ML20216K008

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Forwards Insp Rept 50-346/97-201 on 970505-0620.No Violations Noted
ML20216K008
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 09/04/1997
From: Richards S
NRC (Affiliation Not Assigned)
To: Jeffery Wood
CENTERIOR ENERGY
Shared Package
ML20216K011 List:
References
50-346-97-201, NUDOCS 9709180173
Download: ML20216K008 (4)


See also: IR 05000346/1997201

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UNITED STATES

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NUCLEAR REQULATORY Commission

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September 4, 1997

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-Mr.-John K. Wood

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Vice-President - Nuclear, Davis-Besse

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Centerior Service Company

c/o Toledo Edison Company

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Davis Besse Nuclear Power Station

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5501 North State Route 2

Dak. Harbor, Ohio 43449-9760

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SUBJECit DAVIS-BESSE DESIGN INSPECT 10N'

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(NRC.INSPEC110N REPORT NO. 50-346/97-201)

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Dear Mr. Wood:

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.A design inspection at Davic-Besse was performed by the Special Inspection

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BranchoftheOfficeofNuclearReactorRegulation-(NRR)duringtheperiod

. April 14, 1997 through June 20, 1997, including on-site inspections during

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May 5-9, May 19-23, and June 9-20, 1997.

The team selected for inspection the

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high pressure injection (HPI) system and the low pressure injection (LPI)

functionsofthedecayheatremoval. system (DHRS).

The purpose of the

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~ inspection was to evaluate the ,apability of the systems to perform safety

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functions required by their design bases, the adherence to the design and

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licensing bases, and the consistency of the as-built configuration with the

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updated safety analysis report (USAR),

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The results'of this ins uction are presented in the enclosed report.

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inspection team noted t1at the mechanical, electrical, and instrumentation and

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control designs of the HPI and.LPI systems were adequate to provide the

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required emergency core cooling flow to mitigate design basis accidents, and

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concluded that the systems were capable of performing their safety functions.

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The team identified some weaknesses in the design process and installation of

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the systems.

For example: reverse flow testing of check valves DH81 and DH82

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on the-two LPI pump tuction linas from the borated water storage tank (BWST)

and seat leakage testing of stop check valves HP31 and.HP32'on the HPI pump

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recirculation lines were not done; and although your staff had identified the

deterioration of the BWST level transmitter support hardware in 1994, no

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. action was taken to remove, examine, _and replace the hardware until the

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inspection team expressed its concern on the condition of the supports. =The

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-team referred to NRR-staff for evaluation the issue of the acceptability of

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Lthe use of normally open safety-related valves as safety class interface

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between the HPI-system and: local pressure gages that were not seismically

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qualified.

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Mr. John K. Wood

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Other issues identified by the team included USAR discrepancies, weaknesses in

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periodic testing of battery chargers, lack of testing of inverters, not

including certain electrical components in the environmental qualification

program, and not revising an installation detail drawing af ter modifying the

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actuators for DHR cooler outlet and bypass valves.

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You have initiated measures to addresh the team's concerns.

In order for the

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NRC to coordinate follow-up inspections, please provide within 60 days of this

letter a schedule for com)1etion of your corrective actions for the open items

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listed in Appendix A of t.1e enclosed report,

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Any enforcement action resulting from this inspection will be handled by the

NRC Region ill office via separate correspondence.

As with all NRC inspections, we expect that you will evaluate the

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ap)1icability of the results of this inspection and the specific findings to

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olier systems and components.

In accordance with 10 CFR 2.790(a), a copy of this letter and the enclosure

will be placed in the NRC Public Document Room.

Should you have any questions

concerning the attached inspection report, please contact the project manager,

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Mr. A.G. Hansen at (301) 415-1390, or the inspection team leader, Mr. S.K.

Malur at (301) 415-2963.

Sincerely,

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Stuart A. Richards, Chief

Special Inspection Branch

Division of Inspection and Support Programs

Office of Nuclear Reactor Regulation

Docket No.:

50-346

Enclosure :

NRC Inspection Report No.: 50-346/97-201

cc:

see next page

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John K. Wood

Davis-Besse Nuclear Power Station

Toledo Edison Company

Unit No. 1

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Mary E. O'Reilly

Robert E. Owen, Chief

Centerior Energy Corporation

Bureau of Radiological Health

300 Madison Avenue

Service

Toledo, OH 43652

Ohio Department of Health

P.O. Box 118

James L. Freels

Columbus, OH 43266-0118

Manager - Regulatory Affairs

Toledo Edison Company

James R. Williams

Davis-Besse Nuclear Power Station

Chief of Staff

5501 North State - Route 2

Ohio Emergency Management Agency

Oak Harbor, 011 43449-9760

2055 West Dublin Granville Road

Columbus, OH 43235-2206

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Gerald Charnoff, Esq.

Shaw, Pittman, Potts

Donna Owens, Director

and Trowbridge

Ohio Department of Commerce

2300 N Street, NW.

Division of Industrial Compliance

Washington, DC 20037

Bureau of Operations & Maintenance

6606 Tussing Road

P.O. Box 4009

Regional Administrator

Reynoldsburg, OH 43068-9009

U.S. NRC, Region 111

801 Warrenville Road

Ohio Environmental Protection Agency

Lisle, IL 60523-4351

DERR--Compliance Unit

ATTN:

Zack A. Clayton

Robert B. Borsum

P.O. Box 1049

Babcock & Wilcox

Columbus, OH 43266-0149

Nuclear Power Generation Division

1700 Rockville Pike, Suite 525

State of Ohio

Rockville, MD 20852

Public Utilities Commission

180 East Broad Street

Resident inspector

Columbus, OH 43266-0573

U.S. Nuclear Regulatory Commission

5503 North State Route 2

Attorney General

Oak Harbor. OH 43449

Department of Attorney

30 East Broad Street

James H. Lash, Plant Manager

Columbus, OH 43216

Toledo Edison Company

Davis-Besse Nuclear Power Station

President, Board of County

5501 North State Route 2

Commissioner of Ottawa County

Oak Harbor, OH 43449-f760

Port Clinton, OH 43252

Roy P. Lessy, Jr.

Akin, Gump. Srauss, Hauer & Feld, LLP

1333 New Hampshire Ave., NW., Ste 400

Washington, DC 20036

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Distribution -

Docket files 50-346

PSIB R/F

BSheron, NRR

FPGillespie, NRR

SARichards, NRR

DPNorkin, NRR-

CERossi, AE00-

EAdensam, NRR

GHMarcus, NRR

AGHansen, NRR

CBoyle. NRR

SStasek, SRI

Regional Administrators

Regional Division Directors

Inspection Team

PUBLIC

ACRS (3)

.0GC (3)

15 Distribution

SPSB, NRR

PRAB,'RES

RAB, AE00

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