, ci; f V,cs Presiaenf and General Manager k
- f~~
' F0554 and Hycio Generahon u) ' 6 4
7
- .e m
Qj P
LRECEWED
. FEB161982* 5 a
Director;of tbclear Reactor Regulation
- U. 5., Nuclear Pegulatory Commission nr a mrrm m :a
- Washington, D. C.
20555/
- QN.
S
.c j
. NRC DOCKET.30-321 Id l
(
.g "J
-OPERATING LICENSE DPR-57
]
7.
EDWIN I. HATCH NUCLEAR PLANT UNIT l-IMMEDIATE' RELIEF FOR DRYWELL.INERTING-TECHNICAL SPECIFICATION h
-)
y~
Gentlemen-
, a
'1 Pursuanti to 10 CFR -50.90, as required by ~10 CFR 50.59(c), Georgia Power ;
i
. Company proposes 1 an amendment to the. Unit 1 Technical' Specifications
'l 1
(Appendix"A to the~ Operating ~ License).
Technical Specification 3.7. A.S.b - requires "withinithe 124-hour period :
/ subsequent to ' placing the reactor in the RUN mode following a' shutdown, the j
containment atmosphere ~ oxygen concentration shcIl be reduced to'less than 40 1
- byJvolume andLmaintained in this' condition".
However, during the startup.of February 7; L1982, Lit became apparent thatL there was ~an insufficient amount-
- i Lof' liquid nitrogen ' available to meetH this' 24-hour JLCO.
Additionally, j
resupplies ?are not available until after the 'LCO expires.'. We hereby request-1 a-one time extension :of the 24-hour-LCO to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> beginning at 3 'p.m'.
EST n,
on February 7, 1982.
Minimum levels '(2000 gallons) of nitrogen are being h,,
- mainta'ined to preserve operability of the Containment Atmosphere Dilution i
L(CAD). system per Technical Specification 3.7.A.6.b.
L Safety Evaluation'- Drywell Inerting b
The basis for a 24-hour requirement on attaining a 4 percent oxygen
- 1. <
~ concentration following. entry into the RUN mooe is to minimize the i
possibility of. hydrogen combustion.following a loss-of-coolant accident.
The 24-hour period was established, as stated in the bases for specification 3.7_. A.5,. as being suf ficient to perform necessary drywell inspections and establish-the required oxygen concentration.
The control is administrative and supplements the CAD system.
j i
3, i
p The CAD system provides the basis for assuring containment integrity
]
y
~
post LOCA.
Due. to the license date for Unit 1, the CAD system was installed l
to Lmeet. the then applicable regulations addressing. hydrogen evolution.
In I
- [X
.Q order to meet the currently applicable interim final rule, capability to q
q install portable hydrogen recombiners is being engineered, and, therefore, l
h/ g M*.7 orgia. Power.Comoany is in compliance with the regulations.
! pl l
bb
%'d B20208 PDR ADOCK 05000321 I b 0
[
WP PCR.
= -.
a
W2, LJ ;MMW+WFWWM+PPP, 7"
" w + w ' ~ m W 5 I
I l
+eg ll 9Y 1
y y
g$
ry -
m y s
m,,
i y y g.
m
..p ;
y[g.g m ; ",
p',<'
l : n' ' ' '
.'-,",b,
,7.
- ,gf t
q t.
-N Y '{
- d i s y-F
's
. 4. 7. t
- 1..
- n u
+
t at J4%GeorgisPo> wsr '
M'"
,v i
1
%yf 17 '
s !
g7e 5 M.
4 v..~.
m,
v~-
N JDirect$dof/ Nuclear. Reactor. Regulation,1 o
+
d@n... A 5
774 iUnS.Aiclear Regulatory Commission' >
F m,%. ym:,7,, < Washingtonf DC C.020535 ;
f:[
'JFebr0aryg,(1982f f,
,9 w
a e
N M R g agq Two
\\ ;
?
w$$W%
N
.n u
, ;.,.. w
%$e; ("g g4 Because3the (24-hourt limit X is h an l administrative ? control, m as ? opposed j to' l'
(providing "a /safetyffunction,duced 'bylallowing a'. : longer. period 'of time; margins of safety,f asi efine d
d~ dl hi
? Specifications,Jareinotfre to?
W 4%^
,,:completeidrywell;..'inerting-TheT safety marginbis ';providedj by7thei CAD; '
i a.c M
o+ ;
system.
, %p '
- Addit.ionally, l due [tof plarb factars,.:' af maximumithe'rmal power flevel* of.-
4
,x y
k@
4Mlesshth'an'[ 50 f percent? will 'be reached.duriiig ithe reque'sted periddi.of(" ?,Y
[
f C
A l
i
. Lextension. JWef estimate ithat :inithe expected ; rod pattern, marginst to Ethe l,,
i V:MAPLHCR limitMshouldLapproach 50 : percent,Jproviding i additionalFconservatism W. '
,f
,%y 1totthe analysis? accident' conditions.
s,-
y-g<
%,,,, 1 Extension 'ofithe drywell'inerting LCO Jalso necessitates anJe'xtenAion/of-..' y' ', y m
the: LCO} for TechnicalL Specificatiori; 3.7. A'.7. (1) dDrywell-SuppressionlChamber m
^
nr, ;, %
-Dif ferential. Pressurei t for. a.' like! time ' period.' Re' quired differential-M y
s.;
- pressurecannotbefestablisheduntil'inertingis-complete.D 7
3 s
s y 3 m
, g4 pni i jThis(submittai Jis; for immediate relief.: AL formal submittal,fincluding m *'
determination ^of amendment class,Lwill. follow.
o e
<..3 2 W, 1 W.E A. Widner ustates f that heJis Vicei President of...GeorgialPower Company cand,
?
Jis l authorized Jto? execute this; cath Lon; behalf of ' Georgia Po.wer L Company,5 and -
4 M
thatt to' the "bestiof his knowledge ' andL belief theJ facts set forth'in this '
'IB 1 M 11etter are true.,
a t
GEORGIA; POWER COMPANY-
}
S n.
m,
, /
' 'l By:
d 'a [,-
F N. 9
(
W. A. Widner r
"8c._
Sworni o and subscribed.before me this 8th day of February,1982.
D; 4
/ /
Notary Public, Georgia, State at Large
-Q My Commission E.xpires Sept. 20,1983 Q '/
gg 1
W f
Notary Public e
M m.
'RES/mb?
y y
E 9
- x'c :
M. Manry u
R. F. Rogers, III
~
J.:P. O'Reilly (Region II - NRC) q; '
- y
.h 1
g L
J 1
'O
- i [.'
I k N,
.I {l i fl ' ' ' '
,f l
_ - _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ - _ - - _