ML20217D541

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Insp Rept 50-002/98-202 on 980223-27.Two Apparent Violations Noted & Being Considered for Escalated Enforcement Action. Major Areas Inspected:Aspects of Organization,Operations & Maint:Review & Audit Requalification Training & Procedures
ML20217D541
Person / Time
Site: University of Michigan
Issue date: 03/24/1998
From:
NRC (Affiliation Not Assigned)
To:
Shared Package
ML20217D535 List:
References
50-002-98-202, 50-2-98-202, NUDOCS 9803300058
Download: ML20217D541 (11)


See also: IR 05000002/1998202

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U.S. NUCLEAR REGULATORY COMMISSION

Docket No:

50-002

License No:

R-28

Report No:

50-002/98202 (DRPM)

Licensee:

University of Michigan

Facility Name:

Ford Nuclear Reactor

Location:

Ann Arbor, Michigan

Dates:

February 23-27,1998

Inspector:

T. M. Burdick, Reactor inspector

Approved by:

Marvin M. Mendonca, Acting Director

Non-Power Reactors and Decommissioning

Project Directorate

Division of Reactor Program Management /NRR

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EXECUTIVE SUMMARY

. Ford Nuclear Reactor

Report No. 50-002/98202(DRPM)

' This routine, announced inspection included aspects of organization, operations, and

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maintenance (39745); review and audit (40745); requalification training (69003); and

procedures (42745).

' Oraanhation. Onarations. and Maintenance

The licensee recently posted a vacancy announcement for the position of Reactor ~

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Manager. This vacancy was open since 1996 pending the University's review of the

Ford Reactor's future status,

e - Operations were temporarily interrupted periodically during the period due to

maintenance, refueling, and unplanned scrams,

Operating problems led the licensee to incorporate new preventive maintenance and

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surveillance for the pneumatic cylinder actuator for the ventilation dampers and its air

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supply into the regular schedule. (Section 1.0)

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Review. Audit. and Desian Chance Functions

e . The inspector identified what appeared to be an inadequate 10 CFR 50.59 review of one

design change affecting Technical Specifications (TS) and the Safety Analysis Report

(SAR) assumptions. This was an apparent violation. Also, the NRC was not notified of

this 10 CFR 50.59 problem as required by TS 6.2.2.b.2. This was also an apparent

violation. (Section 2.0)

Ooerator Reaunlification

e Operators were evaluated in accordance with the requalification program requirements.

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.(Section 3.0)

Procedures .

e Operators were familiar with procedures, and ' associated equipment and limits. An

inspector follow up item was identified on the consistency between operating procedure

guidance and a recently installed modification. (Section 4.0)

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REPORT DETAILS

Plant Summary

The Ford Nuclear Reactor at the University of Michigan continued to operate in support of

tescaing in the graduate and undergraduate programs and of various research and irradiation

services. The University concluded this past summer that future operation of the reactor

would be supported for the duration of the current license, such that a vacancy

announcement for the Reactor Manager position has been issued.

1.0 Organization, Operations, and Maintenance

a.

Insoection Scone (39745)

The inspection was to verify whether the licensee had maintained its organization

as required and whether operations and maintenance were consistent with

requirements.

b.

Finding.s_and Observations

The licensee has not had a permanently assigned Reactor Manager since 1996.

The Assistant Manager, Reactor Operations continued as the acting Reactor

Manager. The licensee recently posted a vacancy announcement for the position

of Reactor Manager as previously mentioned.

The reactor had been operated continuously for several hours during the svening

shift of October 4,1996, within 1.2"F of the reactor safety limit of 11VF reactor

inlet temperature as discussed further in Section 2.0. The licensed shift

supervisor responsible for that shift stated that operation that close to the safety

limit was within the procedural guidance and that it was done to avoid starting

and stopping the cooling tower fans, which causes the reactor pool temperature

to vary widely. This problem has recently been addressed by the installation of

one variable speed fan motor. When asked by the inspector, one of the more

recently licensed operators felt that operating so close to the safety limit was

inadvisable and preferred a larger margin to ensure it was not exceeded. Base'i on

the licensee's calculations the reactor would increase the pool temperature about

1*F every 3.5 minutes at full power without the secondary cooling system in

operation. Reactor pool and inlet temperature was logged by the operators every

two hours. A recent rod rundown was installed to prevent exceed.ng the limit

which is discussed in detailin Section 2.0, and associated operator procedure

guidance is discussed in Section 4.0. Observation of shift operations and

dircussion with shift operators indicated that they continued to be capable of

safely operating within prescribed guidelines.

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Preventive maintenance measures were recently added to the reactor maintenance

schedule and the building checklist involving the Reactor Building ventilation

damper air cylinder and air supply. Ventilation dampers were required to close

automatically on high radiation. The licensee had discovered that the cylinder

stroke was erratic during the freezing months and determined that excessive

moisture in the compressed air line to the cylinder was freezing. The air lines and

cylinder were covered with insulation and electric strip heaters were applied to the

cylinder. Air line moisture removal was added to the checklist at regular intervals.

Also, lubrication of the cylinder at regular intervals was added to the maintenance

schedule.

The reactor building experienced flooding to the beam port floor and the basement

when storm water from the adjacent campus grounds could not be

accommodated by the storm sewer system. The licensee concluded that blockage

that was found in the storm sewer caused the problem. Construction of multiple

new projects surrounding the Phoenix Memorial Lab had also reduced the soil area

to absorb runoff. A modification was approved to cap the storm drain off and to

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reroute nonradioactive drainage to the sanitary sewer. The licensee normally has

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not discharged any radioactive material to the sewer but in this case they did

because all of their storage capacity was filled by the flood water. Operation was

curtailed for about 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Further review of this event will take place during

the next inspection.

c.

Conclusion

The licensee was in compliance with the organization and staffing requirements.

Operators were aware of operating limits prescribed by the licensee. Operators

had varying responses to the procedure guidance discussed.

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2.0 Review, Audit, and Design Change Functions

a.

Insoection Scoce (40745)

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To verify that the licensee had established and conducted review and audit

functions required by the technical specifications and whether modifications to

the facility were consistent with 10 CFR 50.59 and technical specifications (TS).

b.

Observations and Findinos

The inspector reviewed modifications that were safety related.10 CFR 50.59

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required that the licensee perform a safety review before making changes to the

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facility. Any changes that affected the TS were required to be presented to the

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NRC before they were made to obtain necessary TS changes and modification

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approval as appropriate.

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(1) ~ 10 CFR 50.59 Review

The licensee had observed periodic primary cooling flow reductions. In response,-

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Ford Nuclear Reactor (FNR) Modification Request No.120ia primary cooling pump

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and motor replacement oombined with the pump discharge check valve internals

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removal was performed between April 8 and April 18,1996. It was presented to

the Safety Review Committee after completion since the licensee considered it a .

non-substantive modification.

- At the time of the installation the licensee determined in their 10 CFR 50.59

safety review that no TS were affected and no prior NRC approval or TS changes

were sought. The modification resulted in an increase in primary cooling flow rate

- of about 150 gallons per minuta (GPM). The licensee did not identify any adverse

effects to the reactor facility and normal operations resumed.

Operating Procedure 103 required that reactor inlet temperatures be maintained

within the prescribed band of greater than 90 and less than 116'F. On

October 4,1996, a shift crew observed that before automatic rundown actuation -

of the limiting safety system settings (LSSS) (required by TS 3.2) would occur at

a core outlet temperature of 129'F, reactor inlet temperature would have already

exceeded the TS safety limit (SL) of 116'F (all other SL and LSSS were satisfied).

On October 6,1996, the licensee documented the shift crew's observation and on

October 8,1996, confirmed that the LSSS may not prevent exceeding the SL

because of the increased flow rate and the resultant decrease in the temperatu're

rise across the core.

The inspector confirmed this assessment through review of the operating logs for

the period following the pump and valve modification. Reactor inlet temperriture

on October 4,19a6, was at 114.8'F while reactor outlet temperature was at

126.2'F. ' From this data the inspector concluded that, had the reactor pool

temperature been permitted to increase, the 129'F LSSS rod rundown would not

have prevented the 116*F SL from being exceeded. The licensee's safety analysis

- for the pump and valve modification failed to identify the modification's affects on

the TS LSSS rendering it ineffective in oreventing the reactor inlet SL from being

exceeded.

One root cause appears to have been the licensee's inadequate evalut!. tion of the

correlation between core flow and the reactor's safety limit of 116'F reactor

coolant inlet temperature and the 129 F LSSS core outlet temperatwe. Licensee

modification documentation did not address possible changes or idt/ntify any

changes in reactor cooling water temperatures. Another root causa may have

been that the SRC did not review and approve this modification prior to it being

completed.

The reactor has a SL and a LSSS of 900 GPM on the primary coolant flow rate.

Other applicable safety limits include: the 116*F reactor coolarst inlet

temperature,4.68 megawatts (Mw) reactor thermal power, and 18 feet of water

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above the top of the core. The basis of tlw safety limits was "that the calculated -

maximum cladding temperature in the bottom of the, hot channel of the most -

compact FNR core (25 elements) will not reach the boiling point of the water

' coolant."

As described in the Safety Analysis Report (SAR) Chapter 13, page 46, the LSSS'

set point was conservatively based upon a 2.0 Mw power level with a reactor

core temperature delta-T of 15'F, a 131'F reactor core coolant outlet

temperature, and an assumed 2'F instrument error.

For perspective, page 46 of the SAR conservatively concludes that "the reactor

can be safely operated at a power level of 2 Mw and a primary coolant flow rate -

as low as 164 gpm without exceeding the saturation temperature anywhere on

the fuel' plate cladding surfaces." Further, this section of the safety analysis

shows that calculated core outlet temperature could be as high as 151'F (more

than 20*F margin) before cladding' temperature would reach saturation

temperature with all other SL values at their TS limits.-

The risk of exceeding the reactor inlet temperature safety limit during the period

from April 18,1996, until corrective action to reduce the LSSS for reactor outlet

temperature was not high becau.se of operator procedure compliance. Procedure

guidance did require operation with pool temperature greater than 90 but less

than 116'F. Bulk pool temperature would not have changed rapidly. At 2.0 Mw

without secondary cooling, it would require about 3.5 minutes to increase 1*F.

Although the reactor was operated for several hours at greater than 114*F on

October 4,1996, the potential for exceeding the SL was minimal based on the

margins in the analyses and equipment setpoint conservatisms, procedural

requirements and operator training. However, the lack of full understanding of

regulatory requirements in the implementation of 10 CFR 50.59, and the

incomplete evaluation of the effects of the modification on tha system and the TS

are a concern. The licensee missed opportunities to identify the need for a TS

change during the original modification 10 CFR 50.59 evaluation and review, in

the SRC review, in post installation testing, and in five months of operation. This

is an apparent violation of 10 CFR 50.59 (a)(1) (VIO 50-002/98202-01).

(2)- Corrective Action

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On October 6,1996, the licensee documented a conversation with a member of

the shift crew regarding the possibility that the reactor outlet temperature rod

rundown LSSS may not have prevented the reactor inlet temperature from

exceeding the SL of 116*F. On October 8,1996, the licensee issued a temporary

operating instruction to shift crews instructing them that the LSSS for reactcr

outlet temperature must be reduced to 126"F to prevent.the 116*F SL from being

exceeded. The licenses stated that the delay between discussing the concern and

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taking corrective measures was due to evaluation of the operator's concern.

When the licensee finally discovered that the LSSS could not have performed as

designed, the reactor had been in that condition for more than five months. The

reactor had been operated continuously except for periodic maintenance and

refueling shutdowns.

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During an SRC meeting on April 29,1997, that discussed potential additional

considerations, the licensee discussed the possibility of restoring primary flow to

the original valuo which would have eliminated the problem with the LSSS set

point, but this was not considered further to date.

To permanently address the problem, FNR Modification Request No.123, was

designed to add a new rod rundown signal from the reactor core inlet instrument.

The TS SL for reactor inlet temperature is 116*F. The set point for the new

rundown was established at 114*F to avoid potentially exceeding the 116*F TS

SL considering an instrument error of 2*F. The modification was approved by the

SRC on June 30,1997, and installed on September 30,1997. At the time of

installation, the rod rundown set point for reactor outlet temperature was returned

to 129'F. Although this modification was meant to correct the problem with its

SL and the LSSS, the licensee safety review had determined no TS change was

required and NRC approval was not sought.

The licensee missed opportunities to identify the need for a TS change in several

subsequent design reviews after identification of the technical problem in October

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of 1996. However, it should be noted that the licenses took prompt and technical

sound corrective actions once the problem was identified in October of 1996.

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(3)

Reporting Requirernents

TS 6.6.2.b.2 requires that the licensee prepare a written report to the NRC and

forward it within 30 days when they discover any substantial variance from

performance specifications contained in the TS and SAR. As previously

described, the licensee identified the problem and took corrective action on or

about October 8,1996. The licenseo never sought to obtain from the NRC any

change to the TS LSSS nor was NRC notified of the problem. Failure to report the

observed condition after the October 1996 identification of the problem is a

Violation of TS 6.6.2.b.2 (VIO 50-002/98202-02).

A root cause was the apparent lack of understanding the licensee had of the

significance of the SL re!ationship to the LSSS as described in the SAR and

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required in the TS. The inspector determined by discussion with operators and

management that they did not fully understand the regulatory implications. The

Ass!stant Manager of Operations said he originally had the understanding that the

license safety limits needed to be met collectively but not individually. The FNR

has four safety limits: primary cooling flow rate, reactor coolant inlet

temperature, pool water level, and reactor power as previously discussed. His

understanding was based on the safety analysis and limits from the previous

licenso safety limits at the facility.

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Further, during conversations with three licensed operators, the inspector

identified that two of them were not aware of the actions required by 10 CFR 50.36 if a safety limit were exceeded although they were sensitive that it was a

license limit. The licensee committed to prepare a copy of 10 CFR 50.36 for

required reading by alllicensed operators.

(4) Other System Observations

The inspector observed that the pump and motor unit installation was not

consistent with the original design. The unit was strapped to the original bed

plate using metal banding material rather than with a bolted fastener arrangement

as originally installed. The motor electrical connector box cover was also missing.

Specifications for the original design were not available for review. The licensee

committed to evaluate these differences. This will be an inspector follow up item

(IFl 50-002/98202-03),

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Conclusions

The licensee failed to conduct a comprehensive safety review as required by

10 CFR 50.59 and f ailed to notify the NRC as required by TS when it identified an

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inadequate LSSS in accordance with the SAR analysis,

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3.0 Operator Requalification

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a.

Insoection Scoce (69003)

To determine that operator requalification activities and training were conducted

as required.

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b.

Observations and Findinos

All operators were actively enrolled in the requall'ication program according to the

licensee's approved program. Annual operating tests and written examinations

were acceptable and graded accurately.

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Conclusio_r1

Operators were evaluated in accordance with the requalification program

requirements.

4.0 Procedures

a.

Insoection Scoos (42745)

The inspection is to determine whether facility procedures met regulatory

requirements.

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Observations and Findings

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- The licensee operating procedure OP-103 " Reactor Operation, Maintenance, .

Systems, and Components," R32,05/09/95, step .12.10.5, permits bulk pool

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temperature operation at greater than 90*F but less than 116*F. ' The licensee

installed a modification which initiates a rod rundown at 114*F on September 30, .

1997. Operators questioned by the inspector regarding procedure guidance on

pool temperature were aware of the limits and the new actuation set point. The

inconsistency between the procedure and modified system is an inspector follow-

up item (IFl 50-002/98202-04).

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Conclusions

Operators were familiar with selected procedures, and associate'd equipment and

limits. An inspector follow up item on the consistency between equipment and

procedures was identified.

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5.0 Exit Meeting Summary

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.The inspector presented the inspection results to members of the licensee

management at an exit meeting on February 27,1998. The licensee acknowledged

the findings presented. : The inspector asked the licensee whether any material

examined during the inspection should be considered proprietary. None were

identified.

A second exit was conducted telephonically with the licensee on March 9,1998.

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Persons Contacted

University of Michiaan

+ 'R. Fleming

Director, Phoenix Memorial Laboratory

'B. Ducamp

Assistant Manager, Reactor Operations

'J.

Lee

Chair, Safety Review Committee

The inspector also contacted other technical and administrative staff personnel during the

inspection.

  • Denotes those attending the exit meeting on February 27,1998.

+ Denotes those on telephone exit meeting on March 9,1998,

insoection Procedures Used

IP39745 Class i Non-Power Reactor OrgarJ2ation, Operation, and Maintenance

IP40745 Class 1 Non-Power Review, Audit, and Design Change Function

IP69003 Class 1 Non-Power Reactor Operator Requalification Training

IP42745 Class i Non-Power Reactor Procedures

items Ooened and Closed

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50-002/98202-01

VIO

10 CFR 50.59 review failed to identify affected TS

50-002/98202-02

VIO

Licensee failed to notify NRC of TS and SAR variances

50-002/98202-03

IFl

Primary cooling pump not installed as original design

50-002/98202-04

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Licensee procedure guidance inconsistent with modification

List of Documents Reviewed

Administrative Procedures

Logs and Records

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Maintenance Procedures

Modification Records

Operating Procedures

Reactor Operating Licenses

Requalification Records

Safety Analysis Report

Safety Review Committee Minutes

Surveillance Procedures and Records

Technical Specifications

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List of Acronyms used

CFR

Code of. Federal Rogulations

DRPM

Division of Reactor Project Manrgement

LSSS

Umiting safety system setting-

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NRC

Nuclear Regulatory Commission

PDR

Public Document Room

SL

Safety limit

SRC

Safety Review Committee

TS

Technical Specification

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