ML20236R726

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Forwards Insp Repts 50-277/98-06 & 50-278/98-06 on 980505-0622 & NOV Re Failure of Site Engineering Personnel to Take Prompt & Effective Corrective Actions to Change Several Procedures for Rhrs
ML20236R726
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 07/16/1998
From: Anderson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Rainey G
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
Shared Package
ML20236R728 List:
References
50-277-98-06, 50-277-98-6, 50-278-98-06, 50-278-98-6, NUDOCS 9807220242
Download: ML20236R726 (4)


See also: IR 05000277/1998006

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July 16, 1998

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Mr. G. Rainey, President

PECO Nuclear

Nuclear Group Headquarters

Correspondence Control Desk

P.O. Box 195

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Wayne, Pennsylvania 19087-0195

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SUBJECT:

NRC INSPECTION REPORT 50-277/98-06,50-278/98-06;

NOTICE OF VIOLATION

Dear _ M6 Rainey:
On June 22,1998,the NRC completed an inspection at the Peach Bottom Atomic Power

Station.JThe enclosed report presents the results of that inspection.

- During the seven-week ' period covered by this inspection period, your staff continued to

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operate both units at the Peach Bottom Atomic Power Station safely. The decision by your

staff to proceed with on-line scram solenoid pilot valve (SSPV) replacements reflected a

strong safety perspective and was prudent, based on the degraded conditions noted in

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laboratory analyses of the SSPV parts. We also considered the SSPV maintenance

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activities to be particularly well-executed. We observed that Nuclear Maintenance Division

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- technicians and operations personnel displayed good procedure usage and sound work

l practices.- Supervisory personnel also provided very good coordination and oversight.

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Based on the'results of this inspection, the NRC has determined that four violations of NRC

requirements occurred. ' These violations are cited in the enclosed Notice of Violation

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'(Notice) and the circumstances surrounding them are described in detail in the subject

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inspection report.

The first violation resulted from the trip relay for the Main Control Room Emergency

Ventilation (MCREV) radiation monitor not being in the tripped status for approximately

E 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> while the 'B' channel radiation monitor was inoperable. Operations personnel ~

failed to perform a positive verification that the relay tripped when a jumper was installed.

?The corrective actions from a similar event on July 10,1997, failed to prevent this event.

The second violation involved the failure of site engineering personnel to take prompt and

' effective corrective actions to change several procedures for the residual heat removal

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system which contained errors that were identified by Quality Assurance personnel. The

failure to revise the procedures resulted in a residual heat removal system valve being left

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incorrectly positioned when plant operators used an unrevised procedure on March 4,

1998. We are concerned'with the number of valve mispositioning events that continued to

occur during this inspection period. Please address any generic implications to other valve

mispositioning events and any comprehensive corrective actions for plant configuration

control issues in your response to this violation.

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9807220242 990716

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POR

ADOCK 05000277

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. OFFICIAL RECORD COPY

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G. Rainey

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The third violation resulted from Unit 3 recirculation flows being mismatched for over

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> following the runback of the 3A recirculation pump on June 7,1998 during an

electrical storm. This mismatched flow resulted in a violation of Technical Specification 3.4.1. We are concerned that during this event, operations and engineering personnel did

not understand that the mismatch in recirculation flows caused excessive vibration

stresses on the jet pumps and jet pump riser braces. They also failed to recognize that

Unit 3 was in single loop operation following the runback of the 3A recirculation pump.

The fourth violation occurred from the failure of operations personnel to verify that the

difference between the temperature of the reactor coolant in the recirculation loop to

be started and the coolant in the reactor pressure vessel was :s;50 F within 15 minutes

prior to each startup of a recirculation pump. The required technical specification

surveillance verification was not performed during six of the first recirculation pump starts

which occurred on both units from June 25,1996 until March 23,1998. In addition, on

October 29,1997, the Unit 3 temperature differential was 84*F within 15 minutes of the

recirculation pump start.

You are required to respor.d to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. The NRC will use your response, in part,

to determine whether further enforcement action is necessary to ensure compliance with

regulatory requirements.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter

and its enclosures will be placed in the NRC Public Document Room (PDR).

We appreciate your cooperation.

Sincerely,

Oriainal Signed by:

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Clifford J. Anderson, Chief

Projects Branch 4

Division of Reactor Projects

Docket Nos.: 50-277,50-278

License Nos.: DPR-44, DPR-56

Enclosures:

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1. Notice of Violation

2. Inspection Report No. 50-277/98-06and 50-278/98-06

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G. Rainey

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cc w/encis:

G. Edwards, Chairrnan, Nuclear Review Board and Director, Licensing

J. Doering, Vice President, Peach Bottom Atomic Power Station

J. B. Cotton, Vice President, Nuclear Station Support

R. Boyce, Director, Nuclear Quality Assurance

A. F. Kirby, lil, External Operations - Delmarva Power & Light Co.

M. Warner, Plant Manager, Peach Bottom Atomic Power Station

G. J. Lengyel, Manager, Experience Assessment

J. W. Durham, Sr., Senior Vice President and General Counsel

T. M. Messick, Manager, Joint Generation, Atlantic Electric

W. T. Henrick, Manager, External Affairs, Public Service Electric & Gas

R. McLean, Power Plant Siting, Nuclear Evaluations

J. Vannoy, Acting Secretary of Harford County Council

R. Ochs, Maryland Safe Energy Coalition

J. H. Walter, Chie' Engineer, Public Service Commission of Maryland

Mr. & Mrs. Dennis Hiebert, Peach Bottom Alliance

Mr. & Mrs. Kip Adams

Commonwealth of Pennsylvania

State of Maryland

TMI- Alert (TMIA)

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G. Rainey

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- Distribution w/encis:

H. Miller, RA/W. Axelson, DRA (1)

C. Anderson, DRP

D. Florek, DRP

R.Junod,DRP

Region I Docket Room (with concurrences)

Nuclear Safety Information Center (NSIC)

- NRC Resident inspector

PUBLIC

Distribution w/encls: (Via E-Mail)

B. McCabe, OEDO

R. Capra, PDI-2, NRR

inspection Program Branch, NRR (IPAS)

M. Thedani, PM, NRR

B. Buckley, NRR

R. Correia, NRR

F. Talbot, NRR

M. Campion, ORA

DOCDESK

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DOCUMENT NAME: G:\\ BRANCH 4\\PB\\PB980606. INS

.To receive a copy of this document, indicate in the box: "C" = Copy without

attachment /enclo@"E" = Copy with attachment / enclosure

"N" = No copy

OFFICE

Rl/DRP/M

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Rl/DRP

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_NAME

DFl@eis.

CAnderson (f4

DATE

07// M98

07//G/98

OFFICIAL RECORD COPY

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