ML20217A320

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Forwards Insp Repts 50-254/97-13 & 50-265/97-13 on 970731-0905 & Notice of Violation Re Failure to Relocate SRs from TSs to IST Program as Part of TSs Upgrade Program
ML20217A320
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 09/12/1997
From: Grobe J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Pearce L
COMMONWEALTH EDISON CO.
Shared Package
ML20217A325 List:
References
50-254-97-13, 50-265-97-13, NUDOCS 9709190131
Download: ML20217A320 (3)


See also: IR 05000254/1997013

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September 12, 1997

Mr. L. W. Pearce

Site Vice President

Quad Cities Station

Commonwealth Edison Company

22710 206th Avenue North

Cordova,IL 61242

SUBJECT:

NRC ENGINEERING INSPECTION REPORT 50 254/97013(DRS);

50-265/97013(DRS) AND NOTICE OF VIOLATION

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Dear Mr. Pearce:

On September 5,1997, the NRC completed an inspection at your Quad Cities Nuclear Power

Station. The purpose of the inspection was to review the post-modification testing of the

r'.tsidual heat removal service water (RHRSW) pumps' cut water and impeller modifications.

Additionally, your current inservice testing (IST) program related to the RHRSW pumps was

reviewed. The results of this inspection are presented in the enclosed report.

The inspectors noted that neither the post-modification testing nor the inservice testing ensured

the RHRSW pumps would perform within acceptable limits of applicable design documents.

Because of this, your staff was required to perform an operability evaluation of the RHRSW

pumps, in addition, your staff could not readily identify or explain the basis for the RHRSW

pump flow surveillance criteria which was in conflict with the Updated Final Safety Analysis

Report description of the RHRSW pumps.

The NRC identified one test control violation for falling to relocate the surveillance

requirements from technical specifications to your IST progism as part of your technical

specifications upgrade program (TSUP). This violation is a concern because the surveillance

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requirement for the RHRSW pumps provides a basis for determining the operability of the

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RHRSW system. The failure resulted in the operability status of tha RHRSW pumps not being

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verified by testing since TSUP inception. Further, the inspectors noted that test control and

surveillance problems have been identified in recent NRC inspections (Inspection Reports 50-

254/265/96017,50-2v/265/96020 and 50 254/265/97011) and corrective actions taken to date

have not precluded these problems.

The violation is cited in the enclosed Notice of Violation (Notice) and the circumstances

surrounding it are described in detailin the enclosed report. Please note that you are required

to respond to this letter and should follow the instructions specified in the enclosed Notice when

preparing your response, in your response please address how you have assured yourself that

other technical specification surveillance requirements were appropriately relocated to your IST

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L Pearce

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Septaber 12, 1997

program for other components that were affected by the TSUP. The NRC will use your

response, in part, to determine whether further enforcement action is necessary to ensure

compliance with regulatory requirements.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter and its

enclosures wiil be placed in the NRC Public Document Room.

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We will gladly discuss any questions you have concerning this inspection.

Sincerely,

/s/ J. A. Grobo

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-John A. Grobe, Acting Director

Division of Reactor Safety

Dockets No. 50-254; 50 265

Ucenses No. DPR-29; DPR-30

Enclosures:

1. Notice of Violation

2. Inspection Report 50 254/265/97013(DRS)

Sge Attached Distribution

DOCUMENT NAME: G:\\DRS\\QUA97013.DRS

To receive a copy of this document. Indicate in the box *C's Copy w/o attach /end *E= a Co)y w/ attach /enci *N* = No copy

OFFICE

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Rill:DRP .

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NAME-

Augsows/Guzman/kje -

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Jacobsoh/St'bble

DATE

09/O /97

09/io/97

09/10/97

09/17197 /

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OFFICIAL RECORD COPY

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L. Pearce

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septcrnber 12, 1997

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cc w/encls:

R. J. Manning, Executive Vice President,

Generation

M. Wallace, Senior Vice President,

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Corpo. ate Services

E. Kraft, Vice President, BWR Operations

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Llaison Officer, NOC BOD

D. A. Sager, Vice President,

Generation Support

D. Farrar, Nuclear Regulatory

Services Manager

1. Johnson, Licensing Operations Manager

Document Control Desk Licensing

Quad Cities Station Manager

C. C. Peterson, Regulatory Affairs Manager

Richard Hubbard

Nathan Schloss, Economist,

Office of the Attorney General

State Liaison Officer

Chairman, Illinois Commerce Commission

J. R. Bull, Vice President, General &

Transmission, MidAmerican Energy Company

Distribution:

Docket File.wlencly

SRI, Quad Cities w/ encl

TSS w/enci

lPUBLiC IE 01 w/enci

LPM, NRR w/enci

DOCDESK w/enci

OC/LFDCB w/ encl

A. B. Seach, Rlli w/enci

CAA1 w/ encl

DRP w/enci

J. L. Caldwell, Rlli w/enci

DRS w/enct

Rlll Enf. Coordinator w/enci

Rill PRR w/enci

R. A. Capra, NRR w/ encl